HL incident on 2012-03-21 — OK

Operator
Magellan Pipeline Company, Lp
Cause
Material Failure Of Pipe Or Weld
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$38,500
Incident datetime
2012-03-21 19:17
Report number
Location
OK
Narrative
A third party telephoned the magellan operations control center to report a diesel odor in the vicinity of the pipeline near mile post 283.6. Subsequent investigation by magellan personnel discovered a very small crack near a girth weld, which was subsequently repaired. Metallurgical analysis of the pipe specimen indicated the cause was a lack of fusion defect in the erw longitudinal seam that linked up with an imbedded inclusion. The impacted soil was remediated in accordance with company and state standards. Approximately 1,043 cubic yards of soil was remediated.
Detailed record list
Report Received Date
2012-04-11 00:00:00
Iyear
2012
Report Number
20120108
Supplemental Number
21492
Report Type
Supplemental Final
Operator Id
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2012-03-21 18:00:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
12
Recovered Bbls
12
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2012-03-21 19:17:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2012-03-21 18:00:00
Restart Datetime
2012-03-25 17:00:00
On Site Datetime
2012-03-21 19:17:00
Nrc Rpt Datetime
2012-03-21 22:17:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
#6-12" Iowa City To Chicago Line
Segment Name
Line Id #6165
Onshore State Abbreviation
Il
Onshore Postal Code
60184
Onshore City Name
Wayne Township
Onshore County Name
Kane
Designated Location
Milepost/valve Station
Designated Name
283.6
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
32
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Seam
Pipe Diameter
12
Pipe Wall Thickness
0.25
Pipe Smys
42000
Pipe Specification
Api 5lx-42
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Jones & Laughlin
Pipe Coating Type
Coal Tar
Installation Year
1957
Manufactured Year
1957
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
79079
Est Cost Gas Released
8200
Est Cost Prop Damage
38500
Est Cost Emergency
70000
Est Cost Environmental
710721
Est Cost Other
0
Prpty
906500
Accident Psig
625
Mop Psig
963
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
275670
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Metallurgical Ind
Yes
Failure Type
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor
Yes
Other Factor Details
Lack Of Fusion Defect In The Erw Longitudinal Seam
Additional Crack Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2004
Geometry Recent Year
2004
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2007
Hydrtst Most Rcnt Pressure
1380
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
K****** L* L*******
Preparer Title
Sr. Compliance Coordinator
Preparer Email
K***********@m*********.com
Preparer Telephone
918-574-7315
Preparer Fax
918-574-7246
Prepared Date
2016-07-06 00:00:00
Authorizer Name
K****** L* L*******
Authorizer Telephone
918-574-7315
Authorizer Title
Sr. Compliance Coordinator
Authorizer Email
K***********@m*********.com
Narrative
A third party telephoned the magellan operations control center to report a diesel odor in the vicinity of the pipeline near mile post 283.6. Subsequent investigation by magellan personnel discovered a very small crack near a girth weld, which was subsequently repaired. Metallurgical analysis of the pipe specimen indicated the cause was a lack of fusion defect in the erw longitudinal seam that linked up with an imbedded inclusion. The impacted soil was remediated in accordance with company and state standards. Approximately 1,043 cubic yards of soil was remediated.
Report Received Date 2012-04-11 00:00:00
Iyear 2012
Report Number 20120108
Supplemental Number 21492
Report Type Supplemental Final
Operator Id 22610 PHMSA Enforcement
Name Magellan Pipeline Company, Lp
Operator Street Address 100 West 5th Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2012-03-21 18:00:00
Location Latitude 41.95138 Google Maps OpenStreetMap
Location Longitude -88.27772 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls 12
Recovered Bbls 12
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2012-03-21 19:17:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2012-03-21 18:00:00
Restart Datetime 2012-03-25 17:00:00
On Site Datetime 2012-03-21 19:17:00
Nrc Rpt Datetime 2012-03-21 22:17:00
Nrc Rpt Num 1006495 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name #6-12" Iowa City To Chicago Line
Segment Name Line Id #6165
Onshore State Abbreviation Il
Onshore Postal Code 60184
Onshore City Name Wayne Township
Onshore County Name Kane
Designated Location Milepost/valve Station
Designated Name 283.6
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 32
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Seam
Pipe Diameter 12
Pipe Wall Thickness 0.25
Pipe Smys 42000
Pipe Specification Api 5lx-42
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Jones & Laughlin
Pipe Coating Type Coal Tar
Installation Year 1957
Manufactured Year 1957
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 79079
Est Cost Gas Released 8200
Est Cost Prop Damage 38500
Est Cost Emergency 70000
Est Cost Environmental 710721
Est Cost Other 0
Prpty 906500
Accident Psig 625
Mop Psig 963
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 275670
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Metallurgical Ind Yes
Failure Type Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor Yes
Other Factor Details Lack Of Fusion Defect In The Erw Longitudinal Seam
Additional Crack Ind Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2004
Geometry Recent Year 2004
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2007
Hydrtst Most Rcnt Pressure 1380
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name K****** L* L*******
Preparer Title Sr. Compliance Coordinator
Preparer Email K***********@m*********.com
Preparer Telephone 918-574-7315
Preparer Fax 918-574-7246
Prepared Date 2016-07-06 00:00:00
Authorizer Name K****** L* L*******
Authorizer Telephone 918-574-7315
Authorizer Title Sr. Compliance Coordinator
Authorizer Email K***********@m*********.com
Narrative A third party telephoned the magellan operations control center to report a diesel odor in the vicinity of the pipeline near mile post 283.6. Subsequent investigation by magellan personnel discovered a very small crack near a girth weld, which was subsequently repaired. Metallurgical analysis of the pipe specimen indicated the cause was a lack of fusion defect in the erw longitudinal seam that linked up with an imbedded inclusion. The impacted soil was remediated in accordance with company and state standards. Approximately 1,043 cubic yards of soil was remediated.

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