HL incident on 2012-04-09 — OK

Operator
Oneok Ngl Pipeline Lp
Cause
Incorrect Operation
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$100
Incident datetime
2012-04-09 19:15
Report number
Location
OK
Narrative
At 19:15 on 4/09/2012, landowner called oneok pipeline control center in tulsa to report he could see vapors coming from oneok's pipe at the binger jct. #2 location. Field reps were contacted and dispacthed to site. Field rep arrived on site at approximately 19:35 and determined tattletale valve on scraper receiver trap was leaking. Scraper barrel was isolated and blown down. Defective tattletale was replaced. 10/16/2013 - requested by PHMSA david eng to change "apparent cause" to g7 "-incorrect operation". Oneok's incident investigation determined the leak orginated in the threads at, or near the base of the tattletale fitting. It is unknown whether these threads were defective from the factory, damaged during installation of the fitting, or possibly damaged during shipping and installation of the trap to the pipeline during construction. Oneok inspected other traps that were installed with this type fitting during the same time period and found all to be in good working order. 2/19/2014 - the pig trap and tattletale valve were originally installed february of 2012. Nj
Detailed record list
Report Received Date
2012-05-07 00:00:00
Iyear
2012
Report Number
20120139
Supplemental Number
19031
Report Type
Supplemental Final
Operator Id
Name
Oneok Ngl Pipeline Lp
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2012-04-09 19:15:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Y-Grade (Raw Feed)
Unintentional Release Bbls
1.84
Intentional Release Bbls
0.24
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2012-04-09 19:15:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Release Occurred On Pig Trap Barrel, Barrel Was Isolated
On Site Datetime
2012-04-09 19:35:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Oneok Binger Jct. 2
Segment Name
Granite Pipeline Receiver Trap
Onshore State Abbreviation
Ok
Onshore Postal Code
73059
Onshore City Name
Minco
Onshore County Name
Grady
Designated Location
Milepost/valve Station
Designated Name
7007+87
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Pipe Facility Type
Intrastate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Release Type
Leak
Leak Type
Crack
Leak Type Other
Crack In Fitting
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
73
Est Cost Prop Damage
100
Est Cost Emergency
150
Est Cost Environmental
0
Est Cost Other
0
Prpty
323
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage
Operation Type
Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage
Preparer Name
N*** J****
Preparer Title
Dot Compliance Coordinator
Preparer Email
N*********@o****.com
Preparer Telephone
580-395-6304
Preparer Fax
580-395-2933
Prepared Date
2014-02-19 00:00:00
Authorizer Name
N*** J****
Authorizer Telephone
580-395-6304
Authorizer Title
Dot Compliance Coordinator
Authorizer Email
N*********@o****.com
Narrative
At 19:15 on 4/09/2012, landowner called oneok pipeline control center in tulsa to report he could see vapors coming from oneok's pipe at the binger jct. #2 location. Field reps were contacted and dispacthed to site. Field rep arrived on site at approximately 19:35 and determined tattletale valve on scraper receiver trap was leaking. Scraper barrel was isolated and blown down. Defective tattletale was replaced. 10/16/2013 - requested by PHMSA david eng to change "apparent cause" to g7 "-incorrect operation". Oneok's incident investigation determined the leak orginated in the threads at, or near the base of the tattletale fitting. It is unknown whether these threads were defective from the factory, damaged during installation of the fitting, or possibly damaged during shipping and installation of the trap to the pipeline during construction. Oneok inspected other traps that were installed with this type fitting during the same time period and found all to be in good working order. 2/19/2014 - the pig trap and tattletale valve were originally installed february of 2012. Nj
Report Received Date 2012-05-07 00:00:00
Iyear 2012
Report Number 20120139
Supplemental Number 19031
Report Type Supplemental Final
Operator Id 32109 PHMSA Enforcement
Name Oneok Ngl Pipeline Lp
Operator Street Address 100 West Fifth Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2012-04-09 19:15:00
Location Latitude 35.34866 Google Maps OpenStreetMap
Location Longitude -98.09101 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Y-Grade (Raw Feed)
Unintentional Release Bbls 1.84
Intentional Release Bbls 0.24
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2012-04-09 19:15:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Release Occurred On Pig Trap Barrel, Barrel Was Isolated
On Site Datetime 2012-04-09 19:35:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Oneok Binger Jct. 2
Segment Name Granite Pipeline Receiver Trap
Onshore State Abbreviation Ok
Onshore Postal Code 73059
Onshore City Name Minco
Onshore County Name Grady
Designated Location Milepost/valve Station
Designated Name 7007+87
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Pipe Facility Type Intrastate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Release Type Leak
Leak Type Crack
Leak Type Other Crack In Fitting
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 73
Est Cost Prop Damage 100
Est Cost Emergency 150
Est Cost Environmental 0
Est Cost Other 0
Prpty 323
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage
Operation Type Damage By Operator Or Operator's Contractor Not Related To Excavation And Not Due To Motorized Vehicle/equipment Damage
Preparer Name N*** J****
Preparer Title Dot Compliance Coordinator
Preparer Email N*********@o****.com
Preparer Telephone 580-395-6304
Preparer Fax 580-395-2933
Prepared Date 2014-02-19 00:00:00
Authorizer Name N*** J****
Authorizer Telephone 580-395-6304
Authorizer Title Dot Compliance Coordinator
Authorizer Email N*********@o****.com
Narrative At 19:15 on 4/09/2012, landowner called oneok pipeline control center in tulsa to report he could see vapors coming from oneok's pipe at the binger jct. #2 location. Field reps were contacted and dispacthed to site. Field rep arrived on site at approximately 19:35 and determined tattletale valve on scraper receiver trap was leaking. Scraper barrel was isolated and blown down. Defective tattletale was replaced. 10/16/2013 - requested by PHMSA david eng to change "apparent cause" to g7 "-incorrect operation". Oneok's incident investigation determined the leak orginated in the threads at, or near the base of the tattletale fitting. It is unknown whether these threads were defective from the factory, damaged during installation of the fitting, or possibly damaged during shipping and installation of the trap to the pipeline during construction. Oneok inspected other traps that were installed with this type fitting during the same time period and found all to be in good working order. 2/19/2014 - the pig trap and tattletale valve were originally installed february of 2012. Nj

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