HL incident on 2011-08-13 — TX

Operator
Enterprise Products Operating Llc
Cause
Natural Force Damage
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$7,368,470
Incident datetime
2011-08-13 02:16
Report number
Location
TX
Narrative
The downstream pump closest to the failure automatically shutdown on under speed, and the operations controller detected a pressure drop at the same pump station. The controller shutdown upstream pump stations and closed upstream block valves, and after downstream pump stations pulled down the line pressure, the mov at the closest downstream pump station was closed to isolate the failed pipeline segment. The controller notified company personnel and county sheriff offices on both sides of the river. The controller then blocked in and bled down the pressure on the second company operated pipeline in the row. When field operations personnel arrived at the river between 3:00 and 4:00 am, product could not be seen or smelled on the west side, and product could not be seen but could be smelled in the vicinity of aerial marker 271 on the east side of the river. Both the failed line, and the line next to it operated by the operator remain shutdown under corrective action order, cf no. 3-2011-5009h. Divers located a break in the failed line on august 31, but the failure site is still underwater and inaccessible at the time of this report. The product released was natural gasoline, but no released product has been detected other than an odor on first arrival at the east side of the river. The initial volume reported was the line volume estimated between block valves. Most of the product trapped in isolated pipe has since been displaced from the line and was metered. The displaced volume was subtracted from the line fill volume, reducing the estimated unintended release volume. Product in the pipe near the west bank of the river is still not completely displaced. Supplement 6-1-12 the red was restarted on october 22, 2011. Installation of the red lines according to the approved repair plan was completed on january 16, 2012 with the completion of the main line valve motor operator work the amount of natural gasoline displaced from the red line on september 7, 2011 was metered and measured 2952.3 bbl. Approximately 507 gallons of additional natural gasoline was displaced september 28, 2011 and an additional 68 gallons of product was displaced from the red line on october 8, 2011. Pipe segments from both sides of the red line break have been removed from under water. Displacement of residual product with nitrogen was completed on april 11, 2012. The recovered amount of product from this displacement was 129 bbls. The total displacement of natural gasoline to date from the pipeline reduces the estimated release volume to 675 bbls. After the displacement the remaining sections of the affected pipe that could not be removed were either capped and abandoned or capped and placed in an idle state according to the submitted repair plan. Supplement/final 8-7-12 the metallurgical report was completed on july 2, 2012. There were no defects attributed to orginal construction/installation. The failure analysis indicated that the failure occurred because of the stresses associated with the flooding condition.
Detailed record list
Report Received Date
2011-09-10 00:00:00
Iyear
2011
Report Number
20110335
Supplemental Number
18081
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2011-08-13 01:57:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Other
Commodity Details
Natural Gasoline
Unintentional Release Bbls
675
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Controller
Operator Type
Operator Employee
Incident Identified Datetime
2011-08-13 02:16:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2011-08-13 02:19:00
Restart Datetime
2011-10-22 10:02:00
On Site Datetime
2011-08-13 03:30:00
Nrc Rpt Datetime
2011-08-13 04:23:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
West Leg Loop Red Line
Segment Name
Line Id 428
Onshore State Abbreviation
Ia
Onshore Postal Code
51040
Onshore City Name
Onawa
Onshore County Name
Monona
Designated Location
Survey Station No.
