GTG incident on 2011-08-16 — TX

Operator
Natural Gas Pipeline Co Of America (Kmi)
Cause
Incorrect Operation
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 1 injury
Property damage (nominal)
$1,318,206
Incident datetime
2011-08-16 09:53
Report number
Location
TX
Narrative
A crew performed maintenance on compressor unit #5 to repair an oil leak below the turbocharger. To repair the leak, the crew intended to support the turbocharger stand with a hydraulic jack, cut the two legs off with a portable grinder, install a gasket under each leg, and then replace each leg to its original position by welding at the location of the cut. The crew completed all of these tasks up to the point of welding the second leg. The incident occurred when the crew was welding the second leg. In order to have sufficient room to perform work on the second leg, the crew had removed the crankcase breather. The crew had used portable gas detectors in and around the work area, but they failed to position the portable gas detectors inside the crankcase, so the crew was not aware that there was combustible gas in the crankcase. After performing a post-incident investigation, it is believed that there was excessive leakage of the packing gland seals, which resulted in the gas migrating to the crankcase.
Detailed record list
Report Received Date
2011-09-15 00:00:00
Iyear
2011
Report Number
20110343
Supplemental Number
16089
Report Type
Supplemental Final
Operator Id
Name
Natural Gas Pipeline Co Of America (Kmi)
Operator Street Address
1001 Louisiana St, Ste 1000
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2011-08-16 09:53:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2011-08-16 11:10:00
Commodity Released Type
Natural Gas
Unintentional Release
0.01
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
Yes
Num Emp Injuries
1
Num Contr Injuries
0
Num Er Injuries
0
Num Worker Injuries
0
Num Gp Injuries
0
Injure
1
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2011-08-16 09:54:00
Restart Datetime
2011-08-20 08:23:00
Ignite Ind
Yes
Explode Ind
Yes
Num Pub Evacuated
0
Incident Identified Datetime
2011-08-16 09:53:00
On Site Datetime
2011-08-16 09:53:00
On Off Shore
Onshore
Onshore State Abbreviation
Il
Onshore Postal Code
60941
Onshore City Name
Herscher
Onshore County Name
Kankakee
Pipe Fac Name
Herscher Storage Facility Station 201
Segment Name
Herscher Storage Facility
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Inside A Building
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Compressor Station Equipment And Piping
Item Involved
Compressor
Installation Year
1952
Material Involved
Material Other Than Carbon Steel Or Plastic
Material Details
Compressor Engine Crankcase
Release Type
Other
Release Type Details
Crankcase Explosion
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
606
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
1
Est Cost Intentional Release
250
Est Cost Prop Damage
1318206
Est Cost Emergency
2612
Est Cost Other
92910
Est Cost Other Details
Incident Investigation Costs
Prpty
1413979
Accident Psig
0
Mop Psig
858
Mop Cfr Section
Not On Omb-Approved Form When Submitted
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Unit 5 was offline at the time of the incident and therefore was not monitored by the contoller
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
3
Num Employees Failed
0
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
The Crew Did Not Identify Whether There May Have Been A Combustible Mixture Inside The Crankcase, Which Was A Potential Hazard. The Crew Also Did Not Use The Portable Gas Detector Inside The Crankcase And Did Not Cover And/or Adequately Cover The Opening To The Crankcase.
Related Other Ind
Yes
Operation Related Details
See The Investigation Report Submitted To Phmsa And Dated June 18, 2012
Category Type
Other Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
M***** M*****
Preparer Title
Compliance Engineer
Preparer Email
M************@k***********.com
Preparer Telephone
2053253863
Preparer Fax
2053253508
Authorizer Name
R*** G*****
Authorizer Title
Director Compliance Codes And Standards
Authorizer Telephone
7134205433
Authorizer Email
R**********@k***********.com
Narrative
A crew performed maintenance on compressor unit #5 to repair an oil leak below the turbocharger. To repair the leak, the crew intended to support the turbocharger stand with a hydraulic jack, cut the two legs off with a portable grinder, install a gasket under each leg, and then replace each leg to its original position by welding at the location of the cut. The crew completed all of these tasks up to the point of welding the second leg. The incident occurred when the crew was welding the second leg. In order to have sufficient room to perform work on the second leg, the crew had removed the crankcase breather. The crew had used portable gas detectors in and around the work area, but they failed to position the portable gas detectors inside the crankcase, so the crew was not aware that there was combustible gas in the crankcase. After performing a post-incident investigation, it is believed that there was excessive leakage of the packing gland seals, which resulted in the gas migrating to the crankcase.
