HL incident on 2011-08-06 — TX

Operator
Mobil Pacific Pipeline Co
Cause
Corrosion Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$35,128
Incident datetime
2011-08-06 17:00
Report number
Location
TX
Narrative
Exxonmobil responded to a leak wheel notification from the operation control center. Exxonmobil had a pipeline in the release area. Exxonmobil notified california fire marshall and california oes once the leak was determined to be on the joughin gathering system line. A leak clamp was installed, and all crude was removed from the pipeline. The leaked pipe section is being prepared for removal upon receipt of necessary permits. A supplemental report will be completed once the cause of the leak is determined with any updated costs. 2-16-12 supplement report created to update cost in part d and add leak cause in part g. Leak cause was internal corrosion. Pipe section removed and new pipe section installed at leak location. Corrected part c-1 to intrastate 2/22/13- supplemental report created to update remediation cost on page 4 section 8g to $196,640 and to close this 7001 report for the 2011 release. A remediation final report has been submitted to l. A. County on remediation work, but empco has not received final closure from l. A. County. Another supplemental will be created for any additional work or cost associated with final remediation if needed.
Detailed record list
Report Received Date
2011-09-06 00:00:00
Iyear
2011
Report Number
20110324
Supplemental Number
17260
Report Type
Supplemental Final
Operator Id
Name
Mobil Pacific Pipeline Co
Operator Street Address
22777 Springwoods Village Parkway E3.5a.608
Operator City Name
Spring
Operator State Abbreviation
TX
Operator Postal Code
77389
Local Datetime
2011-08-06 16:50:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
35
Intentional Release Bbls
0
Recovered Bbls
35
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2011-08-06 17:00:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
On Site Datetime
2011-08-06 17:40:00
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Joughlin Gathering Line ( G131)- To Thumbs
Segment Name
Joughlin Csfm 204 ( G131)
Onshore State Abbreviation
Ca
Onshore Postal Code
90502
Onshore City Name
Torrance
Onshore County Name
Los Angeles
Designated Location
Survey Station No.
Designated Name
D4a-3024
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
48
Crossing
No
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
6.625
Pipe Wall Thickness
0.28
Pipe Smys
35000
Pipe Specification
Grade B
Pipe Seam Type
Erw � Unknown Frequency
Pipe Manufacturer
United States Steel-Southwest,houston,tx
Pipe Coating Type
Fusion Bonded Epoxy(Fbe)
Installation Year
1985
Manufactured Year
1985
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
Yes
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
1465
Est Cost Gas Released
3066
Est Cost Prop Damage
35128
Est Cost Emergency
65227
Est Cost Environmental
91754
Est Cost Other
0
Est Cost Other Details
Remediation Work Report Filed But Awaiting Final Report From L.a. County.
Prpty
196640
Accident Psig
220
Mop Psig
780
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
7476
Internal Inspection Ind
No
Diameter Change Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Gathering
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Surveillance does not include start and stops of pumps. Controller can monitor pressure and flows. Line operates on tank levels and there was no abnormal pressures alarm.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Localized Pitting
Int Microbiological Ind
Yes
Int Metallurgical Basis Ind
Yes
Int Low Point Pipe Loc Ind
Yes
Corrosion Inhibitors
No
Corrosion Lining
No
Cleaning Dewatering
Not Applicable - Not Mainline Pipe
Corrosion Coupons
No
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2009
Hydrtst Most Rcnt Pressure
985
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
L**** H********
Preparer Title
Pipeline Safety Advisor
Preparer Email
L****************@e*********.com
Preparer Telephone
903-654-5345
Preparer Fax
903-654-5302
Prepared Date
2013-02-22 00:00:00
Authorizer Name
M*** D* W******
Authorizer Telephone
713-656-0227
Authorizer Title
Manager-Safety Health And Environmental Dept
Authorizer Email
M*************@e*********.com
Narrative
Exxonmobil responded to a leak wheel notification from the operation control center. Exxonmobil had a pipeline in the release area. Exxonmobil notified california fire marshall and california oes once the leak was determined to be on the joughin gathering system line. A leak clamp was installed, and all crude was removed from the pipeline. The leaked pipe section is being prepared for removal upon receipt of necessary permits. A supplemental report will be completed once the cause of the leak is determined with any updated costs. 2-16-12 supplement report created to update cost in part d and add leak cause in part g. Leak cause was internal corrosion. Pipe section removed and new pipe section installed at leak location. Corrected part c-1 to intrastate 2/22/13- supplemental report created to update remediation cost on page 4 section 8g to $196,640 and to close this 7001 report for the 2011 release. A remediation final report has been submitted to l. A. County on remediation work, but empco has not received final closure from l. A. County. Another supplemental will be created for any additional work or cost associated with final remediation if needed.
