HL incident on 2012-04-08 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$1,560,277
Incident datetime
2012-04-08 22:04
Report number
Location
TX
Narrative
The station operator observed oil in the dike of tanks 21 and 22 during daily location inspection. The lines were isolated and free standing oil was removed prior to excavation. Line was hydro excavated and the leak was clamped the following morning. 1500 feet of 24 inch pipe from manifold a to tank #23 was removed and replaced. Line was put back into service on june 22, 2012. The removed pipe was sent to lab for metallurgical analysis. Metallurgical report on the pipe indicated internal corrosion was the reason for the leak. Additional corrosion inhibitor has been added to the injection point for this area to assist in mitigating the internal corrosion. Remediation was completed on the remaining contamination.
Detailed record list
Report Received Date
2012-05-09 00:00:00
Iyear
2012
Report Number
20120141
Supplemental Number
19599
Report Type
Supplemental Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2012-04-08 22:04:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
600
Intentional Release Bbls
0
Recovered Bbls
600
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2012-04-08 22:04:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2012-04-08 22:04:00
Restart Datetime
2012-06-22 15:00:00
On Site Datetime
2012-04-08 22:04:00
Nrc Rpt Datetime
2012-04-08 22:46:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
C75
Segment Name
Cushing West Terminal
Onshore State Abbreviation
Ok
Onshore Postal Code
74023
Onshore City Name
Cushing
Onshore County Name
Payne
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
24
Pipe Wall Thickness
0.281
Pipe Smys
65000
Pipe Specification
Api 5l
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Manufactured Year
1991
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Leak Type Other
Size Of A Dime
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
60000
Est Cost Prop Damage
1560277
Est Cost Emergency
63100
Est Cost Environmental
14950
Est Cost Other
0
Prpty
1698327
Accident Psig
20
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
It was obvious that operator was not at fault. Pipe was under atmospheric pressure at the time of the incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Water Acid Ind
Yes
Int Microbiological Ind
Yes
Int Metallurgical Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
No
Corrosion Coupons
No
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2006
Hydrtst Most Rcnt Pressure
364
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
S**** D****
Preparer Title
Senior Pipeline Compliance Engineer
Preparer Email
S******@e****.com
Preparer Telephone
713.381.6487
Prepared Date
2014-07-25 00:00:00
Authorizer Name
S**** D****
Authorizer Telephone
713.381.6487
Authorizer Title
Senior Pipeline Compliance Engineer
Authorizer Email
S******@e****.com
Narrative
The station operator observed oil in the dike of tanks 21 and 22 during daily location inspection. The lines were isolated and free standing oil was removed prior to excavation. Line was hydro excavated and the leak was clamped the following morning. 1500 feet of 24 inch pipe from manifold a to tank #23 was removed and replaced. Line was put back into service on june 22, 2012. The removed pipe was sent to lab for metallurgical analysis. Metallurgical report on the pipe indicated internal corrosion was the reason for the leak. Additional corrosion inhibitor has been added to the injection point for this area to assist in mitigating the internal corrosion. Remediation was completed on the remaining contamination.
Report Received Date 2012-05-09 00:00:00
Iyear 2012
Report Number 20120141
Supplemental Number 19599
Report Type Supplemental Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2012-04-08 22:04:00
Location Latitude 35.953247 Google Maps OpenStreetMap
Location Longitude -96.758858 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 600
Intentional Release Bbls 0
Recovered Bbls 600
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2012-04-08 22:04:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2012-04-08 22:04:00
Restart Datetime 2012-06-22 15:00:00
On Site Datetime 2012-04-08 22:04:00
Nrc Rpt Datetime 2012-04-08 22:46:00
Nrc Rpt Num 1008104 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name C75
Segment Name Cushing West Terminal
Onshore State Abbreviation Ok
Onshore Postal Code 74023
Onshore City Name Cushing
Onshore County Name Payne
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 24
Pipe Wall Thickness 0.281
Pipe Smys 65000
Pipe Specification Api 5l
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Manufactured Year 1991
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Leak Type Other Size Of A Dime
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 60000
Est Cost Prop Damage 1560277
Est Cost Emergency 63100
Est Cost Environmental 14950
Est Cost Other 0
Prpty 1698327
Accident Psig 20
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details It was obvious that operator was not at fault. Pipe was under atmospheric pressure at the time of the incident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Water Acid Ind Yes
Int Microbiological Ind Yes
Int Metallurgical Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering No
Corrosion Coupons No
Collected Data Ind No
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2006
Hydrtst Most Rcnt Pressure 364
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name S**** D****
Preparer Title Senior Pipeline Compliance Engineer
Preparer Email S******@e****.com
Preparer Telephone 713.381.6487
Prepared Date 2014-07-25 00:00:00
Authorizer Name S**** D****
Authorizer Telephone 713.381.6487
Authorizer Title Senior Pipeline Compliance Engineer
Authorizer Email S******@e****.com
Narrative The station operator observed oil in the dike of tanks 21 and 22 during daily location inspection. The lines were isolated and free standing oil was removed prior to excavation. Line was hydro excavated and the leak was clamped the following morning. 1500 feet of 24 inch pipe from manifold a to tank #23 was removed and replaced. Line was put back into service on june 22, 2012. The removed pipe was sent to lab for metallurgical analysis. Metallurgical report on the pipe indicated internal corrosion was the reason for the leak. Additional corrosion inhibitor has been added to the injection point for this area to assist in mitigating the internal corrosion. Remediation was completed on the remaining contamination.

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