HL incident on 2011-11-22 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2011-11-22 03:37
Report number
Location
TX
Narrative
Enterprise sulphur facility was shut down due to a leak on pig trap. The safety bleed on the pig barrel became loose and started leaking around threads of safety device. Installed new safety plug and chain to pig trap door. Returned to service.
Detailed record list
Report Received Date
2011-12-22 00:00:00
Iyear
2011
Report Number
20110454
Supplemental Number
16283
Report Type
Original Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2011-11-22 03:37:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Ethane
Unintentional Release Bbls
85
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Emergency Responder
Incident Identified Datetime
2011-11-22 03:37:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2011-11-22 04:42:00
Restart Datetime
2011-11-22 13:53:00
On Site Datetime
2011-11-22 04:42:00
Nrc Rpt Datetime
2011-11-22 05:39:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Automatic
Downstream Valve Type Ind
Automatic
Num Pub Evacuated
0
Pipe Fac Name
Sulphur Station
Segment Name
Lou-Tex Ngl 24740
Onshore State Abbreviation
La
Onshore Postal Code
70665
Onshore City Name
Sulphur
Onshore County Name
Calcasieu
Designated Location
Milepost/valve Station
Designated Name
103
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Scraper/pig Trap
Installation Year
2000
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Bleed Port Connection
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
2785
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
2785
Accident Psig
890
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
60
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Failure Details
Bleed Valve On Pig Trap Barrel Became Loose And Started Leaking Aroung Threads.
Additional Installation Ind
Yes
Preparer Name
N***** L* G*** J**
Preparer Title
Pipeline Compliance Specialist
Preparer Email
N****@e****.com
Preparer Telephone
9858041376
Prepared Date
2011-12-22 00:00:00
Authorizer Name
N***** L* G*** J**
Authorizer Telephone
9858041376
Authorizer Title
Pipeline Compliance Specialist
Authorizer Email
N****@e****.com
Narrative
Enterprise sulphur facility was shut down due to a leak on pig trap. The safety bleed on the pig barrel became loose and started leaking around threads of safety device. Installed new safety plug and chain to pig trap door. Returned to service.
Report Received Date 2011-12-22 00:00:00
Iyear 2011
Report Number 20110454
Supplemental Number 16283
Report Type Original Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2011-11-22 03:37:00
Location Latitude 30.16485 Google Maps OpenStreetMap
Location Longitude -93.35127 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Ethane
Unintentional Release Bbls 85
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Emergency Responder
Incident Identified Datetime 2011-11-22 03:37:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2011-11-22 04:42:00
Restart Datetime 2011-11-22 13:53:00
On Site Datetime 2011-11-22 04:42:00
Nrc Rpt Datetime 2011-11-22 05:39:00
Nrc Rpt Num 996202 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Automatic
Downstream Valve Type Ind Automatic
Num Pub Evacuated 0
Pipe Fac Name Sulphur Station
Segment Name Lou-Tex Ngl 24740
Onshore State Abbreviation La
Onshore Postal Code 70665
Onshore City Name Sulphur
Onshore County Name Calcasieu
Designated Location Milepost/valve Station
Designated Name 103
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Scraper/pig Trap
Installation Year 2000
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Bleed Port Connection
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 2785
Est Cost Prop Damage 0
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 2785
Accident Psig 890
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 60
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Failure Details Bleed Valve On Pig Trap Barrel Became Loose And Started Leaking Aroung Threads.
Additional Installation Ind Yes
Preparer Name N***** L* G*** J**
Preparer Title Pipeline Compliance Specialist
Preparer Email N****@e****.com
Preparer Telephone 9858041376
Prepared Date 2011-12-22 00:00:00
Authorizer Name N***** L* G*** J**
Authorizer Telephone 9858041376
Authorizer Title Pipeline Compliance Specialist
Authorizer Email N****@e****.com
Narrative Enterprise sulphur facility was shut down due to a leak on pig trap. The safety bleed on the pig barrel became loose and started leaking around threads of safety device. Installed new safety plug and chain to pig trap door. Returned to service.

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