GD incident on 2012-01-08 — KS

Operator
Black Hills Energy
Cause
Miscellaneous Root Causes
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 4 injuries
Property damage (nominal)
$10,000
Incident datetime
2012-01-08 09:03
Report number
Location
KS, HASKELL
Narrative
On sunday, january 8, 2012, at approximately 9:00 am there was a house explosion and subsequent fire located at 104 wooten street in sublette, ks. Two local company employees heard the explosion from their homes and reported to the site immediately. Upon arrival, bhe employees requested the assistance from local emergency management personnel to treat injuries and assist with evacuating the surrounding area. Seven people were home at the time of the explosion and four were taken to the hospital. Bar-hole testing was completed in the alley adjacent to the incident site and natural gas was detected. Bhe personnel took precautionary measures and shut off the east side of town in order to isolate the section of line. Service was shut off to approximately 250 customers. Bhe personnel continued to test for gas readings in the alley while other work was being performed. Bhe personnel restored gas to the eastern part of the system and began the re-lighting process that evening. Bhe personnel exposed the 2' coated steel main at each end of the alley and capped it off. A pressure test was then conducted on the main at utilization pressure (9 psi) and the line would not pressure up. Excavations began in the alley near the service line and tap to the incident site and then continued east along the main. The 2' main was uncovered and damage was found on the line approximately 15' from the aforementioned tap. It appears that the line had been previously damaged by a backhoe bucket. Damage to the steel line was seen under and along the sides of the steel pipe and what appeared to be a stress crack was noted across the entire bottom circumference of the pipe. Upon further excavation we discovered a sanitary sewer lateral crossing our line directly under the damaged area. The damaged section of pipe was secured and then removed from the site. There were no signs of recent excavation in the area.
Detailed record list
Occurred At
2012-01-08 09:03:00
Year
2012
Report Received Date
2012-02-06 00:00:00
Iyear
2012.0
Report Number
20120012.0
Supplemental Number
15511.0
Report Type
Supplemental Final
Operator Id
Name
Black Hills Energy
Operator Street Address
1102 E 1st Street
Operator City Name
Papillion
Operator State Abbreviation
NE
Operator Postal Code
68046-7641
Local Datetime
2012-01-08 09:03:00
Location Street Address
104 Wooten
Location City Name
Sublette
Location County Name
Haskell
Location State Abbreviation
KS
Location Postal Code
67877
Location Latitude
Location Longitude
Nrc Rpt Datetime
2012-01-08 10:35:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Fatality Ind
No
Fatal
0
Injury Ind
Yes
Num Emp Injuries
0
Num Contr Injuries
0
Num Er Injuries
0
Num Worker Injuries
0
Num Gp Injuries
4
Injure
4
Ignite Ind
Yes
Explode Ind
Yes
Num Pub Evacuated
15.0
Incident Identified Datetime
2012-01-08 09:03:00
On Site Datetime
2012-01-08 09:11:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
28.0
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Main
Installation Year
1964.0
Pipe Diameter
2.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Wt Steel
0.154
Release Type
Mechanical Puncture
Puncture Axial
1.0
Puncture Circum
3.0
Class Location Type
Class 3 Location
Est Cost Oper Paid
125000.0
Est Cost Prop Damage
10000.0
Est Cost Emergency
20000.0
Est Cost Other
25000.0
Est Cost Other Details
Replaced Line In Alley
Est Cost Unintentional Release
2500.0
Prpty
182500.0
Commercial Affected
30.0
Industrial Affected
0.0
Residences Affected
220.0
Accident Psig
9.0
Normal Psig
9.0
Mop Psig
9.5
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Previous Damage Due To Excavation Activity
Ex Party Type
Previous Damage Due To Excavation Activity
Ex Hydrotest Leak Survey Date
2011-11-11 00:00:00
Ex Hydrotest Conducted Ind
No
Notify Cga Dirt
No
Public Row Ind
Yes
Public Subtype
Other
Excavator Type
Unknown/other
Excavator Equipment
Backhoe/trackhoe
Work Performed
Sewer (Sanitary/storm)
One Call Notified Ind
No
Locator Type
Unknown/other
Visible Marks
Unknown/other
Service Interruption
No
Root Cause Category
Miscellaneous Root Causes
Root Cause Type
Previous Damage
Preparer Name
J**** W******
Preparer Title
Senior Manager Of Technical Services
Preparer Email
J************@b*************.com
Preparer Telephone
316-941-1642
Preparer Fax
402-829-2790
Authorizer Name
V**** C******
Authorizer Title
General Manager Kansas Gas
Authorizer Telephone
785-832-3950
Authorizer Email
V************@b*************.com
Narrative
On sunday, january 8, 2012, at approximately 9:00 am there was a house explosion and subsequent fire located at 104 wooten street in sublette, ks. Two local company employees heard the explosion from their homes and reported to the site immediately. Upon arrival, bhe employees requested the assistance from local emergency management personnel to treat injuries and assist with evacuating the surrounding area. Seven people were home at the time of the explosion and four were taken to the hospital. Bar-hole testing was completed in the alley adjacent to the incident site and natural gas was detected. Bhe personnel took precautionary measures and shut off the east side of town in order to isolate the section of line. Service was shut off to approximately 250 customers. Bhe personnel continued to test for gas readings in the alley while other work was being performed. Bhe personnel restored gas to the eastern part of the system and began the re-lighting process that evening. Bhe personnel exposed the 2' coated steel main at each end of the alley and capped it off. A pressure test was then conducted on the main at utilization pressure (9 psi) and the line would not pressure up. Excavations began in the alley near the service line and tap to the incident site and then continued east along the main. The 2' main was uncovered and damage was found on the line approximately 15' from the aforementioned tap. It appears that the line had been previously damaged by a backhoe bucket. Damage to the steel line was seen under and along the sides of the steel pipe and what appeared to be a stress crack was noted across the entire bottom circumference of the pipe. Upon further excavation we discovered a sanitary sewer lateral crossing our line directly under the damaged area. The damaged section of pipe was secured and then removed from the site. There were no signs of recent excavation in the area.
