Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2011-07-17 — OK
Operator
Oneok Ngl Pipeline Lp
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$10
Incident datetime
2011-07-17 09:20
Report number
Location
OK
Narrative
3rd party notified oneok control center of a possible leak at edmond booster. Oneok employee responded edmond booster, found small leak in between the nut and the tubing. The tubing and fitting were replaced.
Detailed record list
Report Received Date
2011-08-05 00:00:00
Iyear
2011
Report Number
20110276
Supplemental Number
17317
Report Type
Supplemental Final
Operator Id
32109
Name
Oneok Ngl Pipeline Lp
Operator Street Address
100 West Fifth Street
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74103
Local Datetime
2011-07-17 09:20:00
Location Latitude
35.6376
Location Longitude
-97.70893
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
0.74
Intentional Release Bbls
0.1
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2011-07-17 09:20:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Was Able To Isolate Area Without Shutting Down Pipeline
On Site Datetime
2011-07-17 10:00:00
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
Oklahoma Gathering/edmond Booster
Segment Name
Edmond Booster Site 146
Onshore State Abbreviation
Ok
Onshore Postal Code
73078-0000
Onshore City Name
Piedmont
Onshore County Name
Canadian
Designated Location
Milepost/valve Station
Designated Name
Edmond Bst
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Intrastate
Item Involved
Tubing
Release Type
Leak
Leak Type
Pinhole
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
38
Est Cost Prop Damage
10
Est Cost Emergency
100
Est Cost Environmental
0
Est Cost Other
0
Prpty
148
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Preparer Name
P**** G**********
Preparer Email
P****************@o****.com
Preparer Telephone
580-395-6238
Preparer Fax
580-395-3111
Prepared Date
2013-03-04 00:00:00
Authorizer Name
N*** J****
Authorizer Telephone
580-395-6304
Authorizer Title
Dot Regulations Coordinator
Authorizer Email
N*********@o****.com
Narrative
3rd party notified oneok control center of a possible leak at edmond booster. Oneok employee responded edmond booster, found small leak in between the nut and the tubing. The tubing and fitting were replaced.
| Report Received Date | 2011-08-05 00:00:00 |
|---|---|
| Iyear | 2011 |
| Report Number | 20110276 |
| Supplemental Number | 17317 |
| Report Type | Supplemental Final |
| Operator Id | 32109 PHMSA Enforcement |
| Name | Oneok Ngl Pipeline Lp |
| Operator Street Address | 100 West Fifth Street |
| Operator City Name | Tulsa |
| Operator State Abbreviation | OK |
| Operator Postal Code | 74103 |
| Local Datetime | 2011-07-17 09:20:00 |
| Location Latitude | 35.6376 Google Maps OpenStreetMap |
| Location Longitude | -97.70893 Google Maps OpenStreetMap |
| Commodity Released Type | Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions |
| Commodity Subtype | Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid) |
| Unintentional Release Bbls | 0.74 |
| Intentional Release Bbls | 0.1 |
| Recovered Bbls | 0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2011-07-17 09:20:00 |
| System Part Involved | Onshore Pump/meter Station Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | No |
| Shutdown Explain | Was Able To Isolate Area Without Shutting Down Pipeline |
| On Site Datetime | 2011-07-17 10:00:00 |
| Ignite Ind | No |
| Explode Ind | No |
| Pipe Fac Name | Oklahoma Gathering/edmond Booster |
| Segment Name | Edmond Booster Site 146 |
| Onshore State Abbreviation | Ok |
| Onshore Postal Code | 73078-0000 |
| Onshore City Name | Piedmont |
| Onshore County Name | Canadian |
| Designated Location | Milepost/valve Station |
| Designated Name | Edmond Bst |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Intrastate |
| Item Involved | Tubing |
| Release Type | Leak |
| Leak Type | Pinhole |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 38 |
| Est Cost Prop Damage | 10 |
| Est Cost Emergency | 100 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 148 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Threaded Connection/coupling Failure |
| Eq Failure Type | Threaded Connection/coupling Failure |
| Preparer Name | P**** G********** |
| Preparer Email | P****************@o****.com |
| Preparer Telephone | 580-395-6238 |
| Preparer Fax | 580-395-3111 |
| Prepared Date | 2013-03-04 00:00:00 |
| Authorizer Name | N*** J**** |
| Authorizer Telephone | 580-395-6304 |
| Authorizer Title | Dot Regulations Coordinator |
| Authorizer Email | N*********@o****.com |
| Narrative | 3rd party notified oneok control center of a possible leak at edmond booster. Oneok employee responded edmond booster, found small leak in between the nut and the tubing. The tubing and fitting were replaced. |
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