GTG incident on 2012-11-23 — TX

Operator
Pvr Marcellus Gas Gathering, Llc
Cause
Equipment Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2012-11-23 03:05
Report number
Location
TX
Narrative
On friday, november 23rd at 3:00 am, a 4 inch anderson greenwood pressure relief valve on the inlet side of the chapin dehydration facility malfunctioned causing non-odorized gas to be released to the atmosphere. A pvr operator and the local fire department responded to the facility. The incident lasted for approximately 30 minutes before the local operator manually closed the block valve under the relief valve to stop the gas from venting. Since natural gas is lighter than air, the released volume quickly dissipated without any risk to the public, environment, or employees. An internal investigation team determined that the presence of ice in the pilot sensing line of the valve was likely the cause of the equipment malfunction. The valve was sent to a third party for further inspection and analysis. The third party could not definitively determine whether ice resulted in the malfunction. However, the report does state that ice could have very well been the primary causal factor. Due to redundant overpressure protection on this system, pvr does not plan to reinstall a valve at this location.
Detailed record list
Report Received Date
2012-12-20 00:00:00
Iyear
2012
Report Number
20120127
Supplemental Number
15720
Report Type
Supplemental Final
Operator Id
Name
Pvr Marcellus Gas Gathering, Llc
Operator Street Address
301 Commerce, Ste 700
Operator City Name
Fort Worth
Operator State Abbreviation
TX
Operator Postal Code
76102
Local Datetime
2012-11-23 03:00:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2012-11-28 19:17:00
Commodity Released Type
Natural Gas
Unintentional Release
5400
Intentional Release
0
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2012-11-23 03:26:00
Restart Datetime
2012-11-23 04:31:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2012-11-23 03:05:00
On Site Datetime
2012-11-23 03:21:00
On Off Shore
Onshore
Onshore State Abbreviation
Pa
Onshore Postal Code
18612
Onshore City Name
Dallas
Onshore County Name
Monroe Township
Pipe Fac Name
Wyoming 24" At Chapin Station
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Valve
Valve Type
Relief Valve
Installation Year
2012
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Faulty Relief Valve
Class Location Type
Class 2 Location
Could Be Hca
No
Pir Radius
637
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
21060
Est Cost Intentional Release
0
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Other
0
Prpty
21060
Accident Psig
1172
Mop Psig
1480
Mop Cfr Section
Not On Omb-Approved Form When Submitted
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
1
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Type A Gathering
Scada In Place Ind
No
Accident Identifier
Notification From Public
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Relief Valve Ind
Yes
Additional Defect Ind
Yes
Preparer Name
E***** S*********
Preparer Title
Safety And Regulatory Compliance Manager
Preparer Email
E**********@p**********.com
Preparer Telephone
5705053777
Preparer Fax
5705053798
Authorizer Name
E***** S*********
Authorizer Title
Safety And Regulatory Compliance Manager
Authorizer Telephone
5705053777
Authorizer Email
E**********@p**********.com
Narrative
On friday, november 23rd at 3:00 am, a 4 inch anderson greenwood pressure relief valve on the inlet side of the chapin dehydration facility malfunctioned causing non-odorized gas to be released to the atmosphere. A pvr operator and the local fire department responded to the facility. The incident lasted for approximately 30 minutes before the local operator manually closed the block valve under the relief valve to stop the gas from venting. Since natural gas is lighter than air, the released volume quickly dissipated without any risk to the public, environment, or employees. An internal investigation team determined that the presence of ice in the pilot sensing line of the valve was likely the cause of the equipment malfunction. The valve was sent to a third party for further inspection and analysis. The third party could not definitively determine whether ice resulted in the malfunction. However, the report does state that ice could have very well been the primary causal factor. Due to redundant overpressure protection on this system, pvr does not plan to reinstall a valve at this location.
Report Received Date 2012-12-20 00:00:00
Iyear 2012
Report Number 20120127
Supplemental Number 15720
Report Type Supplemental Final
Operator Id 32668 PHMSA Enforcement
Name Pvr Marcellus Gas Gathering, Llc
Operator Street Address 301 Commerce, Ste 700
Operator City Name Fort Worth
Operator State Abbreviation TX
Operator Postal Code 76102
Local Datetime 2012-11-23 03:00:00
Location Latitude 41.391058 Google Maps OpenStreetMap
Location Longitude -75.985302 Google Maps OpenStreetMap
Nrc Rpt Num 1031807 NRC Report How to search
Nrc Rpt Datetime 2012-11-28 19:17:00
Commodity Released Type Natural Gas
Unintentional Release 5400
Intentional Release 0
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind Yes
Shutdown Datetime 2012-11-23 03:26:00
Restart Datetime 2012-11-23 04:31:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2012-11-23 03:05:00
On Site Datetime 2012-11-23 03:21:00
On Off Shore Onshore
Onshore State Abbreviation Pa
Onshore Postal Code 18612
Onshore City Name Dallas
Onshore County Name Monroe Township
Pipe Fac Name Wyoming 24" At Chapin Station
Federal No
Location Type Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Valve
Valve Type Relief Valve
Installation Year 2012
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Faulty Relief Valve
Class Location Type Class 2 Location
Could Be Hca No
Pir Radius 637
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 21060
Est Cost Intentional Release 0
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Other 0
Prpty 21060
Accident Psig 1172
Mop Psig 1480
Mop Cfr Section Not On Omb-Approved Form When Submitted View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 1
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Type A Gathering
Scada In Place Ind No
Accident Identifier Notification From Public
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Relief Valve Ind Yes
Additional Defect Ind Yes
Preparer Name E***** S*********
Preparer Title Safety And Regulatory Compliance Manager
Preparer Email E**********@p**********.com
Preparer Telephone 5705053777
Preparer Fax 5705053798
Authorizer Name E***** S*********
Authorizer Title Safety And Regulatory Compliance Manager
Authorizer Telephone 5705053777
Authorizer Email E**********@p**********.com
Narrative On friday, november 23rd at 3:00 am, a 4 inch anderson greenwood pressure relief valve on the inlet side of the chapin dehydration facility malfunctioned causing non-odorized gas to be released to the atmosphere. A pvr operator and the local fire department responded to the facility. The incident lasted for approximately 30 minutes before the local operator manually closed the block valve under the relief valve to stop the gas from venting. Since natural gas is lighter than air, the released volume quickly dissipated without any risk to the public, environment, or employees. An internal investigation team determined that the presence of ice in the pilot sensing line of the valve was likely the cause of the equipment malfunction. The valve was sent to a third party for further inspection and analysis. The third party could not definitively determine whether ice resulted in the malfunction. However, the report does state that ice could have very well been the primary causal factor. Due to redundant overpressure protection on this system, pvr does not plan to reinstall a valve at this location.

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