GTG incident on 2012-10-15 — OK

Operator
Oneok Westex Transmission, Llc
Cause
Material Failure Of Pipe Or Weld
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,000
Incident datetime
2012-10-15 10:15
Report number
Location
OK
Narrative
Oneok westex transmission was conducting ecda confirmation digs on 6 inch diameter pipeline 0420-000 on monday october 15, 2012 utilizing a third party contractor. The contractor had uncovered the pipeline and two contractor personnel were in the ditch removing the old coating in preparation for recoating the pipeline. At approximately 1015 hours, the pipeline split open longitudinally releasing natural gas and the contractor personnel immediately left the ditch. There was no fire, no explosion, and no injuries. The local sheriff was notified and the 5-7 nearby structures were evacuated as a precautionary measure only. Line pressure at the time of the incident was 132 psi which was reduced to 84 psi to minimize hazards. Initial gas loss calculations and estimated repair costs were determined to be less than reportable limits. The railroad commission of texas was provided a courtesy call at 1236 hours. Further assessment of the damaged pipe resulted in a decision to repair via pipe replacement. This would cause a loss of natural gas service downstream of the incident site to the town of stanton with an estimated 850 customers. The national response center was provided a courtesy call at 1454 hours (incident number 1027378) based on the loss of service to the town of stanton. The railroad commission of texas was notified of the nrc incident number (texas incident number 755). The town of stanton went down at 1430 hours in preparation for the pipe replacement. Repairs were completed and evacuated structures released for occupancy by 1900 hours the same day. Full service to all customers and approval to relight occurred at 2145 hours. The delay between the completion of the pipe repair and relight was because a small 2 inch meter had to be utilized to pressure up the line and it took some time to achieve full line pressure. Further refined gas loss calculation results caused this incident to become reportable based on greater than 3 mmcf unintentional release of natural gas. The entire joint of pipe where the split occurred was replaced (total of 23.5 feet). A failure analysis is in process to determine the cause of the rupture. Update: failure analysis by external third party was inconclusive so the cause of the long seam weld failure could not be determined. In addition to the failure analysis of the failed longitudinal seam, a segment from the same joint of pipe adjacent to the seam failure portion was hydrotested to failure at 1500+ psig. Part g5 amended to reflect this. The incident costs and authorized signature information were also updated. This is a supplemental and final incident report.
Detailed record list
Report Received Date
2012-11-14 00:00:00
Iyear
2012
Report Number
20120112
Supplemental Number
16199
Report Type
Supplemental Final
Operator Id
Name
Oneok Westex Transmission, Llc
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2012-10-15 10:15:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2012-10-15 14:54:00
Commodity Released Type
Natural Gas
Unintentional Release
3649
Intentional Release
216
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2012-10-15 14:30:00
Restart Datetime
2012-10-15 21:45:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
10
Incident Identified Datetime
2012-10-15 10:15:00
On Site Datetime
2012-10-15 10:15:00
On Off Shore
Onshore
Onshore State Abbreviation
Tx
Onshore Postal Code
79705
Onshore City Name
Midland
Onshore County Name
Midland
Pipe Fac Name
0420-000
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Seam
Pipe Diameter
6.625
Pipe Wall Thickness
0.203
Pipe Smys
24000
Pipe Specification
Api 5l?
