GD incident on 2011-07-19 — NE

Operator
Superior Utilities, City Of
Cause
Equipment Failure
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 1 injury
Property damage (nominal)
$45,008
Incident datetime
2011-07-19 12:24
Report number
Location
NE, NUCKOLLS
Narrative
This is a condensed summary of the events. This narrative will truncate due to space considerations. For the full report, see the complete attachment submitted originally. On july 11, 2011 operations were began to abandon a segment of 6' piping, operating at 18 ounces of pressure, from within the system. An inflatable bag was inserted into the 6' main and inflated to stop gas flow to downstream piping. The downstream piping was purged of gas and gas flow was confirmed stopped at 10:25 am. A segment of piping was removed downstream of the stop point and preparation began to seal the end of pipe. At approximately 12:20 pm. There was a failure of the inflatable line stopper, a release of natural gas and instantaneous ignition of that natural gas. Upon ignition, the gas department employee safely exited the excavation as a second employee attempted to extinguish the fire. Emergency operations began and gas flow was stopped and 6' piping sealed by 3:00 pm. This release of natural gas and subsequent fire damaged excavator equipment and local utility facilities in the area. This fire necessitated the shutdown of part of the electrical power system.
Detailed record list
Occurred At
2011-07-19 12:24:00
Year
2011
Report Received Date
2011-08-11 00:00:00
Iyear
2011.0
Report Number
20110285.0
Supplemental Number
16001.0
Report Type
Supplemental
Operator Id
Name
Superior Utilities, City Of
Operator Street Address
135 W 4th Street - Po Box 160
Operator City Name
Superior
Operator State Abbreviation
NE
Operator Postal Code
68978
Local Datetime
2011-07-19 12:24:00
Location Street Address
320 E 2nd
Location City Name
Superior
Location County Name
Nuckolls
Location State Abbreviation
NE
Location Postal Code
68978
Location Latitude
Location Longitude
Nrc Rpt Datetime
2011-07-19 16:30:00
Commodity Released Type
Natural Gas
Unintentional Release
1024.0
Fatality Ind
No
Fatal
0
Injury Ind
Yes
Num Emp Injuries
0
Num Contr Injuries
0
Num Er Injuries
1
Num Worker Injuries
0
Num Gp Injuries
0
Injure
1
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
12.0
Incident Identified Datetime
2011-07-19 12:24:00
On Site Datetime
2011-07-19 12:24:00
Federal
No
Location Type
Utility Right-Of-Way / Easement
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
37.0
Crossing
No
Pipe Facility Type
Municipally Owned
System Part Involved
Main
Pipe Diameter
6.0
Pipe Specification
Unknown
Pipe Manufacturer
Unknown
Material Involved
Steel
Wt Steel
0.25
Release Type
Other
Release Type Details
Failure Of Line Stopper.
Class Location Type
Class 2 Location
Est Cost Oper Paid
150.0
Est Cost Prop Damage
45008.0
Est Cost Emergency
1174.0
Est Cost Other
0.0
Est Cost Unintentional Release
913.0
Prpty
47245.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
1.17
Normal Psig
1.17
Mop Psig
1.44
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind
Yes
Num Employees Tested
5
Num Employees Failed
0
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Other Control Relief Ind
Yes
Other Control Relief Details
Inflatable Line Stopper
Preparer Name
L**** S*****
Preparer Title
Gas Department Foreman
Preparer Email
L**********@y****.com
Preparer Telephone
402-879-4750
Preparer Fax
402-879-4752
Authorizer Name
L**** S*****
Authorizer Title
Gas Department Foreman
Authorizer Telephone
402-879-4750
Authorizer Email
L**********@y****.com
Narrative
This is a condensed summary of the events. This narrative will truncate due to space considerations. For the full report, see the complete attachment submitted originally. On july 11, 2011 operations were began to abandon a segment of 6' piping, operating at 18 ounces of pressure, from within the system. An inflatable bag was inserted into the 6' main and inflated to stop gas flow to downstream piping. The downstream piping was purged of gas and gas flow was confirmed stopped at 10:25 am. A segment of piping was removed downstream of the stop point and preparation began to seal the end of pipe. At approximately 12:20 pm. There was a failure of the inflatable line stopper, a release of natural gas and instantaneous ignition of that natural gas. Upon ignition, the gas department employee safely exited the excavation as a second employee attempted to extinguish the fire. Emergency operations began and gas flow was stopped and 6' piping sealed by 3:00 pm. This release of natural gas and subsequent fire damaged excavator equipment and local utility facilities in the area. This fire necessitated the shutdown of part of the electrical power system.
