HL incident on 2012-01-22 — OK

Operator
Oneok Ngl Pipeline Lp
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$3
Incident datetime
2012-01-22 09:00
Report number
Location
OK
Narrative
At approximately 9:00 hrs. On 1/22/2012, on duty operator was making rounds at the oneok des moines storage facility and discovered a 1/2 inch blowdown valve in the manifold system blowing refinery grade butane (rgb) to the ground. Operator shutdown pipeline delivery and closed and plugged valve isolating the release. Pipeline delivery was restarted. Operator contacted management personnel to investigate and clean up release. Operator and contract employees were called in to recover product and remediate the area. Approximately 225 gallons of product was recovered from containment at facility and 7 1/2 drums of stained snow, soil and debris were picked up for disposal.
Detailed record list
Report Received Date
2012-02-03 00:00:00
Iyear
2012
Report Number
20120034
Supplemental Number
17301
Report Type
Supplemental Final
Operator Id
Name
Oneok Ngl Pipeline Lp
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2012-01-22 09:00:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Refinery Grade Butane (Rgb)
Unintentional Release Bbls
11.9
Intentional Release Bbls
0.1
Recovered Bbls
5.95
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2012-01-22 09:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2012-01-22 09:00:00
Restart Datetime
2012-01-22 09:10:00
On Site Datetime
2012-01-22 09:00:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Oneok Des Moines Storage Facility
Onshore State Abbreviation
Ia
Onshore Postal Code
50327
Onshore City Name
Pleasant Hill
Onshore County Name
Polk
Designated Location
Milepost/valve Station
Designated Name
Piping Header
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Installation Year
1995
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Plug Came Out Of Valve Allowing Product To Escape
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
890
Est Cost Prop Damage
3
Est Cost Emergency
1500
Est Cost Environmental
3000
Est Cost Other
0
Prpty
5393
Accident Psig
180
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Operator determined controller(s) actions had no part in the release. Operator investigation was incunclusive but believes a contributing factor could be vibration of the pipe header caused pipe plug to fall out of valve.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Threaded Fitting
Additional Vibration Ind
Yes
Additional Installation Ind
Yes
Preparer Name
N*** J****
Preparer Title
Dot Compliance Coordinator
Preparer Email
N*********@o****.com
Preparer Telephone
580-395-6304
Preparer Fax
580-395-2933
Prepared Date
2013-03-04 00:00:00
Authorizer Name
N*** J****
Authorizer Telephone
580-395-6304
Authorizer Title
Regulatory Compliance Coordinator
Authorizer Email
N*********@o****.com
Narrative
At approximately 9:00 hrs. On 1/22/2012, on duty operator was making rounds at the oneok des moines storage facility and discovered a 1/2 inch blowdown valve in the manifold system blowing refinery grade butane (rgb) to the ground. Operator shutdown pipeline delivery and closed and plugged valve isolating the release. Pipeline delivery was restarted. Operator contacted management personnel to investigate and clean up release. Operator and contract employees were called in to recover product and remediate the area. Approximately 225 gallons of product was recovered from containment at facility and 7 1/2 drums of stained snow, soil and debris were picked up for disposal.
Report Received Date 2012-02-03 00:00:00
Iyear 2012
Report Number 20120034
Supplemental Number 17301
Report Type Supplemental Final
Operator Id 32109 PHMSA Enforcement
Name Oneok Ngl Pipeline Lp
Operator Street Address 100 West Fifth Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2012-01-22 09:00:00
Location Latitude 41.56563 Google Maps OpenStreetMap
Location Longitude -93.526816 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Refinery Grade Butane (Rgb)
Unintentional Release Bbls 11.9
Intentional Release Bbls 0.1
Recovered Bbls 5.95
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2012-01-22 09:00:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2012-01-22 09:00:00
Restart Datetime 2012-01-22 09:10:00
On Site Datetime 2012-01-22 09:00:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Oneok Des Moines Storage Facility
Onshore State Abbreviation Ia
Onshore Postal Code 50327
Onshore City Name Pleasant Hill
Onshore County Name Polk
Designated Location Milepost/valve Station
Designated Name Piping Header
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Installation Year 1995
Material Involved Carbon Steel
Release Type Other
Release Type Details Plug Came Out Of Valve Allowing Product To Escape
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 890
Est Cost Prop Damage 3
Est Cost Emergency 1500
Est Cost Environmental 3000
Est Cost Other 0
Prpty 5393
Accident Psig 180
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Operator determined controller(s) actions had no part in the release. Operator investigation was incunclusive but believes a contributing factor could be vibration of the pipe header caused pipe plug to fall out of valve.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Threaded Connection/coupling Failure
Eq Failure Type Threaded Connection/coupling Failure
Other Stripped Ind Threaded Fitting
Additional Vibration Ind Yes
Additional Installation Ind Yes
Preparer Name N*** J****
Preparer Title Dot Compliance Coordinator
Preparer Email N*********@o****.com
Preparer Telephone 580-395-6304
Preparer Fax 580-395-2933
Prepared Date 2013-03-04 00:00:00
Authorizer Name N*** J****
Authorizer Telephone 580-395-6304
Authorizer Title Regulatory Compliance Coordinator
Authorizer Email N*********@o****.com
Narrative At approximately 9:00 hrs. On 1/22/2012, on duty operator was making rounds at the oneok des moines storage facility and discovered a 1/2 inch blowdown valve in the manifold system blowing refinery grade butane (rgb) to the ground. Operator shutdown pipeline delivery and closed and plugged valve isolating the release. Pipeline delivery was restarted. Operator contacted management personnel to investigate and clean up release. Operator and contract employees were called in to recover product and remediate the area. Approximately 225 gallons of product was recovered from containment at facility and 7 1/2 drums of stained snow, soil and debris were picked up for disposal.

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