Pipe Seam Type
Lap Welded
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
1928
Manufactured Year
1928
Material Involved
Carbon Steel
Release Type
Rupture
Rupture Orient
Longitudinal
Rupture Length
19
Rupture Width
0.4
Class Location Type
Class 2 Location
Could Be Hca
No
Pir Radius
180
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
13027
Est Cost Intentional Release
771
Est Cost Prop Damage
2000
Est Cost Emergency
10000
Est Cost Other
0
Prpty
25798
Accident Psig
132
Mop Psig
307
Mop Cfr Section
Not On Omb-Approved Form When Submitted
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
92717
Internal Inspection Ind
No
Diameter Change Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Controllers or control room issues did not contribute to this incident. Oneok partners contractor personnel were onsite at the time of the incident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Pwjf Failure Type
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Metallurgical Ind
Yes
Other Analysis Ind
Yes
Other Analysis Details
See Part H Narrative
Other Factor
Yes
Other Factor Details
See Part H Narrative
Pwf Additional Other Ind
Yes
Additional Other Details
See Part H Narrative
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
1971
Hydrtst Most Rcnt Pressure
460
Direct Asmnt Conducted
Yes, And An Investigative Dig Was Cunducted At The Point Of The Accident
Direct Asmnt At Pnt Accdnt Yr
2012
Non Destructive Exam Ind
No
Preparer Name
P**** F***
Preparer Title
Senior Pipeline Safety Engineer
Preparer Email
P*********@o****.com
Preparer Telephone
918 588 7131
Preparer Fax
918 732 1311
Authorizer Name
W***** R* D*****
Authorizer Title
Vice President
Authorizer Telephone
918 588 7424
Authorizer Email
W*********@o****.com
Narrative
Oneok westex transmission was conducting ecda confirmation digs on 6 inch diameter pipeline 0420-000 on monday october 15, 2012 utilizing a third party contractor. The contractor had uncovered the pipeline and two contractor personnel were in the ditch removing the old coating in preparation for recoating the pipeline. At approximately 1015 hours, the pipeline split open longitudinally releasing natural gas and the contractor personnel immediately left the ditch. There was no fire, no explosion, and no injuries. The local sheriff was notified and the 5-7 nearby structures were evacuated as a precautionary measure only. Line pressure at the time of the incident was 132 psi which was reduced to 84 psi to minimize hazards. Initial gas loss calculations and estimated repair costs were determined to be less than reportable limits. The railroad commission of texas was provided a courtesy call at 1236 hours. Further assessment of the damaged pipe resulted in a decision to repair via pipe replacement. This would cause a loss of natural gas service downstream of the incident site to the town of stanton with an estimated 850 customers. The national response center was provided a courtesy call at 1454 hours (incident number 1027378) based on the loss of service to the town of stanton. The railroad commission of texas was notified of the nrc incident number (texas incident number 755). The town of stanton went down at 1430 hours in preparation for the pipe replacement. Repairs were completed and evacuated structures released for occupancy by 1900 hours the same day. Full service to all customers and approval to relight occurred at 2145 hours. The delay between the completion of the pipe repair and relight was because a small 2 inch meter had to be utilized to pressure up the line and it took some time to achieve full line pressure. Further refined gas loss calculation results caused this incident to become reportable based on greater than 3 mmcf unintentional release of natural gas. The entire joint of pipe where the split occurred was replaced (total of 23.5 feet). A failure analysis is in process to determine the cause of the rupture. Update: failure analysis by external third party was inconclusive so the cause of the long seam weld failure could not be determined. In addition to the failure analysis of the failed longitudinal seam, a segment from the same joint of pipe adjacent to the seam failure portion was hydrotested to failure at 1500+ psig. Part g5 amended to reflect this. The incident costs and authorized signature information were also updated. This is a supplemental and final incident report.
Report Received Date 2012-11-14 00:00:00
Iyear 2012
Report Number 20120112
Supplemental Number 16199
Report Type Supplemental Final
Operator Id 31531 PHMSA Enforcement
Name Oneok Westex Transmission, Llc
Operator Street Address 100 West Fifth Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2012-10-15 10:15:00
Location Latitude 32.07206 Google Maps OpenStreetMap
Location Longitude -101.92871 Google Maps OpenStreetMap
Nrc Rpt Num 1027378 NRC Report How to search
Nrc Rpt Datetime 2012-10-15 14:54:00
Commodity Released Type Natural Gas
Unintentional Release 3649
Intentional Release 216
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind Yes
Shutdown Datetime 2012-10-15 14:30:00
Restart Datetime 2012-10-15 21:45:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 10
Incident Identified Datetime 2012-10-15 10:15:00
On Site Datetime 2012-10-15 10:15:00
On Off Shore Onshore
Onshore State Abbreviation Tx
Onshore Postal Code 79705
Onshore City Name Midland
Onshore County Name Midland
Pipe Fac Name 0420-000
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Crossing No
Pipe Facility Type Intrastate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Seam
Pipe Diameter 6.625
Pipe Wall Thickness 0.203
Pipe Smys 24000
Pipe Specification Api 5l?
