HL incident on 2011-11-08 — TX

Operator
Chevron Petrochemical Pipeline Llc
Cause
Material Failure Of Pipe Or Weld
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$517,016
Incident datetime
2011-11-08 10:00
Report number
Location
TX
Narrative
Local land owner called in to the company control center and reported dead vegetation approximately 4-feet in diameter on company right-of-way. Operation personnel was immediatly dispatched to reported site and the pipeline was immediatly shut down. The leak was so small that an instrumented combustiblbe gas indicator ad to be used to confirm leak. Root cause: material failure of original manufacturing-related (erw longitudinal seam "cold weld" lack of fusion), not a girth weld or other welds formed in the field. A "cold weld" was found in longitudinal erw-lf pipe seam, that could have been caused by dirt, grease, scale or other oxide films, or loss of electrical current, resulting in isolated non-bonding of the pipe weld seam. Metallurgical analysis concluded that the cold weld, where the pinhole leak was found, to be an original manufacturing defect. Solution: cut out the joint of pipe containting the leak and replaced with new pipe.
Detailed record list
Report Received Date
2011-12-08 00:00:00
Iyear
2011
Report Number
20110441
Supplemental Number
16715
Report Type
Supplemental Final
Operator Id
Name
Chevron Petrochemical Pipeline Llc
Operator Street Address
9 Greenway Plaza
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77046
Local Datetime
2011-11-08 10:00:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Ethylene
Unintentional Release Bbls
0.23
Intentional Release Bbls
500
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2011-11-08 10:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2011-11-08 10:30:00
Restart Datetime
2011-11-18 18:30:00
On Site Datetime
2011-11-08 10:00:00
Nrc Rpt Datetime
2011-11-08 10:50:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Evangeline Ethylene Pipeline System
Segment Name
Mile Post 81
Onshore State Abbreviation
La
Onshore Postal Code
70546
Onshore City Name
Jennings
Onshore County Name
Jefferson Davis
Designated Location
Milepost/valve Station
Designated Name
Mp 81
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
39
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Seam
Pipe Diameter
16
Pipe Wall Thickness
0.312
Pipe Smys
52000
Pipe Specification
Api 5 Lx
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Youngstown Sheet And Tube Company. Ny
Pipe Coating Type
Coal Tar
Installation Year
1954
Manufactured Year
1953
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
35296
Est Cost Prop Damage
517016
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Est Cost Other Details
Pinhole Leak In Line Pipe
Prpty
552312
Accident Psig
1100
Mop Psig
1336
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
103784
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The leak was so small that it was not detedctable via scada
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Material Failure Of Pipe Or Weld
Cause Details
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Metallurgical Ind
Yes
Failure Type
Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor
Yes
Other Factor Details
Defective Longitudinal Weld
Additional Lack Fusion Ind
Yes
Collected Data Ind
Yes
Axial Magnetic Flx Lkg Ind
Yes
Geometry Deformation Ind
Yes
Axial Recent Year
2007
Geometry Recent Year
2007
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2001
Hydrtst Most Rcnt Pressure
1670
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
H**** L* L****
Preparer Title
Dot Pipeline Safety Specialist
Preparer Email
H*********@c******.com
Preparer Telephone
(337) 654-8915
Preparer Fax
(337) 572-3720
Prepared Date
2012-06-20 00:00:00
Authorizer Name
H**** L* L****
Authorizer Telephone
(337) 654-8915
Authorizer Title
Dot Pipeline Safety Specialist
Authorizer Email
H*********@c******.com
Narrative
Local land owner called in to the company control center and reported dead vegetation approximately 4-feet in diameter on company right-of-way. Operation personnel was immediatly dispatched to reported site and the pipeline was immediatly shut down. The leak was so small that an instrumented combustiblbe gas indicator ad to be used to confirm leak. Root cause: material failure of original manufacturing-related (erw longitudinal seam "cold weld" lack of fusion), not a girth weld or other welds formed in the field. A "cold weld" was found in longitudinal erw-lf pipe seam, that could have been caused by dirt, grease, scale or other oxide films, or loss of electrical current, resulting in isolated non-bonding of the pipe weld seam. Metallurgical analysis concluded that the cold weld, where the pinhole leak was found, to be an original manufacturing defect. Solution: cut out the joint of pipe containting the leak and replaced with new pipe.