Designated Name
14293+63
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Other
Incident Area Details
Exposed By Flood Water Scour
Crossing
Yes
Water Crossing Ind
Yes
Water Type
Uncased
Water Name
Missouri River Flood Plain
Water Depth
15
Water Subtype
Shoreline/bank Crossing
Pipe Facility Type
Interstate
Item Involved
Weld, Including Heat-Affected Zone
Pipe Diameter
8
Pipe Wall Thickness
0.172
Pipe Smys
60000
Pipe Specification
Api5l
Pipe Seam Type
Erw - High Frequency
Pipe Manufacturer
Ipsco Steel
Pipe Coating Type
Cold Applied Tape
Weld Subtype
Pipe Girth Weld
Installation Year
1993
Manufactured Year
1993
Material Involved
Carbon Steel
Release Type
Rupture
Rupture Orient
Circumferential
Rupture Width
2.1
Rupture Length
4.9
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
675
Rel Water Name
Missouririver
Could Be Hca
Yes
Commodity Reached Hca
Yes
Commercially Nav Ind
Yes
Commercially Nav Yes No
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
No
Est Cost Oper Paid
0
Est Cost Gas Released
80595
Est Cost Prop Damage
7368470
Est Cost Emergency
135000
Est Cost Environmental
85000
Est Cost Other
0
Prpty
7669065
Accident Psig
255
Mop Psig
1440
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
56045
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Natural Force Damage
Cause Details
Heavy Rains/floods
Natural Force Type
Heavy Rains/floods
Heavy Rains Subtype
Washouts/scouring
Nf Extreme Weather Ind
Yes
Nf Other Ind
Yes
Nf Extreme Weather Details
Prolonged Flooding Of The Missouri River
Preparer Name
M****** S********
Preparer Title
Sr. Pipeline Compliance Specialist
Preparer Email
M*********@e****.com
Preparer Telephone
713-381-8209
Preparer Fax
713-381-6660
Prepared Date
2013-05-20 00:00:00
Authorizer Name
M****** S********
Authorizer Telephone
713-381-8209
Authorizer Title
Sr. Pipeline Compliance Specialist
Authorizer Email
M*********@e****.com
Narrative
The downstream pump closest to the failure automatically shutdown on under speed, and the operations controller detected a pressure drop at the same pump station. The controller shutdown upstream pump stations and closed upstream block valves, and after downstream pump stations pulled down the line pressure, the mov at the closest downstream pump station was closed to isolate the failed pipeline segment. The controller notified company personnel and county sheriff offices on both sides of the river. The controller then blocked in and bled down the pressure on the second company operated pipeline in the row. When field operations personnel arrived at the river between 3:00 and 4:00 am, product could not be seen or smelled on the west side, and product could not be seen but could be smelled in the vicinity of aerial marker 271 on the east side of the river. Both the failed line, and the line next to it operated by the operator remain shutdown under corrective action order, cf no. 3-2011-5009h. Divers located a break in the failed line on august 31, but the failure site is still underwater and inaccessible at the time of this report. The product released was natural gasoline, but no released product has been detected other than an odor on first arrival at the east side of the river. The initial volume reported was the line volume estimated between block valves. Most of the product trapped in isolated pipe has since been displaced from the line and was metered. The displaced volume was subtracted from the line fill volume, reducing the estimated unintended release volume. Product in the pipe near the west bank of the river is still not completely displaced. Supplement 6-1-12 the red was restarted on october 22, 2011. Installation of the red lines according to the approved repair plan was completed on january 16, 2012 with the completion of the main line valve motor operator work the amount of natural gasoline displaced from the red line on september 7, 2011 was metered and measured 2952.3 bbl. Approximately 507 gallons of additional natural gasoline was displaced september 28, 2011 and an additional 68 gallons of product was displaced from the red line on october 8, 2011. Pipe segments from both sides of the red line break have been removed from under water. Displacement of residual product with nitrogen was completed on april 11, 2012. The recovered amount of product from this displacement was 129 bbls. The total displacement of natural gasoline to date from the pipeline reduces the estimated release volume to 675 bbls. After the displacement the remaining sections of the affected pipe that could not be removed were either capped and abandoned or capped and placed in an idle state according to the submitted repair plan. Supplement/final 8-7-12 the metallurgical report was completed on july 2, 2012. There were no defects attributed to orginal construction/installation. The failure analysis indicated that the failure occurred because of the stresses associated with the flooding condition.
Report Received Date 2011-09-10 00:00:00
Iyear 2011
Report Number 20110335
Supplemental Number 18081
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2011-08-13 01:57:00
Location Latitude 42.00461 Google Maps OpenStreetMap
Location Longitude -96.23684 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Other
Commodity Details Natural Gasoline
Unintentional Release Bbls 675
Intentional Release Bbls 0
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Controller
Operator Type Operator Employee
Incident Identified Datetime 2011-08-13 02:16:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2011-08-13 02:19:00
Restart Datetime 2011-10-22 10:02:00
On Site Datetime 2011-08-13 03:30:00
Nrc Rpt Datetime 2011-08-13 04:23:00
Nrc Rpt Num 985803 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name West Leg Loop Red Line
Segment Name Line Id 428
Onshore State Abbreviation Ia
Onshore Postal Code 51040
Onshore City Name Onawa
Onshore County Name Monona
Designated Location Survey Station No.
