HL incident on 2011-08-23 — TX

Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$28
Incident datetime
2011-08-23 06:45
Report number
Location
TX
Narrative
9/21/2011 - john sterrett a third party contacted field operations of a vapor cloud. A field technician was called out and verified the leak was at a crossover valve. Both lines connected to the crossover were blocked in. The crossover was then blocked in and blown down for repair. The end connection of a small body bleed check valve on the northbound side of a general twin seal crossover valve failed. County sheriff and fire department were called as a courtesy. The small check valve and associated tubing assembly was replaced, and both lines were returned to service within approximately 2 hours of discovery of the leak. The incident did not meet the criteria for an nrc telephonic report. 7/19/2012 - nhan truong a kiefner & associates, inc. Lab analysis received on june 22, 2012 (attached) concluded that the 1-inch fitting failed by a fatigue crack that initiated on the internal surface of the threaded portion of the fitting. The crack propagated nearly completely around the circumference of the fitting before it failed. The source of the alternating stress that caused the fatigue was not identified.
Detailed record list
Report Received Date
2011-09-21 00:00:00
Iyear
2011
Report Number
20110355
Supplemental Number
17648
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2011-08-23 06:45:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Other Hvl
Commodity Details
Y-Grade
Unintentional Release Bbls
19.86
Intentional Release Bbls
17.28
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2011-08-23 06:45:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2011-08-23 07:25:00
Restart Datetime
2011-08-23 08:52:00
On Site Datetime
2011-08-23 07:00:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Mocane Station
Segment Name
Red And Blue Line Crossover
Onshore State Abbreviation
Ok
Onshore Postal Code
73938
Onshore City Name
Forgan
Onshore County Name
Beaver
Designated Location
Survey Station No.
Designated Name
5721+45
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Other
Incident Area Details
Pump Station Crossover
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
End Connection Of Body Bleed Check Valve
Installation Year
1998
Material Involved
Material Other Than Carbon Steel
Material Details
Stainless Steel
Release Type
Other
Release Type Details
End Connection Of A Small Body Bleed Check Valve On A Crossover Valve Failed
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
1714
Est Cost Prop Damage
28
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
1742
Accident Psig
866
Mop Psig
1298
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Threaded Fitting
Eq Additional Other Ind
Yes
Eq Additional Other Details
Fatigue Cracking
Preparer Name
N*** V* T*****
Preparer Title
Pipeline Compliance Engineer
Preparer Email
N*******@e****.com
Preparer Telephone
713-381-2493
Preparer Fax
713-381-6660
Prepared Date
2013-03-22 00:00:00
Authorizer Name
N*** V* T*****
Authorizer Telephone
713-381-2493
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
N*******@e****.com
Narrative
9/21/2011 - john sterrett a third party contacted field operations of a vapor cloud. A field technician was called out and verified the leak was at a crossover valve. Both lines connected to the crossover were blocked in. The crossover was then blocked in and blown down for repair. The end connection of a small body bleed check valve on the northbound side of a general twin seal crossover valve failed. County sheriff and fire department were called as a courtesy. The small check valve and associated tubing assembly was replaced, and both lines were returned to service within approximately 2 hours of discovery of the leak. The incident did not meet the criteria for an nrc telephonic report. 7/19/2012 - nhan truong a kiefner & associates, inc. Lab analysis received on june 22, 2012 (attached) concluded that the 1-inch fitting failed by a fatigue crack that initiated on the internal surface of the threaded portion of the fitting. The crack propagated nearly completely around the circumference of the fitting before it failed. The source of the alternating stress that caused the fatigue was not identified.
Report Received Date 2011-09-21 00:00:00
Iyear 2011
Report Number 20110355
Supplemental Number 17648
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2011-08-23 06:45:00
Location Latitude 36.9006 Google Maps OpenStreetMap
Location Longitude -100.39243 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Other Hvl
Commodity Details Y-Grade
Unintentional Release Bbls 19.86
Intentional Release Bbls 17.28
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2011-08-23 06:45:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2011-08-23 07:25:00
Restart Datetime 2011-08-23 08:52:00
On Site Datetime 2011-08-23 07:00:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Mocane Station
Segment Name Red And Blue Line Crossover
Onshore State Abbreviation Ok
Onshore Postal Code 73938
Onshore City Name Forgan
Onshore County Name Beaver
Designated Location Survey Station No.
Designated Name 5721+45
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Other
Incident Area Details Pump Station Crossover
Crossing No
Pipe Facility Type Interstate
Item Involved Other
Item Involved Details End Connection Of Body Bleed Check Valve
Installation Year 1998
Material Involved Material Other Than Carbon Steel
Material Details Stainless Steel
Release Type Other
Release Type Details End Connection Of A Small Body Bleed Check Valve On A Crossover Valve Failed
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 1714
Est Cost Prop Damage 28
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 1742
Accident Psig 866
Mop Psig 1298
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Threaded Connection/coupling Failure
Eq Failure Type Threaded Connection/coupling Failure
Other Stripped Ind Threaded Fitting
Eq Additional Other Ind Yes
Eq Additional Other Details Fatigue Cracking
Preparer Name N*** V* T*****
Preparer Title Pipeline Compliance Engineer
Preparer Email N*******@e****.com
Preparer Telephone 713-381-2493
Preparer Fax 713-381-6660
Prepared Date 2013-03-22 00:00:00
Authorizer Name N*** V* T*****
Authorizer Telephone 713-381-2493
Authorizer Title Pipeline Compliance Engineer
Authorizer Email N*******@e****.com
Narrative 9/21/2011 - john sterrett a third party contacted field operations of a vapor cloud. A field technician was called out and verified the leak was at a crossover valve. Both lines connected to the crossover were blocked in. The crossover was then blocked in and blown down for repair. The end connection of a small body bleed check valve on the northbound side of a general twin seal crossover valve failed. County sheriff and fire department were called as a courtesy. The small check valve and associated tubing assembly was replaced, and both lines were returned to service within approximately 2 hours of discovery of the leak. The incident did not meet the criteria for an nrc telephonic report. 7/19/2012 - nhan truong a kiefner & associates, inc. Lab analysis received on june 22, 2012 (attached) concluded that the 1-inch fitting failed by a fatigue crack that initiated on the internal surface of the threaded portion of the fitting. The crack propagated nearly completely around the circumference of the fitting before it failed. The source of the alternating stress that caused the fatigue was not identified.

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