Report Received Date 2011-12-08 00:00:00
Iyear 2011
Report Number 20110441
Supplemental Number 16715
Report Type Supplemental Final
Operator Id 31554 PHMSA Enforcement
Name Chevron Petrochemical Pipeline Llc
Operator Street Address 9 Greenway Plaza
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77046
Local Datetime 2011-11-08 10:00:00
Location Latitude 30.355333 Google Maps OpenStreetMap
Location Longitude -92.708299 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Ethylene
Unintentional Release Bbls 0.23
Intentional Release Bbls 500
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2011-11-08 10:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2011-11-08 10:30:00
Restart Datetime 2011-11-18 18:30:00
On Site Datetime 2011-11-08 10:00:00
Nrc Rpt Datetime 2011-11-08 10:50:00
Nrc Rpt Num 994910 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Evangeline Ethylene Pipeline System
Segment Name Mile Post 81
Onshore State Abbreviation La
Onshore Postal Code 70546
Onshore City Name Jennings
Onshore County Name Jefferson Davis
Designated Location Milepost/valve Station
Designated Name Mp 81
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 39
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Seam
Pipe Diameter 16
Pipe Wall Thickness 0.312
Pipe Smys 52000
Pipe Specification Api 5 Lx
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Youngstown Sheet And Tube Company. Ny
Pipe Coating Type Coal Tar
Installation Year 1954
Manufactured Year 1953
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 35296
Est Cost Prop Damage 517016
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Est Cost Other Details Pinhole Leak In Line Pipe
Prpty 552312
Accident Psig 1100
Mop Psig 1336
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 103784
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The leak was so small that it was not detedctable via scada
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Material Failure Of Pipe Or Weld
Cause Details Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Metallurgical Ind Yes
Failure Type Original Manufacturing-Related (Not Girth Weld Or Other Welds Formed In The Field)
Other Factor Yes
Other Factor Details Defective Longitudinal Weld
Additional Lack Fusion Ind Yes
Collected Data Ind Yes
Axial Magnetic Flx Lkg Ind Yes
Geometry Deformation Ind Yes
Axial Recent Year 2007
Geometry Recent Year 2007
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2001
Hydrtst Most Rcnt Pressure 1670
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name H**** L* L****
Preparer Title Dot Pipeline Safety Specialist
Preparer Email H*********@c******.com
Preparer Telephone (337) 654-8915
Preparer Fax (337) 572-3720
Prepared Date 2012-06-20 00:00:00
Authorizer Name H**** L* L****
Authorizer Telephone (337) 654-8915
Authorizer Title Dot Pipeline Safety Specialist
Authorizer Email H*********@c******.com
Narrative Local land owner called in to the company control center and reported dead vegetation approximately 4-feet in diameter on company right-of-way. Operation personnel was immediatly dispatched to reported site and the pipeline was immediatly shut down. The leak was so small that an instrumented combustiblbe gas indicator ad to be used to confirm leak. Root cause: material failure of original manufacturing-related (erw longitudinal seam "cold weld" lack of fusion), not a girth weld or other welds formed in the field. A "cold weld" was found in longitudinal erw-lf pipe seam, that could have been caused by dirt, grease, scale or other oxide films, or loss of electrical current, resulting in isolated non-bonding of the pipe weld seam. Metallurgical analysis concluded that the cold weld, where the pinhole leak was found, to be an original manufacturing defect. Solution: cut out the joint of pipe containting the leak and replaced with new pipe.

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