GD incident on 2011-11-09 — OK

Operator
Oklahoma Natural Gas Co
Cause
Locating Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$100
Incident datetime
2011-11-09 13:00
Report number
Location
OK, HUGHES
Narrative
The city of wetumka was excavating for repair of an 8" water line leak. The city work was performed under a valid locate request issued from the one call system. At 13:00 hours on 11-9-2011 the city notified ong that a gas line had been damaged and gas was venting. An ong crew arrived at 13:40 hours and had the gas turned off at 14:24 hours. System was a one way feed. Portions of the system downstream of the damage filled with water from the leaking water line, causing an extended time to return the line to service (see costs in part d, 2, 2.D). Downstream lines were excavated and cleared of water by 17:00 hours on 11-11-2011 with service to all customers restored.
Detailed record list
Occurred At
2011-11-09 13:00:00
Year
2011
Report Received Date
2011-12-07 00:00:00
Iyear
2011.0
Report Number
20110394.0
Supplemental Number
15363.0
Report Type
Original Final
Operator Id
Name
Oklahoma Natural Gas Co
Operator Street Address
401 N. Harvey
Operator City Name
Oklahoma City
Operator State Abbreviation
OK
Operator Postal Code
73102
Local Datetime
2011-11-09 13:00:00
Location Street Address
522 No. Wewoka
Location City Name
Wetumka
Location County Name
Hughes
Location State Abbreviation
OK
Location Postal Code
74883
Location Latitude
Location Longitude
Nrc Rpt Datetime
2011-11-11 17:50:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
15.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2011-11-09 13:00:00
On Site Datetime
2011-11-09 13:40:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
28.0
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Main
Installation Year
1986.0
Pipe Diameter
2.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Plastic Sdr
11
Material Pe Pipe Code
2406
Release Type
Mechanical Puncture
Puncture Axial
2.0
Puncture Circum
2.0
Class Location Type
Class 2 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
100.0
Est Cost Emergency
16274.0
Est Cost Other
38500.0
Est Cost Other Details
Removal Of Water From Several Lines In The Low Pressure System.
Est Cost Unintentional Release
54874.0
Prpty
109748.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
41.0
Accident Psig
28.0
Normal Psig
28.0
Mop Psig
30.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Notification From Third Party That Caused The Incident
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
Notify Cga Dirt
Yes
Public Row Ind
Yes
Public Subtype
City Street
Excavator Type
Municipality
Excavator Equipment
Backhoe/trackhoe
Work Performed
Water
One Call Notified Ind
Yes
One Call Ticket Num
1.11109e+13
One Call Center Name
Okie One Call
Locator Type
Contract Locator
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
51.0
Root Cause Category
Locating Issue
Root Cause Type
Facility Not Marked Due To Locator Error
Preparer Name
N*** N*****
Preparer Title
Engineer Iii
Preparer Email
N**********@o****.com
Preparer Telephone
918-831-8303
Preparer Fax
918-831-8208
Authorizer Name
B**** B*******
Authorizer Title
Director - Divisions Operations
Authorizer Telephone
405-551-6653
Authorizer Email
B********@o**.com
Narrative
The city of wetumka was excavating for repair of an 8" water line leak. The city work was performed under a valid locate request issued from the one call system. At 13:00 hours on 11-9-2011 the city notified ong that a gas line had been damaged and gas was venting. An ong crew arrived at 13:40 hours and had the gas turned off at 14:24 hours. System was a one way feed. Portions of the system downstream of the damage filled with water from the leaking water line, causing an extended time to return the line to service (see costs in part d, 2, 2.D). Downstream lines were excavated and cleared of water by 17:00 hours on 11-11-2011 with service to all customers restored.
Occurred At 2011-11-09 13:00:00
Year 2011
Report Received Date 2011-12-07 00:00:00
Iyear 2011.0
Report Number 20110394.0
Supplemental Number 15363.0
Report Type Original Final
Operator Id 14210 PHMSA Enforcement
Name Oklahoma Natural Gas Co
Operator Street Address 401 N. Harvey
Operator City Name Oklahoma City
Operator State Abbreviation OK
Operator Postal Code 73102
Local Datetime 2011-11-09 13:00:00
Location Street Address 522 No. Wewoka
Location City Name Wetumka
Location County Name Hughes
Location State Abbreviation OK
Location Postal Code 74883
Location Latitude 35.24256 Google Maps OpenStreetMap
Location Longitude -96.24546 Google Maps OpenStreetMap
Nrc Rpt Datetime 2011-11-11 17:50:00
Nrc Rpt Num 995284 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 15.0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0.0
Incident Identified Datetime 2011-11-09 13:00:00
On Site Datetime 2011-11-09 13:40:00
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 28.0
Crossing No
Pipe Facility Type Privately Owned
System Part Involved Main
Installation Year 1986.0
Pipe Diameter 2.0
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Plastic
Plastic Type Polyethylene (Pe)
Plastic Sdr 11
Material Pe Pipe Code 2406
Release Type Mechanical Puncture
Puncture Axial 2.0
Puncture Circum 2.0
Class Location Type Class 2 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 100.0
Est Cost Emergency 16274.0
Est Cost Other 38500.0
Est Cost Other Details Removal Of Water From Several Lines In The Low Pressure System.
Est Cost Unintentional Release 54874.0
Prpty 109748.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 41.0
Accident Psig 28.0
Normal Psig 28.0
Mop Psig 30.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Notification From Third Party That Caused The Incident
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
Notify Cga Dirt Yes
Public Row Ind Yes
Public Subtype City Street
Excavator Type Municipality
Excavator Equipment Backhoe/trackhoe
Work Performed Water
One Call Notified Ind Yes
One Call Ticket Num 1.11109e+13
One Call Center Name Okie One Call
Locator Type Contract Locator
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 51.0
Root Cause Category Locating Issue
Root Cause Type Facility Not Marked Due To Locator Error
Preparer Name N*** N*****
Preparer Title Engineer Iii
Preparer Email N**********@o****.com
Preparer Telephone 918-831-8303
Preparer Fax 918-831-8208
Authorizer Name B**** B*******
Authorizer Title Director - Divisions Operations
Authorizer Telephone 405-551-6653
Authorizer Email B********@o**.com
Narrative The city of wetumka was excavating for repair of an 8" water line leak. The city work was performed under a valid locate request issued from the one call system. At 13:00 hours on 11-9-2011 the city notified ong that a gas line had been damaged and gas was venting. An ong crew arrived at 13:40 hours and had the gas turned off at 14:24 hours. System was a one way feed. Portions of the system downstream of the damage filled with water from the leaking water line, causing an extended time to return the line to service (see costs in part d, 2, 2.D). Downstream lines were excavated and cleared of water by 17:00 hours on 11-11-2011 with service to all customers restored.

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