HL incident on 2012-04-04 — PA

Operator
West Shore Pipeline Co
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2012-04-04 06:22
Report number
Location
PA
Narrative
At 6:22 am cst on april 4, 2012 a release was identified by citgo refinery operations personnel at the citgo lemont refinery in lockport, il. Product was leaking from twin seal valves at the west shore pipe line company (wspl) unmanned meter station located within the citgo refinery. Refinery personnel immediately reported the release to wspl, and then to the buckeye control center. The line was isolated, emergency response procedures were initiated, and all appropriate notifications were made. Approximately 15 gallons of crude oil were released (contained within a tank dike) and 15 gallons were recovered. Impacted soil, gravel, and free liquids were removed and no further remediation is needed. The line is currently back in service. Supplemental/final report filed to populate field e5.F
Detailed record list
Report Received Date
2012-05-03 00:00:00
Iyear
2012
Report Number
20120133
Supplemental Number
17860
Report Type
Supplemental Final
Operator Id
Name
West Shore Pipeline Co
Operator Street Address
5 Tek Park
Operator City Name
Breinigsville
Operator State Abbreviation
PA
Operator Postal Code
18031
Local Datetime
2012-04-04 06:22:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.36
Intentional Release Bbls
0
Recovered Bbls
0.36
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2012-04-04 06:22:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2012-04-04 06:55:00
Restart Datetime
2012-04-04 20:56:00
On Site Datetime
2012-04-04 07:30:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Citgo Lemont Refinery
Segment Name
So257em
Onshore State Abbreviation
Il
Onshore Postal Code
60441
Onshore City Name
Lockport
Onshore County Name
Will
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Relief Valve
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Commercially Nav Ind
Yes
Commercially Nav Yes No
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
35000
Est Cost Environmental
0
Est Cost Other
0
Prpty
35000
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Preparer Name
J*** R*******
Preparer Title
Compliance Manager
Preparer Email
J********@b******.com
Preparer Telephone
610-904-4185
Preparer Fax
610-904-4545
Prepared Date
2013-04-10 00:00:00
Authorizer Name
J*** B* R*******
Authorizer Telephone
610-904-4185
Authorizer Title
Regulatory Compliance Manager
Authorizer Email
J********@b******.com
Narrative
At 6:22 am cst on april 4, 2012 a release was identified by citgo refinery operations personnel at the citgo lemont refinery in lockport, il. Product was leaking from twin seal valves at the west shore pipe line company (wspl) unmanned meter station located within the citgo refinery. Refinery personnel immediately reported the release to wspl, and then to the buckeye control center. The line was isolated, emergency response procedures were initiated, and all appropriate notifications were made. Approximately 15 gallons of crude oil were released (contained within a tank dike) and 15 gallons were recovered. Impacted soil, gravel, and free liquids were removed and no further remediation is needed. The line is currently back in service. Supplemental/final report filed to populate field e5.F
Report Received Date 2012-05-03 00:00:00
Iyear 2012
Report Number 20120133
Supplemental Number 17860
Report Type Supplemental Final
Operator Id 22430 PHMSA Enforcement
Name West Shore Pipeline Co
Operator Street Address 5 Tek Park
Operator City Name Breinigsville
Operator State Abbreviation PA
Operator Postal Code 18031
Local Datetime 2012-04-04 06:22:00
Location Latitude 41.658008 Google Maps OpenStreetMap
Location Longitude -88.041942 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.36
Intentional Release Bbls 0
Recovered Bbls 0.36
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2012-04-04 06:22:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2012-04-04 06:55:00
Restart Datetime 2012-04-04 20:56:00
On Site Datetime 2012-04-04 07:30:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Citgo Lemont Refinery
Segment Name So257em
Onshore State Abbreviation Il
Onshore Postal Code 60441
Onshore City Name Lockport
Onshore County Name Will
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Relief Valve
Release Type Leak
Leak Type Seal Or Packing
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Commercially Nav Ind Yes
Commercially Nav Yes No Yes
High Pop Ind Yes
High Pop Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 0
Est Cost Emergency 35000
Est Cost Environmental 0
Est Cost Other 0
Prpty 35000
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Equipment Not Installed Properly
Operation Type Equipment Not Installed Properly
Preparer Name J*** R*******
Preparer Title Compliance Manager
Preparer Email J********@b******.com
Preparer Telephone 610-904-4185
Preparer Fax 610-904-4545
Prepared Date 2013-04-10 00:00:00
Authorizer Name J*** B* R*******
Authorizer Telephone 610-904-4185
Authorizer Title Regulatory Compliance Manager
Authorizer Email J********@b******.com
Narrative At 6:22 am cst on april 4, 2012 a release was identified by citgo refinery operations personnel at the citgo lemont refinery in lockport, il. Product was leaking from twin seal valves at the west shore pipe line company (wspl) unmanned meter station located within the citgo refinery. Refinery personnel immediately reported the release to wspl, and then to the buckeye control center. The line was isolated, emergency response procedures were initiated, and all appropriate notifications were made. Approximately 15 gallons of crude oil were released (contained within a tank dike) and 15 gallons were recovered. Impacted soil, gravel, and free liquids were removed and no further remediation is needed. The line is currently back in service. Supplemental/final report filed to populate field e5.F

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