Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2011-07-22 — TX
Operator
Sunoco Pipeline L.p.
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$0
Incident datetime
2011-07-22 15:32
Report number
Location
TX
Narrative
Pump unit #2 was started against a closed discharge valve resulting in gasket failure on the pump. Re-submitted on 3/26/2013 to include part e5f per PHMSA request.
Detailed record list
Report Received Date
2011-08-19 00:00:00
Iyear
2011
Report Number
20110298
Supplemental Number
17691
Report Type
Supplemental Final
Operator Id
18718
Name
Sunoco Pipeline L.p.
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2011-07-22 15:32:00
Location Latitude
31.1611
Location Longitude
-94.6751
Commodity Released Type
Crude Oil
Unintentional Release Bbls
1.5
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2011-07-22 15:32:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2011-07-22 15:42:00
Restart Datetime
2011-08-04 14:00:00
On Site Datetime
2011-07-22 15:32:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Diboll Station
Segment Name
Millennium 12"
Onshore State Abbreviation
Tx
Onshore Postal Code
75941
Onshore City Name
Diboll
Onshore County Name
Angelina
Designated Location
Milepost/valve Station
Designated Name
99
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Pump
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
144
Est Cost Prop Damage
0
Est Cost Emergency
2394
Est Cost Environmental
1037
Est Cost Other
0
Prpty
3575
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Pipeline Or Equipment Overpressured
Operation Type
Pipeline Or Equipment Overpressured
Preparer Name
K****** D**** B***
Preparer Title
Area Dot Compliance Supervisor
Preparer Email
K*****@s**************.com
Preparer Telephone
281-637-6497
Preparer Fax
281-637-6425
Prepared Date
2013-03-26 00:00:00
Authorizer Name
K****** D**** B***
Authorizer Telephone
281-637-6497
Authorizer Title
Area Dot Compliance Supervisor
Authorizer Email
K*****@s**************.com
Narrative
Pump unit #2 was started against a closed discharge valve resulting in gasket failure on the pump. Re-submitted on 3/26/2013 to include part e5f per PHMSA request.
| Report Received Date | 2011-08-19 00:00:00 |
|---|---|
| Iyear | 2011 |
| Report Number | 20110298 |
| Supplemental Number | 17691 |
| Report Type | Supplemental Final |
| Operator Id | 18718 PHMSA Enforcement |
| Name | Sunoco Pipeline L.p. |
| Operator Street Address | 1300 Main Street |
| Operator City Name | Houston |
| Operator State Abbreviation | TX |
| Operator Postal Code | 77002 |
| Local Datetime | 2011-07-22 15:32:00 |
| Location Latitude | 31.1611 Google Maps OpenStreetMap |
| Location Longitude | -94.6751 Google Maps OpenStreetMap |
| Commodity Released Type | Crude Oil |
| Unintentional Release Bbls | 1.5 |
| Intentional Release Bbls | 0 |
| Recovered Bbls | 0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2011-07-22 15:32:00 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2011-07-22 15:42:00 |
| Restart Datetime | 2011-08-04 14:00:00 |
| On Site Datetime | 2011-07-22 15:32:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Diboll Station |
| Segment Name | Millennium 12" |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 75941 |
| Onshore City Name | Diboll |
| Onshore County Name | Angelina |
| Designated Location | Milepost/valve Station |
| Designated Name | 99 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Interstate |
| Item Involved | Pump |
| Release Type | Leak |
| Leak Type | Seal Or Packing |
| Water Contam Ind | No |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 144 |
| Est Cost Prop Damage | 0 |
| Est Cost Emergency | 2394 |
| Est Cost Environmental | 1037 |
| Est Cost Other | 0 |
| Prpty | 3575 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Incorrect Operation |
| Cause Details | Pipeline Or Equipment Overpressured |
| Operation Type | Pipeline Or Equipment Overpressured |
| Preparer Name | K****** D**** B*** |
| Preparer Title | Area Dot Compliance Supervisor |
| Preparer Email | K*****@s**************.com |
| Preparer Telephone | 281-637-6497 |
| Preparer Fax | 281-637-6425 |
| Prepared Date | 2013-03-26 00:00:00 |
| Authorizer Name | K****** D**** B*** |
| Authorizer Telephone | 281-637-6497 |
| Authorizer Title | Area Dot Compliance Supervisor |
| Authorizer Email | K*****@s**************.com |
| Narrative | Pump unit #2 was started against a closed discharge valve resulting in gasket failure on the pump. Re-submitted on 3/26/2013 to include part e5f per PHMSA request. |
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