HL incident on 2011-11-12 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$40
Incident datetime
2011-11-12 14:45
Report number
Location
TX
Narrative
Control center noticed the rates not being consistant from the ringgold delivery, control called area tech who was on call to go see what the problem was, when tech arrived he found oil spraying a mist of oil from the back pressure valve on the delivery skid. There was about 1.5 bbl's released all of which stayed on the property. Pump was shutdown and the diaphram was replaced and pump started back up.
Detailed record list
Report Received Date
2011-11-16 00:00:00
Iyear
2011
Report Number
20110427
Supplemental Number
17516
Report Type
Supplemental Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2011-11-12 14:45:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1.5
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Ignite Ind
No
Explode Ind
No
Onshore State Abbreviation
Tx
Onshore Postal Code
76261
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Release Type
Leak
Leak Type
Other
Leak Type Other
Diaphram On Back Pressure Valv
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
150
Est Cost Prop Damage
40
Est Cost Emergency
5000
Est Cost Environmental
0
Est Cost Other
0
Prpty
5190
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Other Equipment Failure
Eq Failure Type
Other Equipment Failure
Preparer Name
N*** B******
Preparer Title
Sr Pipeline Compliance Specialist
Preparer Email
W********@e****.com
Preparer Telephone
713-381-3536
Preparer Fax
281-887-7704
Prepared Date
2013-03-14 00:00:00
Authorizer Name
N*** B******
Authorizer Telephone
713-381-3536
Authorizer Title
Sr Pipeline Compliance Specialist
Authorizer Email
W********@e****.com
Narrative
Control center noticed the rates not being consistant from the ringgold delivery, control called area tech who was on call to go see what the problem was, when tech arrived he found oil spraying a mist of oil from the back pressure valve on the delivery skid. There was about 1.5 bbl's released all of which stayed on the property. Pump was shutdown and the diaphram was replaced and pump started back up.
Report Received Date 2011-11-16 00:00:00
Iyear 2011
Report Number 20110427
Supplemental Number 17516
Report Type Supplemental Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2011-11-12 14:45:00
Location Latitude 33.86345 Google Maps OpenStreetMap
Location Longitude -97.953363 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1.5
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Ignite Ind No
Explode Ind No
Onshore State Abbreviation Tx
Onshore Postal Code 76261
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Pipe Facility Type Interstate
Item Involved Valve
Valve Type Auxiliary Or Other Valve
Release Type Leak
Leak Type Other
Leak Type Other Diaphram On Back Pressure Valv
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 150
Est Cost Prop Damage 40
Est Cost Emergency 5000
Est Cost Environmental 0
Est Cost Other 0
Prpty 5190
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Other Equipment Failure
Eq Failure Type Other Equipment Failure
Preparer Name N*** B******
Preparer Title Sr Pipeline Compliance Specialist
Preparer Email W********@e****.com
Preparer Telephone 713-381-3536
Preparer Fax 281-887-7704
Prepared Date 2013-03-14 00:00:00
Authorizer Name N*** B******
Authorizer Telephone 713-381-3536
Authorizer Title Sr Pipeline Compliance Specialist
Authorizer Email W********@e****.com
Narrative Control center noticed the rates not being consistant from the ringgold delivery, control called area tech who was on call to go see what the problem was, when tech arrived he found oil spraying a mist of oil from the back pressure valve on the delivery skid. There was about 1.5 bbl's released all of which stayed on the property. Pump was shutdown and the diaphram was replaced and pump started back up.

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