HL incident on 2011-10-12 — TX

Operator
West Texas Gulf Pipeline Co
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$2,095
Incident datetime
2011-10-12 07:45
Report number
Location
TX
Narrative
Internal corrosion on 2" sump discharge line found by operator during routine station check. Line segment replaced. Re-submitted on 3/19/2013 to include part e5f per PHMSA request.
Detailed record list
Report Received Date
2011-11-11 00:00:00
Iyear
2011
Report Number
20110417
Supplemental Number
17586
Report Type
Supplemental Final
Operator Id
Name
West Texas Gulf Pipeline Co
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2011-10-12 07:45:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2011-10-12 07:45:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2011-10-12 07:45:00
Restart Datetime
2011-10-12 16:20:00
On Site Datetime
2011-10-12 07:45:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Wtg-Longview Station
Segment Name
Wtg-Sump Discharge Line
Onshore State Abbreviation
Tx
Onshore Postal Code
75604
Onshore City Name
Longview
Onshore County Name
Gregg
Designated Location
Milepost/valve Station
Designated Name
Longview Sta.
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Release Type
Leak
Leak Type
Pinhole
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
82
Est Cost Prop Damage
2095
Est Cost Emergency
1598
Est Cost Environmental
745
Est Cost Other
0
Prpty
4520
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Preparer Name
T*** G* N*******
Preparer Title
Dot Compliance Specialist
Preparer Email
T*********@s**************.com
Preparer Telephone
281-637-6576
Preparer Fax
281-637-6425
Prepared Date
2013-03-19 00:00:00
Authorizer Name
T*** G* N*******
Authorizer Telephone
281-637-6576
Authorizer Title
Dot Compliance Specialist
Authorizer Email
T*********@s**************.com
Narrative
Internal corrosion on 2" sump discharge line found by operator during routine station check. Line segment replaced. Re-submitted on 3/19/2013 to include part e5f per PHMSA request.
Report Received Date 2011-11-11 00:00:00
Iyear 2011
Report Number 20110417
Supplemental Number 17586
Report Type Supplemental Final
Operator Id 22442 PHMSA Enforcement
Name West Texas Gulf Pipeline Co
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2011-10-12 07:45:00
Location Latitude 32.4819 Google Maps OpenStreetMap
Location Longitude -94.8351 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 1
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2011-10-12 07:45:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2011-10-12 07:45:00
Restart Datetime 2011-10-12 16:20:00
On Site Datetime 2011-10-12 07:45:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Wtg-Longview Station
Segment Name Wtg-Sump Discharge Line
Onshore State Abbreviation Tx
Onshore Postal Code 75604
Onshore City Name Longview
Onshore County Name Gregg
Designated Location Milepost/valve Station
Designated Name Longview Sta.
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Release Type Leak
Leak Type Pinhole
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 82
Est Cost Prop Damage 2095
Est Cost Emergency 1598
Est Cost Environmental 745
Est Cost Other 0
Prpty 4520
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Preparer Name T*** G* N*******
Preparer Title Dot Compliance Specialist
Preparer Email T*********@s**************.com
Preparer Telephone 281-637-6576
Preparer Fax 281-637-6425
Prepared Date 2013-03-19 00:00:00
Authorizer Name T*** G* N*******
Authorizer Telephone 281-637-6576
Authorizer Title Dot Compliance Specialist
Authorizer Email T*********@s**************.com
Narrative Internal corrosion on 2" sump discharge line found by operator during routine station check. Line segment replaced. Re-submitted on 3/19/2013 to include part e5f per PHMSA request.

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