HL incident on 2011-08-16 — PA

Operator
Buckeye Partners, Lp
Cause
Other Outside Force Damage
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$18,103
Incident datetime
2011-08-16 15:03
Report number
Location
PA
Narrative
At 3:03 pm on august 16, 2011 a release was identified by a third party on the bn160as line section in sharpsburg, il. The third party who identified the accident hit the line while mowing. The third party immediately notified the buckeye control center using the phone number from the nearby line marker. The line was isolated and emergency response procedures were initiated. All appropriate notifications were made. Approximately 840 gallons of gasoline were released. All free product was recovered, and impacted soil and surface water was removed. All remediation has been completed. A temporary pipeline repair has been completed and tested, and the line is back in service. Permanent repairs will be completed in october 2011.
Detailed record list
Report Received Date
2011-09-14 00:00:00
Iyear
2011
Report Number
20110341
Supplemental Number
16386
Report Type
Supplemental Final
Operator Id
Name
Buckeye Partners, Lp
Operator Street Address
The Buckeye Building 6161 Hamilton Boulevar
Operator City Name
Allentown
Operator State Abbreviation
PA
Operator Postal Code
18106
Local Datetime
2011-08-16 15:03:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
20
Intentional Release Bbls
0
Recovered Bbls
20
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Third Party That Caused The Accident
Incident Identified Datetime
2011-08-16 15:03:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2011-08-16 15:19:00
Restart Datetime
2011-08-22 16:35:00
On Site Datetime
2011-08-16 16:00:00
Nrc Rpt Datetime
2011-08-16 16:23:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Barnett To Auburn
Segment Name
Bn160as
Onshore State Abbreviation
Il
Onshore Postal Code
62568
Onshore City Name
Sharpsburg
Onshore County Name
Christian
Designated Location
Survey Station No.
Designated Name
363683
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Aboveground
Incident Area Subtype
In Or Spanning An Open Ditch
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
14
Pipe Wall Thickness
0.313
Pipe Smys
48000
Pipe Specification
Api 5lx
Pipe Seam Type
Seamless
Pipe Manufacturer
Uss
Pipe Coating Type
Paint
Installation Year
1953
Manufactured Year
1953
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Third Party Damage Not Related To Excavation.
Wildlife Impact Ind
Yes
Fish Aquatic Impact Ind
Yes
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Surface Water Remed Ind
Yes
Groundwater Remed Ind
Yes
Soil Remed Ind
Yes
Vegetation Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
7
Rel Water Name
Un-Named Drainage Ditch
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
18103
Est Cost Emergency
6977
Est Cost Environmental
150000
Est Cost Other
0
Prpty
175080
Accident Psig
868
Mop Psig
1142
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
209510
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Release was the direct result of the actions of the third party who caused the accident.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Outside Force Damage
Cause Details
Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Outside Force Type
Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Vehicle Subtype
Third Party
Preparer Name
L** H*****
Preparer Title
Compliance Specialist
Preparer Email
L******@b******.com
Preparer Telephone
610-904-4248
Preparer Fax
610-904-4545
Prepared Date
2012-02-02 00:00:00
Authorizer Name
J*** R*******
Authorizer Telephone
610-904-4185
Authorizer Title
Regulatory Compliance Group Leader
Authorizer Email
J********@b******.com
Narrative
At 3:03 pm on august 16, 2011 a release was identified by a third party on the bn160as line section in sharpsburg, il. The third party who identified the accident hit the line while mowing. The third party immediately notified the buckeye control center using the phone number from the nearby line marker. The line was isolated and emergency response procedures were initiated. All appropriate notifications were made. Approximately 840 gallons of gasoline were released. All free product was recovered, and impacted soil and surface water was removed. All remediation has been completed. A temporary pipeline repair has been completed and tested, and the line is back in service. Permanent repairs will be completed in october 2011.
Report Received Date 2011-09-14 00:00:00
Iyear 2011
Report Number 20110341
Supplemental Number 16386
Report Type Supplemental Final
Operator Id 1845 PHMSA Enforcement
Name Buckeye Partners, Lp
Operator Street Address The Buckeye Building 6161 Hamilton Boulevar
Operator City Name Allentown
Operator State Abbreviation PA
Operator Postal Code 18106
Local Datetime 2011-08-16 15:03:00
Location Latitude 39.61412 Google Maps OpenStreetMap
Location Longitude -89.34578 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 20
Intentional Release Bbls 0
Recovered Bbls 20
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Third Party That Caused The Accident
Incident Identified Datetime 2011-08-16 15:03:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2011-08-16 15:19:00
Restart Datetime 2011-08-22 16:35:00
On Site Datetime 2011-08-16 16:00:00
Nrc Rpt Datetime 2011-08-16 16:23:00
Nrc Rpt Num 986185 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Barnett To Auburn
Segment Name Bn160as
Onshore State Abbreviation Il
Onshore Postal Code 62568
Onshore City Name Sharpsburg
Onshore County Name Christian
Designated Location Survey Station No.
Designated Name 363683
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Aboveground
Incident Area Subtype In Or Spanning An Open Ditch
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 14
Pipe Wall Thickness 0.313
Pipe Smys 48000
Pipe Specification Api 5lx
Pipe Seam Type Seamless
Pipe Manufacturer Uss
Pipe Coating Type Paint
Installation Year 1953
Manufactured Year 1953
Material Involved Carbon Steel
Release Type Other
Release Type Details Third Party Damage Not Related To Excavation.
Wildlife Impact Ind Yes
Fish Aquatic Impact Ind Yes
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Surface Water Remed Ind Yes
Groundwater Remed Ind Yes
Soil Remed Ind Yes
Vegetation Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 7
Rel Water Name Un-Named Drainage Ditch
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 18103
Est Cost Emergency 6977
Est Cost Environmental 150000
Est Cost Other 0
Prpty 175080
Accident Psig 868
Mop Psig 1142
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 209510
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Release was the direct result of the actions of the third party who caused the accident.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Outside Force Damage
Cause Details Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Outside Force Type Damage By Car, Truck, Or Other Motorized Vehicle/equipment Not Engaged In Excavation
Vehicle Subtype Third Party
Preparer Name L** H*****
Preparer Title Compliance Specialist
Preparer Email L******@b******.com
Preparer Telephone 610-904-4248
Preparer Fax 610-904-4545
Prepared Date 2012-02-02 00:00:00
Authorizer Name J*** R*******
Authorizer Telephone 610-904-4185
Authorizer Title Regulatory Compliance Group Leader
Authorizer Email J********@b******.com
Narrative At 3:03 pm on august 16, 2011 a release was identified by a third party on the bn160as line section in sharpsburg, il. The third party who identified the accident hit the line while mowing. The third party immediately notified the buckeye control center using the phone number from the nearby line marker. The line was isolated and emergency response procedures were initiated. All appropriate notifications were made. Approximately 840 gallons of gasoline were released. All free product was recovered, and impacted soil and surface water was removed. All remediation has been completed. A temporary pipeline repair has been completed and tested, and the line is back in service. Permanent repairs will be completed in october 2011.

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