HL incident on 2011-11-13 — WY

Operator
Belle Fourche Pipeline Co
Cause
Excavation Issue
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$29,525
Incident datetime
2011-11-13 08:45
Report number
Location
WY
Narrative
Contractor installing water and sewer lines to kld trucking facility struck marked gathering line compromising it and spilling crude into the bell hole/ditch in which the contractor was working. Contractor originally called one-call on 10/14 and belle fourche pipeline located with pin flags the location of the facility. Belle fourche asked to be on site during excavation and asked on multiple occasions for a meet time. Contractor did not respond and did not begin digging until after the initial locate request had expired. On sunday november 13th, while digging to install sewer lines, contractor compromised the belle fourche oil gathering pipeline spilling about 200 barrels of crude into ditch and contaminating surrounding soils. An update excavation notice was not executed until november 16th (ticket #11155260). Strike occured at approximately 8:00 a.M. On november 13th and belle fourche had employees on the scene around 8:45. Line was shut down and repaired by cutting out a segment and welding in new pipe. On november 14th at approximately 4:00 p.M. Belle fourche restarted the pipeline.
Detailed record list
Report Received Date
2011-12-13 00:00:00
Iyear
2011
Report Number
20110448
Supplemental Number
16553
Report Type
Supplemental Final
Operator Id
Name
Belle Fourche Pipeline Co
Operator Street Address
455 N Poplar St.
Operator City Name
Casper
Operator State Abbreviation
WY
Operator Postal Code
82602
Local Datetime
2011-11-13 08:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
200
Recovered Bbls
120
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Third Party That Caused The Accident
Incident Identified Datetime
2011-11-13 08:45:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2011-11-13 09:00:00
Restart Datetime
2011-11-14 16:00:00
On Site Datetime
2011-11-13 08:45:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Dickinson Gathering
Segment Name
Dickinson Gathering
Onshore State Abbreviation
Nd
Onshore Postal Code
58601
Onshore City Name
Dickinson
Onshore County Name
Stark
Designated Location
Milepost/valve Station
Designated Name
1
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
6
Pipe Wall Thickness
0.156
Pipe Smys
42000
Pipe Specification
Api 5l
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Unkown
Pipe Coating Type
Coal Tar
Installation Year
1995
Manufactured Year
1995
Material Involved
Carbon Steel
Release Type
Mechanical Puncture
Puncture Axial
4
Puncture Circum
1.7
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Vegetation Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
3630
Est Cost Prop Damage
29525
Est Cost Emergency
2835
Est Cost Environmental
4353
Est Cost Other
0
Est Cost Other Details
Operators Exposure To 8a And 8e Limited As Third Party Was Responsible
Prpty
40343
Accident Psig
100
Mop Psig
1428
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Gathering
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
Notify Cga Dirt
Yes
Pipeline Easement Row Ind
Yes
Excavator Type
Contractor
Excavator Equipment
Backhoe/trackhoe
Work Performed
Sewer (Sanitary/storm)
One Call Notified Ind
Yes
One Call Ticket Num
11133777
One Call Center Name
Only One Call Center In N. Dakota Called North Dakota One Call
Locator Type
Utility Owner
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
32
Root Cause Category
Excavation Issue
Root Cause Type
Improper Backfilling Practices
Preparer Name
K****** D* D*********
Preparer Title
Dot Compliance Coordinator
Preparer Email
K*************@t******.com
Preparer Telephone
307-266-0275
Prepared Date
2012-04-16 00:00:00
Authorizer Name
K****** D* D*********
Authorizer Telephone
307-266-0275
Authorizer Title
Dot Compliance Coordinator
Authorizer Email
K*************@t******.com
Narrative
Contractor installing water and sewer lines to kld trucking facility struck marked gathering line compromising it and spilling crude into the bell hole/ditch in which the contractor was working. Contractor originally called one-call on 10/14 and belle fourche pipeline located with pin flags the location of the facility. Belle fourche asked to be on site during excavation and asked on multiple occasions for a meet time. Contractor did not respond and did not begin digging until after the initial locate request had expired. On sunday november 13th, while digging to install sewer lines, contractor compromised the belle fourche oil gathering pipeline spilling about 200 barrels of crude into ditch and contaminating surrounding soils. An update excavation notice was not executed until november 16th (ticket #11155260). Strike occured at approximately 8:00 a.M. On november 13th and belle fourche had employees on the scene around 8:45. Line was shut down and repaired by cutting out a segment and welding in new pipe. On november 14th at approximately 4:00 p.M. Belle fourche restarted the pipeline.
