Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2011-12-07 — TX
Operator
Enterprise Crude Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$10
Incident datetime
2011-12-07 13:00
Report number
Location
TX
Narrative
Enterprise driver was unloading at callisburg station and noticed oil spraying from the mainline unit, he notified the area tech who called the control center to shut down the unit. When area tech arrived he discovered oil had sprayed from the seal flush line and misted everything within a 50' radius around the pump, no oil was standing and we estimated 1 bbl of oil had been released. Rock and piping has been cleaned up. Tubing replaced with stainless steel tubing.
Detailed record list
Report Received Date
2011-12-12 00:00:00
Iyear
2011
Report Number
20110446
Supplemental Number
17517
Report Type
Supplemental Final
Operator Id
30829
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2011-12-07 13:00:00
Location Latitude
33.68092
Location Longitude
-97.075241
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Ignite Ind
No
Explode Ind
No
Onshore State Abbreviation
Tx
Onshore Postal Code
76240
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Intrastate
Item Involved
Tubing
Release Type
Leak
Leak Type
Crack
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
95
Est Cost Prop Damage
10
Est Cost Emergency
0
Est Cost Environmental
4500
Est Cost Other
0
Prpty
4605
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Defective Or Loose Tubing Or Fitting
Eq Failure Type
Defective Or Loose Tubing Or Fitting
Preparer Name
N*** B******
Preparer Title
Sr Pipeline Compliance Specialist
Preparer Email
W********@e****.com
Preparer Telephone
713-381-3536
Preparer Fax
281-887-7704
Prepared Date
2013-03-14 00:00:00
Authorizer Name
N*** B******
Authorizer Telephone
713-381-3536
Authorizer Title
Sr Pipeline Compliance Specialist
Authorizer Email
W********@e****.com
Narrative
Enterprise driver was unloading at callisburg station and noticed oil spraying from the mainline unit, he notified the area tech who called the control center to shut down the unit. When area tech arrived he discovered oil had sprayed from the seal flush line and misted everything within a 50' radius around the pump, no oil was standing and we estimated 1 bbl of oil had been released. Rock and piping has been cleaned up. Tubing replaced with stainless steel tubing.
| Report Received Date | 2011-12-12 00:00:00 |
|---|---|
| Iyear | 2011 |
| Report Number | 20110446 |
| Supplemental Number | 17517 |
| Report Type | Supplemental Final |
| Operator Id | 30829 PHMSA Enforcement |
| Name | Enterprise Crude Pipeline Llc |
| Operator Street Address | 1100 Louisiana Street |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2011-12-07 13:00:00 |
| Location Latitude | 33.68092 Google Maps OpenStreetMap |
| Location Longitude | -97.075241 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 1 |
| Intentional Release Bbls | 0 |
| Recovered Bbls | 0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Ignite Ind | No |
| Explode Ind | No |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 76240 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Intrastate |
| Item Involved | Tubing |
| Release Type | Leak |
| Leak Type | Crack |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 95 |
| Est Cost Prop Damage | 10 |
| Est Cost Emergency | 0 |
| Est Cost Environmental | 4500 |
| Est Cost Other | 0 |
| Prpty | 4605 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Defective Or Loose Tubing Or Fitting |
| Eq Failure Type | Defective Or Loose Tubing Or Fitting |
| Preparer Name | N*** B****** |
| Preparer Title | Sr Pipeline Compliance Specialist |
| Preparer Email | W********@e****.com |
| Preparer Telephone | 713-381-3536 |
| Preparer Fax | 281-887-7704 |
| Prepared Date | 2013-03-14 00:00:00 |
| Authorizer Name | N*** B****** |
| Authorizer Telephone | 713-381-3536 |
| Authorizer Title | Sr Pipeline Compliance Specialist |
| Authorizer Email | W********@e****.com |
| Narrative | Enterprise driver was unloading at callisburg station and noticed oil spraying from the mainline unit, he notified the area tech who called the control center to shut down the unit. When area tech arrived he discovered oil had sprayed from the seal flush line and misted everything within a 50' radius around the pump, no oil was standing and we estimated 1 bbl of oil had been released. Rock and piping has been cleaned up. Tubing replaced with stainless steel tubing. |
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