Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2011-12-01 — TX
Operator
Sunoco Pipeline L.p.
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$1,650
Incident datetime
2011-12-01 10:30
Report number
Location
TX
Narrative
Failure of pump unit #2 outboard seal. Station was by-passed and a new seal was installed. Re-submitted on 3/26/2013 to include part e5f per PHMSA request.
Detailed record list
Report Received Date
2011-12-14 00:00:00
Iyear
2011
Report Number
20110450
Supplemental Number
17684
Report Type
Supplemental Final
Operator Id
18718
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2011-12-01 10:30:00
Location Latitude
33.22053
Location Longitude
-99.87124
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.36
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2011-12-01 10:30:00
Restart Datetime
2011-12-01 21:30:00
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
Rule Station
Segment Name
Hawley To Dixon 8" & 10"
Onshore State Abbreviation
Tx
Onshore Postal Code
79548
Onshore City Name
Rule
Onshore County Name
Haskell
Designated Location
Milepost/valve Station
Designated Name
Rule Station
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Intrastate
Item Involved
Pump
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
35
Est Cost Prop Damage
1650
Est Cost Emergency
2000
Est Cost Environmental
500
Est Cost Other
0
Prpty
4185
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Preparer Name
K****** D**** B***
Preparer Title
Area Dot Compliance Supervisor
Preparer Email
K*****@s**************.com
Preparer Telephone
281-637-6497
Preparer Fax
281-637-6425
Prepared Date
2013-03-26 00:00:00
Authorizer Name
K****** D**** B***
Authorizer Telephone
281-637-6497
Authorizer Title
Area Dot Compliance Supervisor
Authorizer Email
K*****@s**************.com
Narrative
Failure of pump unit #2 outboard seal. Station was by-passed and a new seal was installed. Re-submitted on 3/26/2013 to include part e5f per PHMSA request.
| Report Received Date | 2011-12-14 00:00:00 |
|---|---|
| Iyear | 2011 |
| Report Number | 20110450 |
| Supplemental Number | 17684 |
| Report Type | Supplemental Final |
| Operator Id | 18718 PHMSA Enforcement |
| Name | Sunoco Pipeline L.p. |
| Operator Street Address | 1300 Main Street |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2011-12-01 10:30:00 |
| Location Latitude | 33.22053 Google Maps OpenStreetMap |
| Location Longitude | -99.87124 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 0.36 |
| Intentional Release Bbls | 0 |
| Recovered Bbls | 0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2011-12-01 10:30:00 |
| Restart Datetime | 2011-12-01 21:30:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Pipe Fac Name | Rule Station |
| Segment Name | Hawley To Dixon 8" & 10" |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 79548 |
| Onshore City Name | Rule |
| Onshore County Name | Haskell |
| Designated Location | Milepost/valve Station |
| Designated Name | Rule Station |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Intrastate |
| Item Involved | Pump |
| Release Type | Leak |
| Leak Type | Seal Or Packing |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 35 |
| Est Cost Prop Damage | 1650 |
| Est Cost Emergency | 2000 |
| Est Cost Environmental | 500 |
| Est Cost Other | 0 |
| Prpty | 4185 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Pump Or Pump-Related Equipment |
| Eq Failure Type | Pump Or Pump-Related Equipment |
| Preparer Name | K****** D**** B*** |
| Preparer Title | Area Dot Compliance Supervisor |
| Preparer Email | K*****@s**************.com |
| Preparer Telephone | 281-637-6497 |
| Preparer Fax | 281-637-6425 |
| Prepared Date | 2013-03-26 00:00:00 |
| Authorizer Name | K****** D**** B*** |
| Authorizer Telephone | 281-637-6497 |
| Authorizer Title | Area Dot Compliance Supervisor |
| Authorizer Email | K*****@s**************.com |
| Narrative | Failure of pump unit #2 outboard seal. Station was by-passed and a new seal was installed. Re-submitted on 3/26/2013 to include part e5f per PHMSA request. |
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