Report Received Date 2011-09-15 00:00:00
Iyear 2011
Report Number 20110343
Supplemental Number 16089
Report Type Supplemental Final
Operator Id 13120 PHMSA Enforcement
Name Natural Gas Pipeline Co Of America (Kmi)
Operator Street Address 1001 Louisiana St, Ste 1000
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2011-08-16 09:53:00
Location Latitude 41.03423 Google Maps OpenStreetMap
Location Longitude -88.08837 Google Maps OpenStreetMap
Nrc Rpt Num 986120 NRC Report How to search
Nrc Rpt Datetime 2011-08-16 11:10:00
Commodity Released Type Natural Gas
Unintentional Release 0.01
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind Yes
Num Emp Injuries 1
Num Contr Injuries 0
Num Er Injuries 0
Num Worker Injuries 0
Num Gp Injuries 0
Injure 1
Shutdown Due Accident Ind Yes
Shutdown Datetime 2011-08-16 09:54:00
Restart Datetime 2011-08-20 08:23:00
Ignite Ind Yes
Explode Ind Yes
Num Pub Evacuated 0
Incident Identified Datetime 2011-08-16 09:53:00
On Site Datetime 2011-08-16 09:53:00
On Off Shore Onshore
Onshore State Abbreviation Il
Onshore Postal Code 60941
Onshore City Name Herscher
Onshore County Name Kankakee
Pipe Fac Name Herscher Storage Facility Station 201
Segment Name Herscher Storage Facility
Federal No
Location Type Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Inside A Building
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Compressor Station Equipment And Piping
Item Involved Compressor
Installation Year 1952
Material Involved Material Other Than Carbon Steel Or Plastic
Material Details Compressor Engine Crankcase
Release Type Other
Release Type Details Crankcase Explosion
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 606
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 1
Est Cost Intentional Release 250
Est Cost Prop Damage 1318206
Est Cost Emergency 2612
Est Cost Other 92910
Est Cost Other Details Incident Investigation Costs
Prpty 1413979
Accident Psig 0
Mop Psig 858
Mop Cfr Section Not On Omb-Approved Form When Submitted View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Unit 5 was offline at the time of the incident and therefore was not monitored by the contoller
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 3
Num Employees Failed 0
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details The Crew Did Not Identify Whether There May Have Been A Combustible Mixture Inside The Crankcase, Which Was A Potential Hazard. The Crew Also Did Not Use The Portable Gas Detector Inside The Crankcase And Did Not Cover And/or Adequately Cover The Opening To The Crankcase.
Related Other Ind Yes
Operation Related Details See The Investigation Report Submitted To Phmsa And Dated June 18, 2012
Category Type Other Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name M***** M*****
Preparer Title Compliance Engineer
Preparer Email M************@k***********.com
Preparer Telephone 2053253863
Preparer Fax 2053253508
Authorizer Name R*** G*****
Authorizer Title Director Compliance Codes And Standards
Authorizer Telephone 7134205433
Authorizer Email R**********@k***********.com
Narrative A crew performed maintenance on compressor unit #5 to repair an oil leak below the turbocharger. To repair the leak, the crew intended to support the turbocharger stand with a hydraulic jack, cut the two legs off with a portable grinder, install a gasket under each leg, and then replace each leg to its original position by welding at the location of the cut. The crew completed all of these tasks up to the point of welding the second leg. The incident occurred when the crew was welding the second leg. In order to have sufficient room to perform work on the second leg, the crew had removed the crankcase breather. The crew had used portable gas detectors in and around the work area, but they failed to position the portable gas detectors inside the crankcase, so the crew was not aware that there was combustible gas in the crankcase. After performing a post-incident investigation, it is believed that there was excessive leakage of the packing gland seals, which resulted in the gas migrating to the crankcase.

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