Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2011-08-10 — TX
Operator
Sfpp, Lp
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$1,000
Incident datetime
2011-08-10 03:36
Report number
Location
TX
Narrative
A hi-hi vapor alarm alerted operations to a potential problem at 0336. A technician was dispatched and arrived at 0424. Smelling gasoline, he did not turn on the lights due to the presence of gasoline vapors. At approximately 0517 the release amount was determined to exceed 5 gallons and external notifications were begun. The cause of the release was failure of the inboard pump seal. The technician and contractor support team replaced the seal later that day. Approximately 14.7 gallons (0.35 bbls) of gasoline was released into containment and transferred into transmix storage. Note: part a, #9 and 11 determined from dimensions of containment. Note: part c, #3, the pump was installed in 1956; unknown date of subsequent (if any) seal replacement.
Detailed record list
Report Received Date
2011-09-06 00:00:00
Iyear
2011
Report Number
20110325
Supplemental Number
18326
Report Type
Supplemental Final
Operator Id
18092
Name
Sfpp, Lp
Operator Street Address
500 Dallas Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2011-08-10 03:36:00
Location Latitude
39.120239
Location Longitude
-120.943522
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
0.35
Intentional Release Bbls
0
Recovered Bbls
0.35
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2011-08-10 03:36:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2011-08-10 03:39:00
Restart Datetime
2011-08-10 08:30:00
On Site Datetime
2011-08-10 04:24:00
Nrc Rpt Datetime
2011-08-10 05:46:00
Nrc Rpt Num
985452
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Colfax Station
Segment Name
Ls 12 (0.0 Mp)
Onshore State Abbreviation
Ca
Onshore Postal Code
95713
Onshore City Name
Colfax
Onshore County Name
Placer
Designated Location
Milepost/valve Station
Designated Name
Ls 12(0.0 Mp)
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Pump
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Other Pop Ind
Yes
Other Pop Yes No
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
46
Est Cost Prop Damage
1000
Est Cost Emergency
1000
Est Cost Environmental
0
Est Cost Other
0
Prpty
2046
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Pump Or Pump-Related Equipment
Eq Failure Type
Pump Or Pump-Related Equipment
Preparer Name
S**** M*******
Preparer Title
Mgr-Ccs
Preparer Email
S*************@k***********.com
Preparer Telephone
9098735146
Preparer Fax
3039843620
Prepared Date
2013-07-29 00:00:00
Authorizer Name
E* A* F***
Authorizer Telephone
7133699454
Authorizer Title
Director-Ccs
Authorizer Email
B********@k***********.com
Narrative
A hi-hi vapor alarm alerted operations to a potential problem at 0336. A technician was dispatched and arrived at 0424. Smelling gasoline, he did not turn on the lights due to the presence of gasoline vapors. At approximately 0517 the release amount was determined to exceed 5 gallons and external notifications were begun. The cause of the release was failure of the inboard pump seal. The technician and contractor support team replaced the seal later that day. Approximately 14.7 gallons (0.35 bbls) of gasoline was released into containment and transferred into transmix storage. Note: part a, #9 and 11 determined from dimensions of containment. Note: part c, #3, the pump was installed in 1956; unknown date of subsequent (if any) seal replacement.
| Report Received Date | 2011-09-06 00:00:00 |
|---|---|
| Iyear | 2011 |
| Report Number | 20110325 |
| Supplemental Number | 18326 |
| Report Type | Supplemental Final |
| Operator Id | 18092 PHMSA Enforcement |
| Name | Sfpp, Lp |
| Operator Street Address | 500 Dallas Street |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2011-08-10 03:36:00 |
| Location Latitude | 39.120239 Google Maps OpenStreetMap |
| Location Longitude | -120.943522 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Gasoline (Non-Ethanol) |
| Unintentional Release Bbls | 0.35 |
| Intentional Release Bbls | 0 |
| Recovered Bbls | 0.35 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2011-08-10 03:36:00 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2011-08-10 03:39:00 |
| Restart Datetime | 2011-08-10 08:30:00 |
| On Site Datetime | 2011-08-10 04:24:00 |
| Nrc Rpt Datetime | 2011-08-10 05:46:00 |
| Nrc Rpt Num | 985452 NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Colfax Station |
| Segment Name | Ls 12 (0.0 Mp) |
| Onshore State Abbreviation | Ca |
| Onshore Postal Code | 95713 |
| Onshore City Name | Colfax |
| Onshore County Name | Placer |
| Designated Location | Milepost/valve Station |
| Designated Name | Ls 12(0.0 Mp) |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Interstate |
| Item Involved | Pump |
| Release Type | Leak |
| Leak Type | Seal Or Packing |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| Other Pop Ind | Yes |
| Other Pop Yes No | Yes |
| Usa Drinking Ind | Yes |
| Usa Drinking Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 46 |
| Est Cost Prop Damage | 1000 |
| Est Cost Emergency | 1000 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 2046 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Pump Or Pump-Related Equipment |
| Eq Failure Type | Pump Or Pump-Related Equipment |
| Preparer Name | S**** M******* |
| Preparer Title | Mgr-Ccs |
| Preparer Email | S*************@k***********.com |
| Preparer Telephone | 9098735146 |
| Preparer Fax | 3039843620 |
| Prepared Date | 2013-07-29 00:00:00 |
| Authorizer Name | E* A* F*** |
| Authorizer Telephone | 7133699454 |
| Authorizer Title | Director-Ccs |
| Authorizer Email | B********@k***********.com |
| Narrative | A hi-hi vapor alarm alerted operations to a potential problem at 0336. A technician was dispatched and arrived at 0424. Smelling gasoline, he did not turn on the lights due to the presence of gasoline vapors. At approximately 0517 the release amount was determined to exceed 5 gallons and external notifications were begun. The cause of the release was failure of the inboard pump seal. The technician and contractor support team replaced the seal later that day. Approximately 14.7 gallons (0.35 bbls) of gasoline was released into containment and transferred into transmix storage. Note: part a, #9 and 11 determined from dimensions of containment. Note: part c, #3, the pump was installed in 1956; unknown date of subsequent (if any) seal replacement. |
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