Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2011-10-17 — OK
Operator
Magellan Pipeline Company, Lp
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$0
Incident datetime
2011-10-17 10:15
Report number
Location
OK
Narrative
While withdrawing a tor tool the plug came loose, resulting in the release. The nearest valve was shut when the tool was removed. Impacted soil was replaced with clean top soil. The impacted soil was collected for waste characterization and disposal in accordance with state and company guidelines.
Detailed record list
Report Received Date
2011-11-11 00:00:00
Iyear
2011
Report Number
20110420
Supplemental Number
16324
Report Type
Supplemental Final
Operator Id
22610
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2011-10-17 10:15:00
Location Latitude
41.93805
Location Longitude
-87.89138
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
0.48
Intentional Release Bbls
0
Recovered Bbls
0.48
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2011-10-17 10:15:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Was Down And Being Moved For A Highway Relocation Project
On Site Datetime
2011-10-17 10:15:00
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
Line Id 6167 & Line Id 6168
Segment Name
Chicago Terminal
Onshore State Abbreviation
Il
Onshore Postal Code
60131
Onshore City Name
Franklin Park
Onshore County Name
Cook
Designated Location
Milepost/valve Station
Designated Name
304+31
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Tor Fitting
Release Type
Leak
Leak Type
Other
Leak Type Other
Loose Tor Plug
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
60
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
500
Est Cost Other
0
Prpty
560
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Equipment Not Installed Properly
Operation Type
Equipment Not Installed Properly
Preparer Name
K****** L* L*******
Preparer Title
Sr. Compliance Coordinator
Preparer Email
K***********@m*********.com
Preparer Telephone
918-574-7315
Preparer Fax
918-574-7246
Prepared Date
2012-01-11 00:00:00
Authorizer Name
K****** L* L*******
Authorizer Telephone
918-574-7315
Authorizer Title
Sr. Compliance Coordinator
Authorizer Email
K***********@m*********.com
Narrative
While withdrawing a tor tool the plug came loose, resulting in the release. The nearest valve was shut when the tool was removed. Impacted soil was replaced with clean top soil. The impacted soil was collected for waste characterization and disposal in accordance with state and company guidelines.
| Report Received Date | 2011-11-11 00:00:00 |
|---|---|
| Iyear | 2011 |
| Report Number | 20110420 |
| Supplemental Number | 16324 |
| Report Type | Supplemental Final |
| Operator Id | 22610 PHMSA Enforcement |
| Name | Magellan Pipeline Company, Lp |
| Operator Street Address | 100 West 5th Street |
| Operator City Name | Tulsa |
| Operator State Abbreviation | OK |
| Operator Postal Code | 74103 |
| Local Datetime | 2011-10-17 10:15:00 |
| Location Latitude | 41.93805 Google Maps OpenStreetMap |
| Location Longitude | -87.89138 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Diesel, Fuel Oil, Kerosene, Jet Fuel |
| Unintentional Release Bbls | 0.48 |
| Intentional Release Bbls | 0 |
| Recovered Bbls | 0.48 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2011-10-17 10:15:00 |
| System Part Involved | Onshore Pipeline, Including Valve Sites |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Line Was Down And Being Moved For A Highway Relocation Project |
| On Site Datetime | 2011-10-17 10:15:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Pipe Fac Name | Line Id 6167 & Line Id 6168 |
| Segment Name | Chicago Terminal |
| Onshore State Abbreviation | Il |
| Onshore Postal Code | 60131 |
| Onshore City Name | Franklin Park |
| Onshore County Name | Cook |
| Designated Location | Milepost/valve Station |
| Designated Name | 304+31 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Interstate |
| Item Involved | Other |
| Item Involved Details | Tor Fitting |
| Release Type | Leak |
| Leak Type | Other |
| Leak Type Other | Loose Tor Plug |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| High Pop Ind | Yes |
| High Pop Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 60 |
| Est Cost Prop Damage | 0 |
| Est Cost Emergency | 0 |
| Est Cost Environmental | 500 |
| Est Cost Other | 0 |
| Prpty | 560 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Incorrect Operation |
| Cause Details | Equipment Not Installed Properly |
| Operation Type | Equipment Not Installed Properly |
| Preparer Name | K****** L* L******* |
| Preparer Title | Sr. Compliance Coordinator |
| Preparer Email | K***********@m*********.com |
| Preparer Telephone | 918-574-7315 |
| Preparer Fax | 918-574-7246 |
| Prepared Date | 2012-01-11 00:00:00 |
| Authorizer Name | K****** L* L******* |
| Authorizer Telephone | 918-574-7315 |
| Authorizer Title | Sr. Compliance Coordinator |
| Authorizer Email | K***********@m*********.com |
| Narrative | While withdrawing a tor tool the plug came loose, resulting in the release. The nearest valve was shut when the tool was removed. Impacted soil was replaced with clean top soil. The impacted soil was collected for waste characterization and disposal in accordance with state and company guidelines. |
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