Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2011-08-31 — OK
Operator
Magellan Pipeline Company, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$0
Incident datetime
2011-08-31 19:05
Report number
Location
OK
Narrative
A corrosion coupon holder was observed to be leaking. The valve isolating the coupon holder was closed to stop the leak. The cap appeared to be not tight enough. The cap was removed, o-ring was inspected and found to be within specifications, so the cap was replaced and tightened and confirmed to be holding. The product released was cleaned up and handled in accordance with company and state guidelines.
Detailed record list
Report Received Date
2011-09-28 00:00:00
Iyear
2011
Report Number
20110366
Supplemental Number
17431
Report Type
Supplemental Final
Operator Id
22610
Name
Magellan Pipeline Company, Lp
Operator Street Address
100 West 5th Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2011-08-31 19:05:00
Location Latitude
43.54571
Location Longitude
-96.79188
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
0.71
Intentional Release Bbls
0
Recovered Bbls
0.71
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Ignite Ind
No
Explode Ind
No
Onshore State Abbreviation
Sd
Onshore Postal Code
57107
Onshore City Name
Sioux Falls
Onshore County Name
Minnehaha
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Corrosion Coupon Holder
Release Type
Leak
Leak Type
Connection Failure
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
0
Est Cost Emergency
125
Est Cost Environmental
100
Est Cost Other
0
Prpty
225
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Defective Or Loose Tubing Or Fitting
Eq Failure Type
Defective Or Loose Tubing Or Fitting
Preparer Name
K****** L* L*******
Preparer Title
Sr. Compliance Coordinator
Preparer Email
K***********@m*********.com
Preparer Telephone
918-574-7315
Preparer Fax
918-574-7246
Prepared Date
2013-03-07 00:00:00
Authorizer Name
K****** L* L*******
Authorizer Telephone
918-574-7315
Authorizer Title
Sr. Compliance Coordinator
Authorizer Email
K***********@m*********.com
Narrative
A corrosion coupon holder was observed to be leaking. The valve isolating the coupon holder was closed to stop the leak. The cap appeared to be not tight enough. The cap was removed, o-ring was inspected and found to be within specifications, so the cap was replaced and tightened and confirmed to be holding. The product released was cleaned up and handled in accordance with company and state guidelines.
| Report Received Date | 2011-09-28 00:00:00 |
|---|---|
| Iyear | 2011 |
| Report Number | 20110366 |
| Supplemental Number | 17431 |
| Report Type | Supplemental Final |
| Operator Id | 22610 PHMSA Enforcement |
| Name | Magellan Pipeline Company, Lp |
| Operator Street Address | 100 West 5th Street |
| Operator City Name | Tulsa |
| Operator State Abbreviation | OK |
| Operator Postal Code | 74103 |
| Local Datetime | 2011-08-31 19:05:00 |
| Location Latitude | 43.54571 Google Maps OpenStreetMap |
| Location Longitude | -96.79188 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Diesel, Fuel Oil, Kerosene, Jet Fuel |
| Unintentional Release Bbls | 0.71 |
| Intentional Release Bbls | 0 |
| Recovered Bbls | 0.71 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Ignite Ind | No |
| Explode Ind | No |
| Onshore State Abbreviation | Sd |
| Onshore Postal Code | 57107 |
| Onshore City Name | Sioux Falls |
| Onshore County Name | Minnehaha |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Interstate |
| Item Involved | Other |
| Item Involved Details | Corrosion Coupon Holder |
| Release Type | Leak |
| Leak Type | Connection Failure |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| Other Pop Ind | Yes |
| Other Pop Yes No | Yes |
| Usa Drinking Ind | Yes |
| Usa Drinking Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 0 |
| Est Cost Prop Damage | 0 |
| Est Cost Emergency | 125 |
| Est Cost Environmental | 100 |
| Est Cost Other | 0 |
| Prpty | 225 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Defective Or Loose Tubing Or Fitting |
| Eq Failure Type | Defective Or Loose Tubing Or Fitting |
| Preparer Name | K****** L* L******* |
| Preparer Title | Sr. Compliance Coordinator |
| Preparer Email | K***********@m*********.com |
| Preparer Telephone | 918-574-7315 |
| Preparer Fax | 918-574-7246 |
| Prepared Date | 2013-03-07 00:00:00 |
| Authorizer Name | K****** L* L******* |
| Authorizer Telephone | 918-574-7315 |
| Authorizer Title | Sr. Compliance Coordinator |
| Authorizer Email | K***********@m*********.com |
| Narrative | A corrosion coupon holder was observed to be leaking. The valve isolating the coupon holder was closed to stop the leak. The cap appeared to be not tight enough. The cap was removed, o-ring was inspected and found to be within specifications, so the cap was replaced and tightened and confirmed to be holding. The product released was cleaned up and handled in accordance with company and state guidelines. |
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