Occurred At 2012-01-08 09:03:00
Year 2012
Report Received Date 2012-02-06 00:00:00
Iyear 2012.0
Report Number 20120012.0
Supplemental Number 15511.0
Report Type Supplemental Final
Operator Id 15359 PHMSA Enforcement
Name Black Hills Energy
Operator Street Address 1102 E 1st Street
Operator City Name Papillion
Operator State Abbreviation NE
Operator Postal Code 68046-7641
Local Datetime 2012-01-08 09:03:00
Location Street Address 104 Wooten
Location City Name Sublette
Location County Name Haskell
Location State Abbreviation KS
Location Postal Code 67877
Location Latitude 37.481657 Google Maps OpenStreetMap
Location Longitude -100.842365 Google Maps OpenStreetMap
Nrc Rpt Datetime 2012-01-08 10:35:00
Nrc Rpt Num 999858 NRC Report How to search
Commodity Released Type Natural Gas
Fatality Ind No
Fatal 0
Injury Ind Yes
Num Emp Injuries 0
Num Contr Injuries 0
Num Er Injuries 0
Num Worker Injuries 0
Num Gp Injuries 4
Injure 4
Ignite Ind Yes
Explode Ind Yes
Num Pub Evacuated 15.0
Incident Identified Datetime 2012-01-08 09:03:00
On Site Datetime 2012-01-08 09:11:00
Federal No
Location Type Public Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 28.0
Crossing No
Pipe Facility Type Privately Owned
System Part Involved Main
Installation Year 1964.0
Pipe Diameter 2.0
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Steel
Steel Seam Type Other
Steel Seam Type Details Unknown
Wt Steel 0.154
Release Type Mechanical Puncture
Puncture Axial 1.0
Puncture Circum 3.0
Class Location Type Class 3 Location
Est Cost Oper Paid 125000.0
Est Cost Prop Damage 10000.0
Est Cost Emergency 20000.0
Est Cost Other 25000.0
Est Cost Other Details Replaced Line In Alley
Est Cost Unintentional Release 2500.0
Prpty 182500.0
Commercial Affected 30.0
Industrial Affected 0.0
Residences Affected 220.0
Accident Psig 9.0
Normal Psig 9.0
Mop Psig 9.5
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Previous Damage Due To Excavation Activity
Ex Party Type Previous Damage Due To Excavation Activity
Ex Hydrotest Leak Survey Date 2011-11-11 00:00:00
Ex Hydrotest Conducted Ind No
Notify Cga Dirt No
Public Row Ind Yes
Public Subtype Other
Excavator Type Unknown/other
Excavator Equipment Backhoe/trackhoe
Work Performed Sewer (Sanitary/storm)
One Call Notified Ind No
Locator Type Unknown/other
Visible Marks Unknown/other
Service Interruption No
Root Cause Category Miscellaneous Root Causes
Root Cause Type Previous Damage
Preparer Name J**** W******
Preparer Title Senior Manager Of Technical Services
Preparer Email J************@b*************.com
Preparer Telephone 316-941-1642
Preparer Fax 402-829-2790
Authorizer Name V**** C******
Authorizer Title General Manager Kansas Gas
Authorizer Telephone 785-832-3950
Authorizer Email V************@b*************.com
Narrative On sunday, january 8, 2012, at approximately 9:00 am there was a house explosion and subsequent fire located at 104 wooten street in sublette, ks. Two local company employees heard the explosion from their homes and reported to the site immediately. Upon arrival, bhe employees requested the assistance from local emergency management personnel to treat injuries and assist with evacuating the surrounding area. Seven people were home at the time of the explosion and four were taken to the hospital. Bar-hole testing was completed in the alley adjacent to the incident site and natural gas was detected. Bhe personnel took precautionary measures and shut off the east side of town in order to isolate the section of line. Service was shut off to approximately 250 customers. Bhe personnel continued to test for gas readings in the alley while other work was being performed. Bhe personnel restored gas to the eastern part of the system and began the re-lighting process that evening. Bhe personnel exposed the 2' coated steel main at each end of the alley and capped it off. A pressure test was then conducted on the main at utilization pressure (9 psi) and the line would not pressure up. Excavations began in the alley near the service line and tap to the incident site and then continued east along the main. The 2' main was uncovered and damage was found on the line approximately 15' from the aforementioned tap. It appears that the line had been previously damaged by a backhoe bucket. Damage to the steel line was seen under and along the sides of the steel pipe and what appeared to be a stress crack was noted across the entire bottom circumference of the pipe. Upon further excavation we discovered a sanitary sewer lateral crossing our line directly under the damaged area. The damaged section of pipe was secured and then removed from the site. There were no signs of recent excavation in the area.

All rights reserved. Copyright © by ClearPHMSA