GTG incident on 2012-09-24 — TX

Operator
Florida Gas Transmission Co
Cause
Corrosion Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$80,000
Incident datetime
2012-09-24 13:50
Report number
Location
TX
Narrative
Monday spetember 24th, 2012 during a routine aerial patrol, the pilot identified an area of dead vegitation with a small hole in the ground on the row upstream of the port lavaca station. Area personnel were dispatched to the location, and confirmation was made that the fgt 20" mainline did have a leak. Area personnel isolated the pipeline section and notifications were made. Plans were developed to investigate and repair the pipeline. A section of pipe was replaced and the pipeline section place back in service september 28th, 2012. **this report is being submitted in response to PHMSA's request, (docket id PHMSA-2013-0028), for supplemental reports from operators who submitted reports for incidents occurring after january 1, 2010, with any of the following: (1) ``pipe girth weld'' was selected as the ``item involved in incident'' in part c3 of the report. The revised report collects data about the pipe adjacent to the girth weld. (2) ``function of pipeline system'' is null in part e5f of the report. The revised report collects the function of the pipeline system for all incidents.** this supplemental report is to acknowledge that the two relevant sections in PHMSA's request have been reviewed and no further actions were needed.
Detailed record list
Report Received Date
2012-10-19 00:00:00
Iyear
2012
Report Number
20120105
Supplemental Number
16034
Report Type
Supplemental Final
Operator Id
Name
Florida Gas Transmission Co
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2012-09-24 13:50:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2012-09-25 16:41:00
Commodity Released Type
Natural Gas
Unintentional Release
750
Intentional Release
2486
Accompanying Liquid
1
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2012-09-24 17:26:00
Restart Datetime
2012-09-24 19:30:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2012-09-24 13:50:00
On Site Datetime
2012-09-24 15:40:00
On Off Shore
Onshore
Onshore State Abbreviation
Tx
Onshore Postal Code
77979
Onshore City Name
Port Lavaca
Onshore County Name
Calhoun
Designated Location
Milepost
Designated Name
174.75/2-4
Pipe Fac Name
Fgt 20"/txmwa-2
Segment Name
2-4-Aa / Txmwa-2-4
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
36
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
20
Pipe Wall Thickness
0.281
Pipe Smys
52000
Pipe Specification
Api-5lx
Pipe Seam Type
Longitudinal Erw - Low Frequency
Pipe Manufacturer
A.o. Smith
Pipe Coating Type
Coal Tar
Installation Year
1959
Manufactured Year
1959
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
430
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
2355
Est Cost Intentional Release
7806
Est Cost Prop Damage
80000
Est Cost Emergency
0
Est Cost Other
0
Prpty
90161
Accident Psig
862
Mop Psig
975
Mop Cfr Section
Not On Omb-Approved Form When Submitted
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Automatic
Length Segment Isolated
73212
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Air Patrol
Operator Type
Operator Employee
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Small leak discovered by patrol during routine flight. Leak confirmed by area personnel.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Galvanic Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
1959
Shielding Evident
Yes
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Close Interval Survey Ind
Yes
Other Cp Survey Ind
Yes
Cp Annual Survey Year
2012
Close Interval Survey Year
2012
Other Cp Survey Year
2012
Prior Damage
No
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Axial Recent Year
1997
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
1959
Hydrtst Most Rcnt Pressure
1227
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
N***** H******
Preparer Title
Director Interstate Regulatory Compliance
Preparer Email
N*************@e*************.com
Preparer Telephone
281-714-2231
Preparer Fax
281-714-2176
Authorizer Name
N***** H******
Authorizer Title
Director Interstate Regulatory Compliance
Authorizer Telephone
281-714-2231
Authorizer Email
N*************@e*************.com
Narrative
Monday spetember 24th, 2012 during a routine aerial patrol, the pilot identified an area of dead vegitation with a small hole in the ground on the row upstream of the port lavaca station. Area personnel were dispatched to the location, and confirmation was made that the fgt 20" mainline did have a leak. Area personnel isolated the pipeline section and notifications were made. Plans were developed to investigate and repair the pipeline. A section of pipe was replaced and the pipeline section place back in service september 28th, 2012. **this report is being submitted in response to PHMSA's request, (docket id PHMSA-2013-0028), for supplemental reports from operators who submitted reports for incidents occurring after january 1, 2010, with any of the following: (1) ``pipe girth weld'' was selected as the ``item involved in incident'' in part c3 of the report. The revised report collects data about the pipe adjacent to the girth weld. (2) ``function of pipeline system'' is null in part e5f of the report. The revised report collects the function of the pipeline system for all incidents.** this supplemental report is to acknowledge that the two relevant sections in PHMSA's request have been reviewed and no further actions were needed.
