HL incident on 2011-08-22 — KS

Operator
Nustar Pipeline Operating Partnership L.p.
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$30,000
Incident datetime
2011-08-22 16:30
Report number
Location
KS
Narrative
The leak occurred near check valve 16-3c with 2.6 foot pups on each end of the valve. The entire section was cut out and sent to keifner for evaluation. Still under investigation. Investigation is now complete. The source of the leak was porosity in the cast steel check valve.
Detailed record list
Report Received Date
2011-09-16 00:00:00
Iyear
2011
Report Number
20110347
Supplemental Number
16546
Report Type
Supplemental Final
Operator Id
Name
Nustar Pipeline Operating Partnership L.p.
Operator Street Address
7340 W. 21st Street N, Suite 200
Operator City Name
Wichita
Operator State Abbreviation
KS
Operator Postal Code
67205
Local Datetime
2011-08-22 16:30:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Anhydrous Ammonia
Unintentional Release Bbls
0.2
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2011-08-22 16:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2011-08-22 16:58:00
Restart Datetime
2011-08-26 18:00:00
On Site Datetime
2011-08-24 07:00:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Ft. Madison Lateral
Segment Name
Ft. Madison Lateral
Onshore State Abbreviation
Ia
Onshore Postal Code
52627
Onshore City Name
Ft. Madison
Onshore County Name
Lee
Designated Location
Milepost/valve Station
Designated Name
16-3c
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Pipe Facility Type
Interstate
Item Involved
Valve
Pipe Type
Pipe Body
Valve Type
Auxiliary Or Other Valve
Release Type
Leak
Leak Type
Other
Leak Type Other
Porosity In Check Valve Body
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Commercially Nav Ind
Yes
Commercially Nav Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Usa Ecological Ind
Yes
Usa Ecological Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
13
Est Cost Prop Damage
30000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
30013
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Eq Failure Type
Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Preparer Name
D***** J* T******
Preparer Title
Director - Hse
Preparer Email
D**********@n***********.com
Preparer Telephone
316-721-7056
Preparer Fax
316-773-9001
Prepared Date
2012-04-13 00:00:00
Authorizer Name
G***** K*********
Authorizer Telephone
316-721-7052
Authorizer Title
Vice President General Manager
Authorizer Email
G**************@n***********.com
Narrative
The leak occurred near check valve 16-3c with 2.6 foot pups on each end of the valve. The entire section was cut out and sent to keifner for evaluation. Still under investigation. Investigation is now complete. The source of the leak was porosity in the cast steel check valve.
Report Received Date 2011-09-16 00:00:00
Iyear 2011
Report Number 20110347
Supplemental Number 16546
Report Type Supplemental Final
Operator Id 10012 PHMSA Enforcement
Name Nustar Pipeline Operating Partnership L.p.
Operator Street Address 7340 W. 21st Street N, Suite 200
Operator City Name Wichita
Operator State Abbreviation KS
Operator Postal Code 67205
Local Datetime 2011-08-22 16:30:00
Location Latitude 40.596305 Google Maps OpenStreetMap
Location Longitude -91.411283 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Anhydrous Ammonia
Unintentional Release Bbls 0.2
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Incident Identified Datetime 2011-08-22 16:30:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2011-08-22 16:58:00
Restart Datetime 2011-08-26 18:00:00
On Site Datetime 2011-08-24 07:00:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Ft. Madison Lateral
Segment Name Ft. Madison Lateral
Onshore State Abbreviation Ia
Onshore Postal Code 52627
Onshore City Name Ft. Madison
Onshore County Name Lee
Designated Location Milepost/valve Station
Designated Name 16-3c
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Pipe Facility Type Interstate
Item Involved Valve
Pipe Type Pipe Body
Valve Type Auxiliary Or Other Valve
Release Type Leak
Leak Type Other
Leak Type Other Porosity In Check Valve Body
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
Commercially Nav Ind Yes
Commercially Nav Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No Yes
Usa Ecological Ind Yes
Usa Ecological Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 13
Est Cost Prop Damage 30000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 30013
Pipeline Function > 20% Smys Regulated Transmission
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Eq Failure Type Failure Of Equipment Body (Except Pump), Tank Plate, Or Other Material
Preparer Name D***** J* T******
Preparer Title Director - Hse
Preparer Email D**********@n***********.com
Preparer Telephone 316-721-7056
Preparer Fax 316-773-9001
Prepared Date 2012-04-13 00:00:00
Authorizer Name G***** K*********
Authorizer Telephone 316-721-7052
Authorizer Title Vice President General Manager
Authorizer Email G**************@n***********.com
Narrative The leak occurred near check valve 16-3c with 2.6 foot pups on each end of the valve. The entire section was cut out and sent to keifner for evaluation. Still under investigation. Investigation is now complete. The source of the leak was porosity in the cast steel check valve.

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