Report Received Date 2011-12-13 00:00:00
Iyear 2011
Report Number 20110448
Supplemental Number 16553
Report Type Supplemental Final
Operator Id 1248 PHMSA Enforcement
Name Belle Fourche Pipeline Co
Operator Street Address 455 N Poplar St.
Operator City Name Casper
Operator State Abbreviation WY
Operator Postal Code 82602
Local Datetime 2011-11-13 08:00:00
Location Latitude 46.861678 Google Maps OpenStreetMap
Location Longitude -102.777616 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 200
Recovered Bbls 120
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Third Party That Caused The Accident
Incident Identified Datetime 2011-11-13 08:45:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2011-11-13 09:00:00
Restart Datetime 2011-11-14 16:00:00
On Site Datetime 2011-11-13 08:45:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Dickinson Gathering
Segment Name Dickinson Gathering
Onshore State Abbreviation Nd
Onshore Postal Code 58601
Onshore City Name Dickinson
Onshore County Name Stark
Designated Location Milepost/valve Station
Designated Name 1
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 48
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 6
Pipe Wall Thickness 0.156
Pipe Smys 42000
Pipe Specification Api 5l
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Unkown
Pipe Coating Type Coal Tar
Installation Year 1995
Manufactured Year 1995
Material Involved Carbon Steel
Release Type Mechanical Puncture
Puncture Axial 4
Puncture Circum 1.7
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Vegetation Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 3630
Est Cost Prop Damage 29525
Est Cost Emergency 2835
Est Cost Environmental 4353
Est Cost Other 0
Est Cost Other Details Operators Exposure To 8a And 8e Limited As Third Party Was Responsible
Prpty 40343
Accident Psig 100
Mop Psig 1428
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Gathering
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
Notify Cga Dirt Yes
Pipeline Easement Row Ind Yes
Excavator Type Contractor
Excavator Equipment Backhoe/trackhoe
Work Performed Sewer (Sanitary/storm)
One Call Notified Ind Yes
One Call Ticket Num 11133777
One Call Center Name Only One Call Center In N. Dakota Called North Dakota One Call
Locator Type Utility Owner
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 32
Root Cause Category Excavation Issue
Root Cause Type Improper Backfilling Practices
Preparer Name K****** D* D*********
Preparer Title Dot Compliance Coordinator
Preparer Email K*************@t******.com
Preparer Telephone 307-266-0275
Prepared Date 2012-04-16 00:00:00
Authorizer Name K****** D* D*********
Authorizer Telephone 307-266-0275
Authorizer Title Dot Compliance Coordinator
Authorizer Email K*************@t******.com
Narrative Contractor installing water and sewer lines to kld trucking facility struck marked gathering line compromising it and spilling crude into the bell hole/ditch in which the contractor was working. Contractor originally called one-call on 10/14 and belle fourche pipeline located with pin flags the location of the facility. Belle fourche asked to be on site during excavation and asked on multiple occasions for a meet time. Contractor did not respond and did not begin digging until after the initial locate request had expired. On sunday november 13th, while digging to install sewer lines, contractor compromised the belle fourche oil gathering pipeline spilling about 200 barrels of crude into ditch and contaminating surrounding soils. An update excavation notice was not executed until november 16th (ticket #11155260). Strike occured at approximately 8:00 a.M. On november 13th and belle fourche had employees on the scene around 8:45. Line was shut down and repaired by cutting out a segment and welding in new pipe. On november 14th at approximately 4:00 p.M. Belle fourche restarted the pipeline.

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