Report Received Date 2012-10-19 00:00:00
Iyear 2012
Report Number 20120105
Supplemental Number 16034
Report Type Supplemental Final
Operator Id 5304 PHMSA Enforcement
Name Florida Gas Transmission Co
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2012-09-24 13:50:00
Location Latitude 28.567233 Google Maps OpenStreetMap
Location Longitude -96.853967 Google Maps OpenStreetMap
Nrc Rpt Num 1025554 NRC Report How to search
Nrc Rpt Datetime 2012-09-25 16:41:00
Commodity Released Type Natural Gas
Unintentional Release 750
Intentional Release 2486
Accompanying Liquid 1
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind Yes
Shutdown Datetime 2012-09-24 17:26:00
Restart Datetime 2012-09-24 19:30:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2012-09-24 13:50:00
On Site Datetime 2012-09-24 15:40:00
On Off Shore Onshore
Onshore State Abbreviation Tx
Onshore Postal Code 77979
Onshore City Name Port Lavaca
Onshore County Name Calhoun
Designated Location Milepost
Designated Name 174.75/2-4
Pipe Fac Name Fgt 20"/txmwa-2
Segment Name 2-4-Aa / Txmwa-2-4
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 36
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 20
Pipe Wall Thickness 0.281
Pipe Smys 52000
Pipe Specification Api-5lx
Pipe Seam Type Longitudinal Erw - Low Frequency
Pipe Manufacturer A.o. Smith
Pipe Coating Type Coal Tar
Installation Year 1959
Manufactured Year 1959
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 430
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 2355
Est Cost Intentional Release 7806
Est Cost Prop Damage 80000
Est Cost Emergency 0
Est Cost Other 0
Prpty 90161
Accident Psig 862
Mop Psig 975
Mop Cfr Section Not On Omb-Approved Form When Submitted View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Automatic
Length Segment Isolated 73212
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Air Patrol
Operator Type Operator Employee
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Small leak discovered by patrol during routine flight. Leak confirmed by area personnel.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Galvanic Corrosion Ind Yes
Field Exam Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year 1959
Shielding Evident Yes
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Close Interval Survey Ind Yes
Other Cp Survey Ind Yes
Cp Annual Survey Year 2012
Close Interval Survey Year 2012
Other Cp Survey Year 2012
Prior Damage No
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Axial Recent Year 1997
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 1959
Hydrtst Most Rcnt Pressure 1227
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name N***** H******
Preparer Title Director Interstate Regulatory Compliance
Preparer Email N*************@e*************.com
Preparer Telephone 281-714-2231
Preparer Fax 281-714-2176
Authorizer Name N***** H******
Authorizer Title Director Interstate Regulatory Compliance
Authorizer Telephone 281-714-2231
Authorizer Email N*************@e*************.com
Narrative Monday spetember 24th, 2012 during a routine aerial patrol, the pilot identified an area of dead vegitation with a small hole in the ground on the row upstream of the port lavaca station. Area personnel were dispatched to the location, and confirmation was made that the fgt 20" mainline did have a leak. Area personnel isolated the pipeline section and notifications were made. Plans were developed to investigate and repair the pipeline. A section of pipe was replaced and the pipeline section place back in service september 28th, 2012. **this report is being submitted in response to PHMSA's request, (docket id PHMSA-2013-0028), for supplemental reports from operators who submitted reports for incidents occurring after january 1, 2010, with any of the following: (1) ``pipe girth weld'' was selected as the ``item involved in incident'' in part c3 of the report. The revised report collects data about the pipe adjacent to the girth weld. (2) ``function of pipeline system'' is null in part e5f of the report. The revised report collects the function of the pipeline system for all incidents.** this supplemental report is to acknowledge that the two relevant sections in PHMSA's request have been reviewed and no further actions were needed.

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