Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2011-10-17 — OK
Operator
Magellan Pipeline Company, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$20
Incident datetime
2011-10-17 16:55
Report number
Location
OK
Narrative
A 3/8" threaded tubing broke at the fitting connection. The tubing was not properly supported and was subjected to a higher vibration fequency.
Detailed record list
Report Received Date
2011-11-09 00:00:00
Iyear
2011
Report Number
20110415
Supplemental Number
17376
Report Type
Supplemental Final
Operator Id
22610
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2011-10-17 16:55:00
Location Latitude
34.63366
Location Longitude
-97.1581
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
5
Intentional Release Bbls
0
Recovered Bbls
5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2011-10-17 16:55:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2011-10-17 16:55:00
Restart Datetime
2011-10-17 21:15:00
On Site Datetime
2011-10-17 16:55:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Wynnewood Station
Segment Name
Tank Farm
Onshore State Abbreviation
Ok
Onshore Postal Code
73098
Onshore City Name
Wynnewood
Onshore County Name
Garvin
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Tubing
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
235
Est Cost Prop Damage
20
Est Cost Emergency
500
Est Cost Environmental
4745
Est Cost Other
0
Prpty
5500
Accident Psig
100
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The tank pump was running at the time of the reported release, operations control would not be aware of the loss of product.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Defective Or Loose Tubing Or Fitting
Eq Failure Type
Defective Or Loose Tubing Or Fitting
Additional Vibration Ind
Yes
Preparer Name
D******* C*********
Preparer Email
D******************@m*********.com
Prepared Date
2013-03-06 00:00:00
Authorizer Name
D******* C*********
Authorizer Telephone
918-574-7386
Authorizer Title
Sr. Compliance Coordinator
Authorizer Email
No Email Address
Narrative
A 3/8" threaded tubing broke at the fitting connection. The tubing was not properly supported and was subjected to a higher vibration fequency.
| Report Received Date | 2011-11-09 00:00:00 |
|---|---|
| Iyear | 2011 |
| Report Number | 20110415 |
| Supplemental Number | 17376 |
| Report Type | Supplemental Final |
| Operator Id | 22610 PHMSA Enforcement |
| Name | Magellan Pipeline Company, Lp |
| Operator Street Address | 100 West 5th Street |
| Operator City Name | Tulsa |
| Operator State Abbreviation | OK |
| Operator Postal Code | 74103 |
| Local Datetime | 2011-10-17 16:55:00 |
| Location Latitude | 34.63366 Google Maps OpenStreetMap |
| Location Longitude | -97.1581 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Gasoline (Non-Ethanol) |
| Unintentional Release Bbls | 5 |
| Intentional Release Bbls | 0 |
| Recovered Bbls | 5 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Notification From Public |
| Incident Identified Datetime | 2011-10-17 16:55:00 |
| System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2011-10-17 16:55:00 |
| Restart Datetime | 2011-10-17 21:15:00 |
| On Site Datetime | 2011-10-17 16:55:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Wynnewood Station |
| Segment Name | Tank Farm |
| Onshore State Abbreviation | Ok |
| Onshore Postal Code | 73098 |
| Onshore City Name | Wynnewood |
| Onshore County Name | Garvin |
| Designated Location | Milepost/valve Station |
| Designated Name | 0 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Incident Area Subtype | Typical Aboveground Facility Piping Or Appurtenance |
| Crossing | No |
| Pipe Facility Type | Interstate |
| Item Involved | Tubing |
| Material Involved | Carbon Steel |
| Release Type | Leak |
| Leak Type | Connection Failure |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | Yes |
| Soil Remed Ind | Yes |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 235 |
| Est Cost Prop Damage | 20 |
| Est Cost Emergency | 500 |
| Est Cost Environmental | 4745 |
| Est Cost Other | 0 |
| Prpty | 5500 |
| Accident Psig | 100 |
| Mop Psig | 275 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Cpm In Place Ind | No |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | The tank pump was running at the time of the reported release, operations control would not be aware of the loss of product. |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Defective Or Loose Tubing Or Fitting |
| Eq Failure Type | Defective Or Loose Tubing Or Fitting |
| Additional Vibration Ind | Yes |
| Preparer Name | D******* C********* |
| Preparer Email | D******************@m*********.com |
| Prepared Date | 2013-03-06 00:00:00 |
| Authorizer Name | D******* C********* |
| Authorizer Telephone | 918-574-7386 |
| Authorizer Title | Sr. Compliance Coordinator |
| Authorizer Email | No Email Address |
| Narrative | A 3/8" threaded tubing broke at the fitting connection. The tubing was not properly supported and was subjected to a higher vibration fequency. |
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