Report Received Date 2011-09-06 00:00:00
Iyear 2011
Report Number 20110324
Supplemental Number 17260
Report Type Supplemental Final
Operator Id 30005 PHMSA Enforcement
Name Mobil Pacific Pipeline Co
Operator Street Address 22777 Springwoods Village Parkway E3.5a.608
Operator City Name Spring
Operator State Abbreviation TX
Operator Postal Code 77389
Local Datetime 2011-08-06 16:50:00
Location Latitude 33.81583 Google Maps OpenStreetMap
Location Longitude -118.29701 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 35
Intentional Release Bbls 0
Recovered Bbls 35
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2011-08-06 17:00:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
On Site Datetime 2011-08-06 17:40:00
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Joughlin Gathering Line ( G131)- To Thumbs
Segment Name Joughlin Csfm 204 ( G131)
Onshore State Abbreviation Ca
Onshore Postal Code 90502
Onshore City Name Torrance
Onshore County Name Los Angeles
Designated Location Survey Station No.
Designated Name D4a-3024
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover 48
Crossing No
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 6.625
Pipe Wall Thickness 0.28
Pipe Smys 35000
Pipe Specification Grade B
Pipe Seam Type Erw � Unknown Frequency
Pipe Manufacturer United States Steel-Southwest,houston,tx
Pipe Coating Type Fusion Bonded Epoxy(Fbe)
Installation Year 1985
Manufactured Year 1985
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment Yes
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 1465
Est Cost Gas Released 3066
Est Cost Prop Damage 35128
Est Cost Emergency 65227
Est Cost Environmental 91754
Est Cost Other 0
Est Cost Other Details Remediation Work Report Filed But Awaiting Final Report From L.a. County.
Prpty 196640
Accident Psig 220
Mop Psig 780
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 7476
Internal Inspection Ind No
Diameter Change Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Gathering
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Surveillance does not include start and stops of pumps. Controller can monitor pressure and flows. Line operates on tank levels and there was no abnormal pressures alarm.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Localized Pitting
Int Microbiological Ind Yes
Int Metallurgical Basis Ind Yes
Int Low Point Pipe Loc Ind Yes
Corrosion Inhibitors No
Corrosion Lining No
Cleaning Dewatering Not Applicable - Not Mainline Pipe
Corrosion Coupons No
Collected Data Ind No
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2009
Hydrtst Most Rcnt Pressure 985
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name L**** H********
Preparer Title Pipeline Safety Advisor
Preparer Email L****************@e*********.com
Preparer Telephone 903-654-5345
Preparer Fax 903-654-5302
Prepared Date 2013-02-22 00:00:00
Authorizer Name M*** D* W******
Authorizer Telephone 713-656-0227
Authorizer Title Manager-Safety Health And Environmental Dept
Authorizer Email M*************@e*********.com
Narrative Exxonmobil responded to a leak wheel notification from the operation control center. Exxonmobil had a pipeline in the release area. Exxonmobil notified california fire marshall and california oes once the leak was determined to be on the joughin gathering system line. A leak clamp was installed, and all crude was removed from the pipeline. The leaked pipe section is being prepared for removal upon receipt of necessary permits. A supplemental report will be completed once the cause of the leak is determined with any updated costs. 2-16-12 supplement report created to update cost in part d and add leak cause in part g. Leak cause was internal corrosion. Pipe section removed and new pipe section installed at leak location. Corrected part c-1 to intrastate 2/22/13- supplemental report created to update remediation cost on page 4 section 8g to $196,640 and to close this 7001 report for the 2011 release. A remediation final report has been submitted to l. A. County on remediation work, but empco has not received final closure from l. A. County. Another supplemental will be created for any additional work or cost associated with final remediation if needed.

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