HL incident on 2011-08-12 — TX

Operator
Enterprise Crude Pipeline Llc
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$25,000
Incident datetime
2011-08-12 09:15
Report number
Location
TX
Narrative
8-12-2011 employee discovered stain area near 36" pig trap. Hydro vacuum trucks have been ordered and response team on site. Trap is blocked isolated. 8-15-2011 at 16:00 hrs confirmed that the leak is on the 12" kicker line on the 36" pig trap. The leak is at the 6 o'clock position in a spot 10 ft from the 90 degree elbow in the ground. Pinhole leak and appears to be internal corrosion. 11-14-2011 on 8/23/2011 a 50 ft section of the 12" kicker line on the 36" pig receiver was cut out and replaced. It was found to have internal corrosion. To alleviate this problem in the future we will be writing a procedure to flush (2) 12' kicker lines once a month. I will have this procedure put in empac.
Detailed record list
Report Received Date
2011-09-12 00:00:00
Iyear
2011
Report Number
20110337
Supplemental Number
16453
Report Type
Supplemental Final
Operator Id
Name
Enterprise Crude Pipeline Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2011-08-12 09:15:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
5
Intentional Release Bbls
0
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2011-08-12 09:15:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Leak Was On A 36" Pig Barrel
On Site Datetime
2011-08-12 09:15:00
Nrc Rpt Datetime
2011-08-12 11:15:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Texas City Tank Farm
Segment Name
Seaway
Onshore State Abbreviation
Tx
Onshore Postal Code
77592
Onshore City Name
Texas City
Onshore County Name
Galveston
Designated Location
Milepost/valve Station
Designated Name
Mp 0.0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Scraper/pig Trap
Installation Year
2004
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
400
Est Cost Prop Damage
25000
Est Cost Emergency
0
Est Cost Environmental
15000
Est Cost Other
0
Prpty
40400
Accident Psig
0
Mop Psig
0
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak was small and contained.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Erosion Ind
Yes
Int Field Exam Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
Yes
Corrosion Lining
No
Cleaning Dewatering
Yes
Corrosion Coupons
Yes
Preparer Name
N*** B******
Preparer Title
Sr Pipeline Compliance Specialist
Preparer Email
W********@e****.com
Preparer Telephone
713-381-3536
Preparer Fax
281-887-7704
Prepared Date
2012-02-27 00:00:00
Authorizer Name
N*** B******
Authorizer Telephone
713-381-3536
Authorizer Title
Sr Pipeline Compliance Specialist
Authorizer Email
W********@e****.com
Narrative
8-12-2011 employee discovered stain area near 36" pig trap. Hydro vacuum trucks have been ordered and response team on site. Trap is blocked isolated. 8-15-2011 at 16:00 hrs confirmed that the leak is on the 12" kicker line on the 36" pig trap. The leak is at the 6 o'clock position in a spot 10 ft from the 90 degree elbow in the ground. Pinhole leak and appears to be internal corrosion. 11-14-2011 on 8/23/2011 a 50 ft section of the 12" kicker line on the 36" pig receiver was cut out and replaced. It was found to have internal corrosion. To alleviate this problem in the future we will be writing a procedure to flush (2) 12' kicker lines once a month. I will have this procedure put in empac.
Report Received Date 2011-09-12 00:00:00
Iyear 2011
Report Number 20110337
Supplemental Number 16453
Report Type Supplemental Final
Operator Id 30829 PHMSA Enforcement
Name Enterprise Crude Pipeline Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2011-08-12 09:15:00
Location Latitude 29.206868 Google Maps OpenStreetMap
Location Longitude -94.561023 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 5
Intentional Release Bbls 0
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2011-08-12 09:15:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Leak Was On A 36" Pig Barrel
On Site Datetime 2011-08-12 09:15:00
Nrc Rpt Datetime 2011-08-12 11:15:00
Nrc Rpt Num 985723 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Texas City Tank Farm
Segment Name Seaway
Onshore State Abbreviation Tx
Onshore Postal Code 77592
Onshore City Name Texas City
Onshore County Name Galveston
Designated Location Milepost/valve Station
Designated Name Mp 0.0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Under Soil
Crossing No
Pipe Facility Type Interstate
Item Involved Scraper/pig Trap
Installation Year 2004
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 400
Est Cost Prop Damage 25000
Est Cost Emergency 0
Est Cost Environmental 15000
Est Cost Other 0
Prpty 40400
Accident Psig 0
Mop Psig 0
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Leak was small and contained.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Erosion Ind Yes
Int Field Exam Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors Yes
Corrosion Lining No
Cleaning Dewatering Yes
Corrosion Coupons Yes
Preparer Name N*** B******
Preparer Title Sr Pipeline Compliance Specialist
Preparer Email W********@e****.com
Preparer Telephone 713-381-3536
Preparer Fax 281-887-7704
Prepared Date 2012-02-27 00:00:00
Authorizer Name N*** B******
Authorizer Telephone 713-381-3536
Authorizer Title Sr Pipeline Compliance Specialist
Authorizer Email W********@e****.com
Narrative 8-12-2011 employee discovered stain area near 36" pig trap. Hydro vacuum trucks have been ordered and response team on site. Trap is blocked isolated. 8-15-2011 at 16:00 hrs confirmed that the leak is on the 12" kicker line on the 36" pig trap. The leak is at the 6 o'clock position in a spot 10 ft from the 90 degree elbow in the ground. Pinhole leak and appears to be internal corrosion. 11-14-2011 on 8/23/2011 a 50 ft section of the 12" kicker line on the 36" pig receiver was cut out and replaced. It was found to have internal corrosion. To alleviate this problem in the future we will be writing a procedure to flush (2) 12' kicker lines once a month. I will have this procedure put in empac.

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