Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2011-07-30 — TX
Operator
Enterprise Products Operating Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$1,000
Incident datetime
2011-07-30 17:35
Report number
Location
TX
Narrative
A company pipeline technician arriving at coffeyville station unit discovered a diesel release from a filter vessel. Upon discovery, the technician notified pipeline control of the release and verified that the line was down. The filter vessel was then isolated for repair. Then the filter was drained, the o-ring replaced, and the filter was placed back in service. Heavy rain storms and a loosely compacted pipe trench provided mechanisms for the released product to spread to more soil than initially anticipated.
Detailed record list
Report Received Date
2011-08-27 00:00:00
Iyear
2011
Report Number
20110315
Supplemental Number
17679
Report Type
Supplemental Final
Operator Id
31618
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2011-07-30 17:35:00
Location Latitude
37.05253
Location Longitude
-95.61166
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
27
Recovered Bbls
27
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2011-07-30 17:35:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Line Was Down Prior To Discovery Of The Leak
On Site Datetime
2011-07-30 17:35:00
Nrc Rpt Datetime
2011-08-02 11:53:00
Nrc Rpt Num
984652
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Coffeyville Station
Segment Name
Line 824
Onshore State Abbreviation
Ks
Onshore Postal Code
67337
Onshore City Name
Coffeyville
Onshore County Name
Montgomery
Designated Location
Survey Station No.
Designated Name
5635+10
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Other
Incident Area Details
Filter Pot O-Ring
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Filter Closure 0-Ring
Installation Year
2011
Material Involved
Material Other Than Carbon Steel
Material Details
Buna-N
Release Type
Leak
Leak Type
Seal Or Packing
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
4240
Est Cost Prop Damage
1000
Est Cost Emergency
50000
Est Cost Environmental
717919
Est Cost Other
0
Prpty
773159
Accident Psig
236
Mop Psig
720
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
O-Ring
Eq Additional Other Ind
Yes
Eq Additional Other Details
Unknown Failure Of O-Ring On A Filter At A Meter Site
Preparer Name
N*** T*****
Preparer Title
Pipeline Compliance Engineer
Preparer Email
N*******@e****.com
Preparer Telephone
713-381-2493
Preparer Fax
713-381-6660
Prepared Date
2013-03-26 00:00:00
Authorizer Name
N*** T*****
Authorizer Telephone
713-381-2493
Authorizer Title
Pipeline Compliance Engineer
Authorizer Email
N*******@e****.com
Narrative
A company pipeline technician arriving at coffeyville station unit discovered a diesel release from a filter vessel. Upon discovery, the technician notified pipeline control of the release and verified that the line was down. The filter vessel was then isolated for repair. Then the filter was drained, the o-ring replaced, and the filter was placed back in service. Heavy rain storms and a loosely compacted pipe trench provided mechanisms for the released product to spread to more soil than initially anticipated.
| Report Received Date | 2011-08-27 00:00:00 |
|---|---|
| Iyear | 2011 |
| Report Number | 20110315 |
| Supplemental Number | 17679 |
| Report Type | Supplemental Final |
| Operator Id | 31618 PHMSA Enforcement |
| Name | Enterprise Products Operating Llc |
| Operator Street Address | 1100 Louisiana Street |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2011-07-30 17:35:00 |
| Location Latitude | 37.05253 Google Maps OpenStreetMap |
| Location Longitude | -95.61166 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Diesel, Fuel Oil, Kerosene, Jet Fuel |
| Unintentional Release Bbls | 27 |
| Recovered Bbls | 27 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Operator Employee |
| Incident Identified Datetime | 2011-07-30 17:35:00 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Line Was Down Prior To Discovery Of The Leak |
| On Site Datetime | 2011-07-30 17:35:00 |
| Nrc Rpt Datetime | 2011-08-02 11:53:00 |
| Nrc Rpt Num | 984652 NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Coffeyville Station |
| Segment Name | Line 824 |
| Onshore State Abbreviation | Ks |
| Onshore Postal Code | 67337 |
| Onshore City Name | Coffeyville |
| Onshore County Name | Montgomery |
| Designated Location | Survey Station No. |
| Designated Name | 5635+10 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Incident Area Subtype | Other |
| Incident Area Details | Filter Pot O-Ring |
| Crossing | No |
| Pipe Facility Type | Interstate |
| Item Involved | Other |
| Item Involved Details | Filter Closure 0-Ring |
| Installation Year | 2011 |
| Material Involved | Material Other Than Carbon Steel |
| Material Details | Buna-N |
| Release Type | Leak |
| Leak Type | Seal Or Packing |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | Yes |
| Soil Remed Ind | Yes |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| Usa Drinking Ind | Yes |
| Usa Drinking Yes No | Yes |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 4240 |
| Est Cost Prop Damage | 1000 |
| Est Cost Emergency | 50000 |
| Est Cost Environmental | 717919 |
| Est Cost Other | 0 |
| Prpty | 773159 |
| Accident Psig | 236 |
| Mop Psig | 720 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Cpm In Place Ind | Yes |
| Cpm Operating Ind | Yes |
| Cpm Functional Ind | Yes |
| Cpm Detection Ind | No |
| Cpm Conf Ind | No |
| Investigation Status | Yes, specify investigation result(s): (select all that apply) |
| Invest Schedule Ind | Yes |
| Invest No Control Room Ind | Yes |
| Invest No Controller Ind | Yes |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Non-Threaded Connection Failure |
| Eq Failure Type | Non-Threaded Connection Failure |
| Other Non Threaded Ind | O-Ring |
| Eq Additional Other Ind | Yes |
| Eq Additional Other Details | Unknown Failure Of O-Ring On A Filter At A Meter Site |
| Preparer Name | N*** T***** |
| Preparer Title | Pipeline Compliance Engineer |
| Preparer Email | N*******@e****.com |
| Preparer Telephone | 713-381-2493 |
| Preparer Fax | 713-381-6660 |
| Prepared Date | 2013-03-26 00:00:00 |
| Authorizer Name | N*** T***** |
| Authorizer Telephone | 713-381-2493 |
| Authorizer Title | Pipeline Compliance Engineer |
| Authorizer Email | N*******@e****.com |
| Narrative | A company pipeline technician arriving at coffeyville station unit discovered a diesel release from a filter vessel. Upon discovery, the technician notified pipeline control of the release and verified that the line was down. The filter vessel was then isolated for repair. Then the filter was drained, the o-ring replaced, and the filter was placed back in service. Heavy rain storms and a loosely compacted pipe trench provided mechanisms for the released product to spread to more soil than initially anticipated. |
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