Occurred At 2011-07-19 12:24:00
Year 2011
Report Received Date 2011-08-11 00:00:00
Iyear 2011.0
Report Number 20110285.0
Supplemental Number 16001.0
Report Type Supplemental
Operator Id 18799 PHMSA Enforcement
Name Superior Utilities, City Of
Operator Street Address 135 W 4th Street - Po Box 160
Operator City Name Superior
Operator State Abbreviation NE
Operator Postal Code 68978
Local Datetime 2011-07-19 12:24:00
Location Street Address 320 E 2nd
Location City Name Superior
Location County Name Nuckolls
Location State Abbreviation NE
Location Postal Code 68978
Location Latitude 40.017804 Google Maps OpenStreetMap
Location Longitude -98.068415 Google Maps OpenStreetMap
Nrc Rpt Datetime 2011-07-19 16:30:00
Nrc Rpt Num 98390 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 1024.0
Fatality Ind No
Fatal 0
Injury Ind Yes
Num Emp Injuries 0
Num Contr Injuries 0
Num Er Injuries 1
Num Worker Injuries 0
Num Gp Injuries 0
Injure 1
Ignite Ind Yes
Explode Ind No
Num Pub Evacuated 12.0
Incident Identified Datetime 2011-07-19 12:24:00
On Site Datetime 2011-07-19 12:24:00
Federal No
Location Type Utility Right-Of-Way / Easement
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 37.0
Crossing No
Pipe Facility Type Municipally Owned
System Part Involved Main
Pipe Diameter 6.0
Pipe Specification Unknown
Pipe Manufacturer Unknown
Material Involved Steel
Wt Steel 0.25
Release Type Other
Release Type Details Failure Of Line Stopper.
Class Location Type Class 2 Location
Est Cost Oper Paid 150.0
Est Cost Prop Damage 45008.0
Est Cost Emergency 1174.0
Est Cost Other 0.0
Est Cost Unintentional Release 913.0
Prpty 47245.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 0.0
Accident Psig 1.17
Normal Psig 1.17
Mop Psig 1.44
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Investigation Status No, the facility was not monitored by a controller(s) at the time of the incident
Employee Drug Test Ind Yes
Num Employees Tested 5
Num Employees Failed 0
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Malfunction Of Control/relief Equipment
Eq Failure Type Malfunction Of Control/relief Equipment
Other Control Relief Ind Yes
Other Control Relief Details Inflatable Line Stopper
Preparer Name L**** S*****
Preparer Title Gas Department Foreman
Preparer Email L**********@y****.com
Preparer Telephone 402-879-4750
Preparer Fax 402-879-4752
Authorizer Name L**** S*****
Authorizer Title Gas Department Foreman
Authorizer Telephone 402-879-4750
Authorizer Email L**********@y****.com
Narrative This is a condensed summary of the events. This narrative will truncate due to space considerations. For the full report, see the complete attachment submitted originally. On july 11, 2011 operations were began to abandon a segment of 6' piping, operating at 18 ounces of pressure, from within the system. An inflatable bag was inserted into the 6' main and inflated to stop gas flow to downstream piping. The downstream piping was purged of gas and gas flow was confirmed stopped at 10:25 am. A segment of piping was removed downstream of the stop point and preparation began to seal the end of pipe. At approximately 12:20 pm. There was a failure of the inflatable line stopper, a release of natural gas and instantaneous ignition of that natural gas. Upon ignition, the gas department employee safely exited the excavation as a second employee attempted to extinguish the fire. Emergency operations began and gas flow was stopped and 6' piping sealed by 3:00 pm. This release of natural gas and subsequent fire damaged excavator equipment and local utility facilities in the area. This fire necessitated the shutdown of part of the electrical power system.

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