Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2011-07-17 — OK
Operator
Oneok Ngl Pipeline Lp
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$820
Incident datetime
2011-07-17 01:06
Report number
Location
OK
Narrative
Oneok control center received gas detection alarm from the farmersville booster station indicating a possible leak and contacted field employee for investigation. Oneok field employee identified control valve leaking around stem packing. Employee isolated equipment and replaced valve stem packing.
Detailed record list
Report Received Date
2011-08-16 00:00:00
Iyear
2011
Report Number
20110293
Supplemental Number
17318
Report Type
Supplemental Final
Operator Id
32109
Name
Oneok Ngl Pipeline Lp
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2011-07-17 01:06:00
Location Latitude
33.179721
Location Longitude
-96.302081
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
2.6
Intentional Release Bbls
12
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2011-07-17 01:06:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2011-07-17 01:06:00
Restart Datetime
2011-07-17 19:17:00
On Site Datetime
2011-07-17 01:45:00
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
Sterling 2/farmersville Booster
Segment Name
Farmersville Booster Site 445
Onshore State Abbreviation
Tx
Onshore Postal Code
75442-0000
Onshore City Name
Farmersville
Onshore County Name
Collin
Designated Location
Milepost/valve Station
Designated Name
Farmersville
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Auxiliary Or Other Valve
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
448
Est Cost Prop Damage
820
Est Cost Emergency
100
Est Cost Environmental
0
Est Cost Other
0
Prpty
1368
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Preparer Name
P**** G**********
Preparer Email
P****************@o****.com
Preparer Telephone
580-395-6238
Preparer Fax
580-395-3111
Prepared Date
2013-03-04 00:00:00
Authorizer Name
N*** J****
Authorizer Telephone
580-395-6304
Authorizer Title
Dot Regulations Coordinator
Authorizer Email
N*********@o****.com
Narrative
Oneok control center received gas detection alarm from the farmersville booster station indicating a possible leak and contacted field employee for investigation. Oneok field employee identified control valve leaking around stem packing. Employee isolated equipment and replaced valve stem packing.
| Report Received Date | 2011-08-16 00:00:00 |
|---|---|
| Iyear | 2011 |
| Report Number | 20110293 |
| Supplemental Number | 17318 |
| Report Type | Supplemental Final |
| Operator Id | 32109 PHMSA Enforcement |
| Name | Oneok Ngl Pipeline Lp |
| Operator Street Address | 100 West Fifth Street |
| Operator City Name | Tulsa |
| Operator State Abbreviation | OK |
| Operator Postal Code | 74103 |
| Local Datetime | 2011-07-17 01:06:00 |
| Location Latitude | 33.179721 Google Maps OpenStreetMap |
| Location Longitude | -96.302081 Google Maps OpenStreetMap |
| Commodity Released Type | Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions |
| Commodity Subtype | Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid) |
| Unintentional Release Bbls | 2.6 |
| Intentional Release Bbls | 12 |
| Recovered Bbls | 0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2011-07-17 01:06:00 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2011-07-17 01:06:00 |
| Restart Datetime | 2011-07-17 19:17:00 |
| On Site Datetime | 2011-07-17 01:45:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Pipe Fac Name | Sterling 2/farmersville Booster |
| Segment Name | Farmersville Booster Site 445 |
| Onshore State Abbreviation | Tx |
| Onshore Postal Code | 75442-0000 |
| Onshore City Name | Farmersville |
| Onshore County Name | Collin |
| Designated Location | Milepost/valve Station |
| Designated Name | Farmersville |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Interstate |
| Item Involved | Valve |
| Valve Type | Auxiliary Or Other Valve |
| Release Type | Leak |
| Leak Type | Seal Or Packing |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 448 |
| Est Cost Prop Damage | 820 |
| Est Cost Emergency | 100 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 1368 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Non-Threaded Connection Failure |
| Eq Failure Type | Non-Threaded Connection Failure |
| Preparer Name | P**** G********** |
| Preparer Email | P****************@o****.com |
| Preparer Telephone | 580-395-6238 |
| Preparer Fax | 580-395-3111 |
| Prepared Date | 2013-03-04 00:00:00 |
| Authorizer Name | N*** J**** |
| Authorizer Telephone | 580-395-6304 |
| Authorizer Title | Dot Regulations Coordinator |
| Authorizer Email | N*********@o****.com |
| Narrative | Oneok control center received gas detection alarm from the farmersville booster station indicating a possible leak and contacted field employee for investigation. Oneok field employee identified control valve leaking around stem packing. Employee isolated equipment and replaced valve stem packing. |
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