HL incident on 2012-04-07 — TX

Operator
Enbridge Energy, Limited Partnership
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$3,100
Incident datetime
2012-04-07 04:23
Report number
Location
TX
Narrative
On april 7 at approximately 04:23, the edmonton control center received a seal fail alarm on line 2 unit 4 at the cleabrook mn terminal. The unit was locked out and the gauger on duty was dispatched to the area. It was discovered that approximately 25 gallons of oil had leaked onto the pumphouse floor. Line 2 was shut down and the field investigation revealed that the pump seal had failed on unit 4. Line 2 was restarted at 07:50 local time using another pump. The inboard seal and outboard seal were replaced and the unit was ready for service later that same day.
Detailed record list
Report Received Date
2012-05-03 00:00:00
Iyear
2012
Report Number
20120131
Supplemental Number
18520
Report Type
Supplemental Final
Operator Id
Name
Enbridge Energy, Limited Partnership
Operator Street Address
915 N Eldridge Parkway, Suite 1100
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77079
Local Datetime
2012-04-07 04:23:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.6
Intentional Release Bbls
0
Recovered Bbls
0.6
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2012-04-07 04:23:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2012-04-07 04:23:00
Restart Datetime
2012-04-07 07:50:00
On Site Datetime
2012-04-07 04:40:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Clearbrook Terminal
Segment Name
Line 2 Unit 2.4
Onshore State Abbreviation
Mn
Onshore Postal Code
56634
Onshore City Name
Clearbrook
Onshore County Name
Clearwater
Designated Location
Milepost/valve Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Pump
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
3100
Est Cost Emergency
7000
Est Cost Environmental
0
Est Cost Other
0
Prpty
10100
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Preparer Name
S**** S****
Preparer Title
Compliance Analyst
Preparer Email
S**********@e*******.com
Preparer Telephone
218-464-5754
Preparer Fax
218-464-5992
Prepared Date
2013-09-09 00:00:00
Authorizer Name
D**** S*******
Authorizer Telephone
218-464-5751
Authorizer Title
Manager Us Pipeline Compliance
Authorizer Email
D*************@e*******.com
Narrative
On april 7 at approximately 04:23, the edmonton control center received a seal fail alarm on line 2 unit 4 at the cleabrook mn terminal. The unit was locked out and the gauger on duty was dispatched to the area. It was discovered that approximately 25 gallons of oil had leaked onto the pumphouse floor. Line 2 was shut down and the field investigation revealed that the pump seal had failed on unit 4. Line 2 was restarted at 07:50 local time using another pump. The inboard seal and outboard seal were replaced and the unit was ready for service later that same day.
Report Received Date 2012-05-03 00:00:00
Iyear 2012
Report Number 20120131
Supplemental Number 18520
Report Type Supplemental Final
Operator Id 11169 PHMSA Enforcement
Name Enbridge Energy, Limited Partnership
Operator Street Address 915 N Eldridge Parkway, Suite 1100
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77079
Local Datetime 2012-04-07 04:23:00
Location Latitude 47.68889 Google Maps OpenStreetMap
Location Longitude -95.41222 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.6
Intentional Release Bbls 0
Recovered Bbls 0.6
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2012-04-07 04:23:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2012-04-07 04:23:00
Restart Datetime 2012-04-07 07:50:00
On Site Datetime 2012-04-07 04:40:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Clearbrook Terminal
Segment Name Line 2 Unit 2.4
Onshore State Abbreviation Mn
Onshore Postal Code 56634
Onshore City Name Clearbrook
Onshore County Name Clearwater
Designated Location Milepost/valve Station
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Pipe Facility Type Interstate
Item Involved Pump
Release Type Leak
Leak Type Seal Or Packing
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 3100
Est Cost Emergency 7000
Est Cost Environmental 0
Est Cost Other 0
Prpty 10100
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Pump Or Pump-Related Equipment
Eq Failure Type Pump Or Pump-Related Equipment
Preparer Name S**** S****
Preparer Title Compliance Analyst
Preparer Email S**********@e*******.com
Preparer Telephone 218-464-5754
Preparer Fax 218-464-5992
Prepared Date 2013-09-09 00:00:00
Authorizer Name D**** S*******
Authorizer Telephone 218-464-5751
Authorizer Title Manager Us Pipeline Compliance
Authorizer Email D*************@e*******.com
Narrative On april 7 at approximately 04:23, the edmonton control center received a seal fail alarm on line 2 unit 4 at the cleabrook mn terminal. The unit was locked out and the gauger on duty was dispatched to the area. It was discovered that approximately 25 gallons of oil had leaked onto the pumphouse floor. Line 2 was shut down and the field investigation revealed that the pump seal had failed on unit 4. Line 2 was restarted at 07:50 local time using another pump. The inboard seal and outboard seal were replaced and the unit was ready for service later that same day.

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