Pipe Seam Type Lap Welded
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Installation Year 1928
Manufactured Year 1928
Material Involved Carbon Steel
Release Type Rupture
Rupture Orient Longitudinal
Rupture Length 19
Rupture Width 0.4
Class Location Type Class 2 Location
Could Be Hca No
Pir Radius 180
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 13027
Est Cost Intentional Release 771
Est Cost Prop Damage 2000
Est Cost Emergency 10000
Est Cost Other 0
Prpty 25798
Accident Psig 132
Mop Psig 307
Mop Cfr Section Not On Omb-Approved Form When Submitted View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 92717
Internal Inspection Ind No
Diameter Change Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Controllers or control room issues did not contribute to this incident. Oneok partners contractor personnel were onsite at the time of the incident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Pwjf Failure Type Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Metallurgical Ind Yes
Other Analysis Ind Yes
Other Analysis Details See Part H Narrative
Other Factor Yes
Other Factor Details See Part H Narrative
Pwf Additional Other Ind Yes
Additional Other Details See Part H Narrative
Collected Data Ind No
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 1971
Hydrtst Most Rcnt Pressure 460
Direct Asmnt Conducted Yes, And An Investigative Dig Was Cunducted At The Point Of The Accident
Direct Asmnt At Pnt Accdnt Yr 2012
Non Destructive Exam Ind No
Preparer Name P**** F***
Preparer Title Senior Pipeline Safety Engineer
Preparer Email P*********@o****.com
Preparer Telephone 918 588 7131
Preparer Fax 918 732 1311
Authorizer Name W***** R* D*****
Authorizer Title Vice President
Authorizer Telephone 918 588 7424
Authorizer Email W*********@o****.com
Narrative Oneok westex transmission was conducting ecda confirmation digs on 6 inch diameter pipeline 0420-000 on monday october 15, 2012 utilizing a third party contractor. The contractor had uncovered the pipeline and two contractor personnel were in the ditch removing the old coating in preparation for recoating the pipeline. At approximately 1015 hours, the pipeline split open longitudinally releasing natural gas and the contractor personnel immediately left the ditch. There was no fire, no explosion, and no injuries. The local sheriff was notified and the 5-7 nearby structures were evacuated as a precautionary measure only. Line pressure at the time of the incident was 132 psi which was reduced to 84 psi to minimize hazards. Initial gas loss calculations and estimated repair costs were determined to be less than reportable limits. The railroad commission of texas was provided a courtesy call at 1236 hours. Further assessment of the damaged pipe resulted in a decision to repair via pipe replacement. This would cause a loss of natural gas service downstream of the incident site to the town of stanton with an estimated 850 customers. The national response center was provided a courtesy call at 1454 hours (incident number 1027378) based on the loss of service to the town of stanton. The railroad commission of texas was notified of the nrc incident number (texas incident number 755). The town of stanton went down at 1430 hours in preparation for the pipe replacement. Repairs were completed and evacuated structures released for occupancy by 1900 hours the same day. Full service to all customers and approval to relight occurred at 2145 hours. The delay between the completion of the pipe repair and relight was because a small 2 inch meter had to be utilized to pressure up the line and it took some time to achieve full line pressure. Further refined gas loss calculation results caused this incident to become reportable based on greater than 3 mmcf unintentional release of natural gas. The entire joint of pipe where the split occurred was replaced (total of 23.5 feet). A failure analysis is in process to determine the cause of the rupture. Update: failure analysis by external third party was inconclusive so the cause of the long seam weld failure could not be determined. In addition to the failure analysis of the failed longitudinal seam, a segment from the same joint of pipe adjacent to the seam failure portion was hydrotested to failure at 1500+ psig. Part g5 amended to reflect this. The incident costs and authorized signature information were also updated. This is a supplemental and final incident report.

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