HL incident on 2011-12-08 — OK

Operator
Oneok Ngl Pipeline Lp
Cause
Excavation Issue
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$15,085
Incident datetime
2011-12-08 16:10
Report number
Location
OK
Narrative
Oneok product movement center received call from woodward fire department that a backhoe had hit and ruptured oneok's pipeline 1 mile east and 1.5 mile south of mooreland,ok. Dcp mooreland injection plant was shutdown oneok field personnel were dispatched to location and closed valves to isolate the release. Product vapored off to atmosphere. Damaged pipe was removed from pipeline and pretested pipe was installed in pipeline. Pipeline was purged with product and restarted. Pipeline personnel had previously met excavator onsite and marked pipeline location. Operator and excavator scheduled a time for operator personnel to be on site during excavation, (12/09/2011). A "no dig" area was defined on either side of operators pipeline. Third party contractor employee began excavation prior to scheduled meeting time and did not respect pipeline markings.
Detailed record list
Report Received Date
2011-12-09 00:00:00
Iyear
2011
Report Number
20110442
Supplemental Number
16329
Report Type
Supplemental Final
Operator Id
Name
Oneok Ngl Pipeline Lp
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2011-12-08 16:10:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
360
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Emergency Responder
Incident Identified Datetime
2011-12-08 16:10:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2011-12-08 16:35:00
Restart Datetime
2011-12-09 20:48:00
On Site Datetime
2011-12-08 17:30:00
Nrc Rpt Datetime
2011-12-08 17:40:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Mooreland Plant To Mooreland Booster 4"
Onshore State Abbreviation
Ok
Onshore Postal Code
73582
Onshore City Name
Mooreland
Onshore County Name
Woodward
Designated Location
Survey Station No.
Designated Name
143+00
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
80
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
4.5
Pipe Wall Thickness
0.156
Pipe Smys
42000
Pipe Specification
5l
Pipe Seam Type
Erw � Unknown Frequency
Pipe Coating Type
Cold Applied Tape
Installation Year
1975
Material Involved
Carbon Steel
Release Type
Rupture
Rupture Orient
Circumferential
Rupture Width
4.5
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
1000
Est Cost Gas Released
14886
Est Cost Prop Damage
15085
Est Cost Emergency
1500
Est Cost Environmental
0
Est Cost Other
0
Prpty
32471
Accident Psig
1325
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
27532
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Operator received call from mooreland fire department stating a backhoe had hit and ruptured oneok's piipeline
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
Notify Cga Dirt
No
Private Row Ind
Yes
Private Subtype
Private Landowner
Pipeline Easement Row Ind
Yes
Excavator Type
Contractor
Excavator Equipment
Backhoe/trackhoe
Work Performed
Electric
One Call Notified Ind
Yes
One Call Ticket Num
1.11206e+13
One Call Center Name
Oklahoma One-Call
Locator Type
Utility Owner
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
28
Root Cause Category
Excavation Issue
Root Cause Type
Improper Backfilling Practices
Preparer Name
N*** J****
Preparer Title
Dot Compliance Coordinator
Preparer Email
N*********@o****.com
Preparer Telephone
580-395-6304
Preparer Fax
580-395-2377
Prepared Date
2012-01-12 00:00:00
Authorizer Name
N*** J****
Authorizer Telephone
580-395-6304
Authorizer Title
Dot Compliance Coordinator
Authorizer Email
N*********@o****.com
Narrative
Oneok product movement center received call from woodward fire department that a backhoe had hit and ruptured oneok's pipeline 1 mile east and 1.5 mile south of mooreland,ok. Dcp mooreland injection plant was shutdown oneok field personnel were dispatched to location and closed valves to isolate the release. Product vapored off to atmosphere. Damaged pipe was removed from pipeline and pretested pipe was installed in pipeline. Pipeline was purged with product and restarted. Pipeline personnel had previously met excavator onsite and marked pipeline location. Operator and excavator scheduled a time for operator personnel to be on site during excavation, (12/09/2011). A "no dig" area was defined on either side of operators pipeline. Third party contractor employee began excavation prior to scheduled meeting time and did not respect pipeline markings.
Report Received Date 2011-12-09 00:00:00
Iyear 2011
Report Number 20110442
Supplemental Number 16329
Report Type Supplemental Final
Operator Id 32109 PHMSA Enforcement
Name Oneok Ngl Pipeline Lp
Operator Street Address 100 West Fifth Street
Operator City Name Tulsa
Operator State Abbreviation OK
Operator Postal Code 74103
Local Datetime 2011-12-08 16:10:00
Location Latitude 36.413056 Google Maps OpenStreetMap
Location Longitude -99.193611 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 360
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Emergency Responder
Incident Identified Datetime 2011-12-08 16:10:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2011-12-08 16:35:00
Restart Datetime 2011-12-09 20:48:00
On Site Datetime 2011-12-08 17:30:00
Nrc Rpt Datetime 2011-12-08 17:40:00
Nrc Rpt Num 997605 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Mooreland Plant To Mooreland Booster 4"
Onshore State Abbreviation Ok
Onshore Postal Code 73582
Onshore City Name Mooreland
Onshore County Name Woodward
Designated Location Survey Station No.
Designated Name 143+00
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 80
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 4.5
Pipe Wall Thickness 0.156
Pipe Smys 42000
Pipe Specification 5l
Pipe Seam Type Erw � Unknown Frequency
Pipe Coating Type Cold Applied Tape
Installation Year 1975
Material Involved Carbon Steel
Release Type Rupture
Rupture Orient Circumferential
Rupture Width 4.5
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 1000
Est Cost Gas Released 14886
Est Cost Prop Damage 15085
Est Cost Emergency 1500
Est Cost Environmental 0
Est Cost Other 0
Prpty 32471
Accident Psig 1325
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 27532
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Operator received call from mooreland fire department stating a backhoe had hit and ruptured oneok's piipeline
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
Notify Cga Dirt No
Private Row Ind Yes
Private Subtype Private Landowner
Pipeline Easement Row Ind Yes
Excavator Type Contractor
Excavator Equipment Backhoe/trackhoe
Work Performed Electric
One Call Notified Ind Yes
One Call Ticket Num 1.11206e+13
One Call Center Name Oklahoma One-Call
Locator Type Utility Owner
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 28
Root Cause Category Excavation Issue
Root Cause Type Improper Backfilling Practices
Preparer Name N*** J****
Preparer Title Dot Compliance Coordinator
Preparer Email N*********@o****.com
Preparer Telephone 580-395-6304
Preparer Fax 580-395-2377
Prepared Date 2012-01-12 00:00:00
Authorizer Name N*** J****
Authorizer Telephone 580-395-6304
Authorizer Title Dot Compliance Coordinator
Authorizer Email N*********@o****.com
Narrative Oneok product movement center received call from woodward fire department that a backhoe had hit and ruptured oneok's pipeline 1 mile east and 1.5 mile south of mooreland,ok. Dcp mooreland injection plant was shutdown oneok field personnel were dispatched to location and closed valves to isolate the release. Product vapored off to atmosphere. Damaged pipe was removed from pipeline and pretested pipe was installed in pipeline. Pipeline was purged with product and restarted. Pipeline personnel had previously met excavator onsite and marked pipeline location. Operator and excavator scheduled a time for operator personnel to be on site during excavation, (12/09/2011). A "no dig" area was defined on either side of operators pipeline. Third party contractor employee began excavation prior to scheduled meeting time and did not respect pipeline markings.

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