Designated Name 14293+63
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Other
Incident Area Details Exposed By Flood Water Scour
Crossing Yes
Water Crossing Ind Yes
Water Type Uncased
Water Name Missouri River Flood Plain
Water Depth 15
Water Subtype Shoreline/bank Crossing
Pipe Facility Type Interstate
Item Involved Weld, Including Heat-Affected Zone
Pipe Diameter 8
Pipe Wall Thickness 0.172
Pipe Smys 60000
Pipe Specification Api5l
Pipe Seam Type Erw - High Frequency
Pipe Manufacturer Ipsco Steel
Pipe Coating Type Cold Applied Tape
Weld Subtype Pipe Girth Weld
Installation Year 1993
Manufactured Year 1993
Material Involved Carbon Steel
Release Type Rupture
Rupture Orient Circumferential
Rupture Width 2.1
Rupture Length 4.9
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 675
Rel Water Name Missouririver
Could Be Hca Yes
Commodity Reached Hca Yes
Commercially Nav Ind Yes
Commercially Nav Yes No Yes
Other Pop Ind Yes
Other Pop Yes No Yes
Usa Drinking Ind Yes
Usa Drinking Yes No No
Est Cost Oper Paid 0
Est Cost Gas Released 80595
Est Cost Prop Damage 7368470
Est Cost Emergency 135000
Est Cost Environmental 85000
Est Cost Other 0
Prpty 7669065
Accident Psig 255
Mop Psig 1440
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 56045
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Control Room Ind Yes
Invest No Controller Ind Yes
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Natural Force Damage
Cause Details Heavy Rains/floods
Natural Force Type Heavy Rains/floods
Heavy Rains Subtype Washouts/scouring
Nf Extreme Weather Ind Yes
Nf Other Ind Yes
Nf Extreme Weather Details Prolonged Flooding Of The Missouri River
Preparer Name M****** S********
Preparer Title Sr. Pipeline Compliance Specialist
Preparer Email M*********@e****.com
Preparer Telephone 713-381-8209
Preparer Fax 713-381-6660
Prepared Date 2013-05-20 00:00:00
Authorizer Name M****** S********
Authorizer Telephone 713-381-8209
Authorizer Title Sr. Pipeline Compliance Specialist
Authorizer Email M*********@e****.com
Narrative The downstream pump closest to the failure automatically shutdown on under speed, and the operations controller detected a pressure drop at the same pump station. The controller shutdown upstream pump stations and closed upstream block valves, and after downstream pump stations pulled down the line pressure, the mov at the closest downstream pump station was closed to isolate the failed pipeline segment. The controller notified company personnel and county sheriff offices on both sides of the river. The controller then blocked in and bled down the pressure on the second company operated pipeline in the row. When field operations personnel arrived at the river between 3:00 and 4:00 am, product could not be seen or smelled on the west side, and product could not be seen but could be smelled in the vicinity of aerial marker 271 on the east side of the river. Both the failed line, and the line next to it operated by the operator remain shutdown under corrective action order, cf no. 3-2011-5009h. Divers located a break in the failed line on august 31, but the failure site is still underwater and inaccessible at the time of this report. The product released was natural gasoline, but no released product has been detected other than an odor on first arrival at the east side of the river. The initial volume reported was the line volume estimated between block valves. Most of the product trapped in isolated pipe has since been displaced from the line and was metered. The displaced volume was subtracted from the line fill volume, reducing the estimated unintended release volume. Product in the pipe near the west bank of the river is still not completely displaced. Supplement 6-1-12 the red was restarted on october 22, 2011. Installation of the red lines according to the approved repair plan was completed on january 16, 2012 with the completion of the main line valve motor operator work the amount of natural gasoline displaced from the red line on september 7, 2011 was metered and measured 2952.3 bbl. Approximately 507 gallons of additional natural gasoline was displaced september 28, 2011 and an additional 68 gallons of product was displaced from the red line on october 8, 2011. Pipe segments from both sides of the red line break have been removed from under water. Displacement of residual product with nitrogen was completed on april 11, 2012. The recovered amount of product from this displacement was 129 bbls. The total displacement of natural gasoline to date from the pipeline reduces the estimated release volume to 675 bbls. After the displacement the remaining sections of the affected pipe that could not be removed were either capped and abandoned or capped and placed in an idle state according to the submitted repair plan. Supplement/final 8-7-12 the metallurgical report was completed on july 2, 2012. There were no defects attributed to orginal construction/installation. The failure analysis indicated that the failure occurred because of the stresses associated with the flooding condition.

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