GTG incident on 2012-05-23 — CA

Operator
San Diego Gas & Electric Co
Cause
Other Outside Force Damage
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$36,000
Incident datetime
2012-05-23 09:43
Report number
Location
CA
Narrative
During planned pipeline blowdown, escaping gas ignited at location of overhead electrical facilities. Gas was shut off immediately, stopping fire. Non-energized static line dropped across roadway and was stuck by 2 vehicles. Drug and alcohol tests were performed on 8 sdg&e employees and 5 contractors. All passed. The immediate correction is to take an electric outage on all overhead electric circuits near blowdown sites. If that is not possible, a site evaluation will be performed by a qualified consultant to determine the safe distance whereby a blowdown may be performed. The permanent solution is to develop a set of guidelines listing the distances, voltages, weather conditions, etc., whereby blowdowns may be safely performed at any site. Any blowdown deviating from those guidelines would require a site-specific evaluation.
Detailed record list
Report Received Date
2012-06-15 00:00:00
Iyear
2012
Report Number
20120064
Supplemental Number
15684
Report Type
Supplemental Final
Operator Id
Name
San Diego Gas & Electric Co
Operator Street Address
8326 Century Park Court
Operator City Name
San Diego
Operator State Abbreviation
CA
Operator Postal Code
92123
Local Datetime
2012-05-23 09:43:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2012-05-23 11:30:00
Commodity Released Type
Natural Gas
Unintentional Release
0
Intentional Release
40
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
No
Shutdown Explain
Planned Blowdown Controlled By Closing Valve. Pipeline Still Energized
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2012-05-23 09:43:00
On Site Datetime
2012-05-23 09:43:00
On Off Shore
Onshore
Onshore State Abbreviation
Ca
Onshore Postal Code
92122
Onshore City Name
San Diego
Onshore County Name
San Diego
Designated Location
Milepost
Designated Name
45.73
Pipe Fac Name
Line 3010
Segment Name
Line 3010
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
1979
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Controlled Release Through Open Valve.
Class Location Type
Class 3 Location
Could Be Hca
Yes
Determination Method
Method2
Pir Radius
505
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
32000
Est Cost Unintentional Release
0
Est Cost Intentional Release
240
Est Cost Prop Damage
36000
Est Cost Emergency
1000
Est Cost Other
0
Prpty
69240
Accident Psig
51
Mop Psig
595
Mop Cfr Section
Not On Omb-Approved Form When Submitted
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
1
Internal Inspection Ind
No
Unsuitable Mainline Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Incident resulted from planned blowdown.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
Yes
Num Employees Tested
8
Num Employees Failed
0
Num Contractors Tested
5
Num Contractors Failed
0
Cause
Other Outside Force Damage
Cause Details
Nearby Industrial, Man-Made, Or Other Fire/explosion As Primary Cause Of Incident
Outside Force Type
Nearby Industrial, Man-Made, Or Other Fire/explosion As Primary Cause Of Incident
Preparer Name
W* J*** K*****
Preparer Title
Sr. Pipeline Safety Advisor
Preparer Email
W******@s**************.com
Preparer Telephone
213 305-8660
Preparer Fax
213 244-8155
Authorizer Name
W* J*** K*****
Authorizer Title
Sr. Pipeline Safety Advisor
Authorizer Telephone
213 305-8660
Authorizer Email
W******@s**************.com
Narrative
During planned pipeline blowdown, escaping gas ignited at location of overhead electrical facilities. Gas was shut off immediately, stopping fire. Non-energized static line dropped across roadway and was stuck by 2 vehicles. Drug and alcohol tests were performed on 8 sdg&e employees and 5 contractors. All passed. The immediate correction is to take an electric outage on all overhead electric circuits near blowdown sites. If that is not possible, a site evaluation will be performed by a qualified consultant to determine the safe distance whereby a blowdown may be performed. The permanent solution is to develop a set of guidelines listing the distances, voltages, weather conditions, etc., whereby blowdowns may be safely performed at any site. Any blowdown deviating from those guidelines would require a site-specific evaluation.
Report Received Date 2012-06-15 00:00:00
Iyear 2012
Report Number 20120064
Supplemental Number 15684
Report Type Supplemental Final
Operator Id 18112 PHMSA Enforcement
Name San Diego Gas & Electric Co
Operator Street Address 8326 Century Park Court
Operator City Name San Diego
Operator State Abbreviation CA
Operator Postal Code 92123
Local Datetime 2012-05-23 09:43:00
Location Latitude 32.84887 Google Maps OpenStreetMap
Location Longitude -117.18463 Google Maps OpenStreetMap
Nrc Rpt Num 101243 NRC Report How to search
Nrc Rpt Datetime 2012-05-23 11:30:00
Commodity Released Type Natural Gas
Unintentional Release 0
Intentional Release 40
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind No
Shutdown Explain Planned Blowdown Controlled By Closing Valve. Pipeline Still Energized
Ignite Ind Yes
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2012-05-23 09:43:00
On Site Datetime 2012-05-23 09:43:00
On Off Shore Onshore
Onshore State Abbreviation Ca
Onshore Postal Code 92122
Onshore City Name San Diego
Onshore County Name San Diego
Designated Location Milepost
Designated Name 45.73
Pipe Fac Name Line 3010
Segment Name Line 3010
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 1979
Material Involved Carbon Steel
Release Type Other
Release Type Details Controlled Release Through Open Valve.
Class Location Type Class 3 Location
Could Be Hca Yes
Determination Method Method2
Pir Radius 505
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 32000
Est Cost Unintentional Release 0
Est Cost Intentional Release 240
Est Cost Prop Damage 36000
Est Cost Emergency 1000
Est Cost Other 0
Prpty 69240
Accident Psig 51
Mop Psig 595
Mop Cfr Section Not On Omb-Approved Form When Submitted View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 1
Internal Inspection Ind No
Unsuitable Mainline Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Incident resulted from planned blowdown.
Employee Drug Test Ind Yes
Contractor Drug Test Ind Yes
Num Employees Tested 8
Num Employees Failed 0
Num Contractors Tested 5
Num Contractors Failed 0
Cause Other Outside Force Damage
Cause Details Nearby Industrial, Man-Made, Or Other Fire/explosion As Primary Cause Of Incident
Outside Force Type Nearby Industrial, Man-Made, Or Other Fire/explosion As Primary Cause Of Incident
Preparer Name W* J*** K*****
Preparer Title Sr. Pipeline Safety Advisor
Preparer Email W******@s**************.com
Preparer Telephone 213 305-8660
Preparer Fax 213 244-8155
Authorizer Name W* J*** K*****
Authorizer Title Sr. Pipeline Safety Advisor
Authorizer Telephone 213 305-8660
Authorizer Email W******@s**************.com
Narrative During planned pipeline blowdown, escaping gas ignited at location of overhead electrical facilities. Gas was shut off immediately, stopping fire. Non-energized static line dropped across roadway and was stuck by 2 vehicles. Drug and alcohol tests were performed on 8 sdg&e employees and 5 contractors. All passed. The immediate correction is to take an electric outage on all overhead electric circuits near blowdown sites. If that is not possible, a site evaluation will be performed by a qualified consultant to determine the safe distance whereby a blowdown may be performed. The permanent solution is to develop a set of guidelines listing the distances, voltages, weather conditions, etc., whereby blowdowns may be safely performed at any site. Any blowdown deviating from those guidelines would require a site-specific evaluation.

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