GD incident on 2011-07-06 — MI

Operator
Consumers Energy Co
Cause
Miscellaneous Root Causes
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$4,375
Incident datetime
2011-07-06 13:44
Report number
Location
MI, OAKLAND
Narrative
Contractor asi paving while milling a parking lot cut through a 1-1/8" plastic medium pressure gas service to 135 crawford causing a fire and igniting contractor's equipment. The apartment complex was evacuated. There were no injuries. Oxford fire department responded to extinguish the fire and put it out at 14:41. Gas flow was squeezed off at 15:30. Once the damaged equipment was removed, the damaged service was repaired and the gas was back on at 00:30. Asi paving had requested staking, which was then accurately provided. However, the 1-1/8" plastic that was damaged was only 2 inches below the bottom of the 6-inch thick pavement being removed. This minimal depth did not allow asi to hand expose the service to determine depth prior to removing pavement (the damage occurred during the pavement removal operation). It is surmised that the 1-1/8" plastic service was buried at proper depth when installed in 1976, but subsequent parking area grading since the installation likely caused the service to be at a shallow depth.
Detailed record list
Occurred At
2011-07-06 13:44:00
Year
2011
Report Received Date
2011-08-05 00:00:00
Iyear
2011.0
Report Number
20110271.0
Supplemental Number
15559.0
Report Type
Supplemental Final
Operator Id
Name
Consumers Energy Co
Operator Street Address
One Energy Plaza
Operator City Name
Jackson
Operator State Abbreviation
MI
Operator Postal Code
49201
Local Datetime
2011-07-06 13:44:00
Location Street Address
135 Crawford Street
Location City Name
Oxford
Location County Name
Oakland
Location State Abbreviation
MI
Location Postal Code
48371
Location Latitude
Location Longitude
Nrc Rpt Datetime
2011-07-06 16:48:00
Nrc Rpt Num
Commodity Released Type
Natural Gas
Unintentional Release
40.67
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
Yes
Explode Ind
No
Num Pub Evacuated
24.0
Incident Identified Datetime
2011-07-06 13:44:00
On Site Datetime
2011-07-06 14:09:00
Federal
No
Location Type
Private Property
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
8.0
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Service
Installation Year
1976.0
Pipe Diameter
1.125
Pipe Specification
Astm D 2513
Pipe Manufacturer
Driscopipe
Material Involved
Plastic
Plastic Type
Polyethylene (Pe)
Plastic Sdr
11
Material Pe Pipe Code
3407
Release Type
Mechanical Puncture
Puncture Axial
1.0
Puncture Circum
1.0
Class Location Type
Class 3 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
4375.0
Est Cost Emergency
0.0
Est Cost Other
100000.0
Est Cost Other Details
Not Paid By Operator: Estimated Cost Of Damage To The Third Party's Equipment
Est Cost Unintentional Release
374.0
Prpty
104749.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
24.0
Accident Psig
41.7
Normal Psig
41.7
Mop Psig
60.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
No
Accident Identifier
Other
Accident Details
911 Operator
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Incident was caused by third party damage.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
Yes
One Call System Ind
Yes
Notify Cga Dirt
No
Private Row Ind
Yes
Private Subtype
Private Business
Excavator Type
Contractor
Excavator Equipment
Milling Equipment
Work Performed
Milling
One Call Notified Ind
Yes
One Call Ticket Num
11671065
Locator Type
Contract Locator
Visible Marks
Yes
Service Interruption
Yes
Service Interruption Hours
1.0
Root Cause Category
Miscellaneous Root Causes
Root Cause Type
Root Cause Not Listed (Comment Required)
Root Cause Type Other
Site Grading After 1976 Install Damaged During Pavement Removal
Preparer Name
A*** M* C*********
Preparer Title
Gas Regulatory Services Engineer
Preparer Email
A**************@c********.com
Preparer Telephone
989-791-5841
Preparer Fax
517-788-1369
Authorizer Name
T**** A* G****
Authorizer Title
Regulatory Compliance Manager
Authorizer Telephone
517-768-3187
Authorizer Email
T**********@c********.com
Narrative
Contractor asi paving while milling a parking lot cut through a 1-1/8" plastic medium pressure gas service to 135 crawford causing a fire and igniting contractor's equipment. The apartment complex was evacuated. There were no injuries. Oxford fire department responded to extinguish the fire and put it out at 14:41. Gas flow was squeezed off at 15:30. Once the damaged equipment was removed, the damaged service was repaired and the gas was back on at 00:30. Asi paving had requested staking, which was then accurately provided. However, the 1-1/8" plastic that was damaged was only 2 inches below the bottom of the 6-inch thick pavement being removed. This minimal depth did not allow asi to hand expose the service to determine depth prior to removing pavement (the damage occurred during the pavement removal operation). It is surmised that the 1-1/8" plastic service was buried at proper depth when installed in 1976, but subsequent parking area grading since the installation likely caused the service to be at a shallow depth.
Occurred At 2011-07-06 13:44:00
Year 2011
Report Received Date 2011-08-05 00:00:00
Iyear 2011.0
Report Number 20110271.0
Supplemental Number 15559.0
Report Type Supplemental Final
Operator Id 2748 PHMSA Enforcement
Name Consumers Energy Co
Operator Street Address One Energy Plaza
Operator City Name Jackson
Operator State Abbreviation MI
Operator Postal Code 49201
Local Datetime 2011-07-06 13:44:00
Location Street Address 135 Crawford Street
Location City Name Oxford
Location County Name Oakland
Location State Abbreviation MI
Location Postal Code 48371
Location Latitude 42.820279 Google Maps OpenStreetMap
Location Longitude -83.26156 Google Maps OpenStreetMap
Nrc Rpt Datetime 2011-07-06 16:48:00
Nrc Rpt Num 981870 NRC Report How to search
Commodity Released Type Natural Gas
Unintentional Release 40.67
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Ignite Ind Yes
Explode Ind No
Num Pub Evacuated 24.0
Incident Identified Datetime 2011-07-06 13:44:00
On Site Datetime 2011-07-06 14:09:00
Federal No
Location Type Private Property
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover 8.0
Crossing No
Pipe Facility Type Privately Owned
System Part Involved Service
Installation Year 1976.0
Pipe Diameter 1.125
Pipe Specification Astm D 2513
Pipe Manufacturer Driscopipe
Material Involved Plastic
Plastic Type Polyethylene (Pe)
Plastic Sdr 11
Material Pe Pipe Code 3407
Release Type Mechanical Puncture
Puncture Axial 1.0
Puncture Circum 1.0
Class Location Type Class 3 Location
Est Cost Oper Paid 0.0
Est Cost Prop Damage 4375.0
Est Cost Emergency 0.0
Est Cost Other 100000.0
Est Cost Other Details Not Paid By Operator: Estimated Cost Of Damage To The Third Party's Equipment
Est Cost Unintentional Release 374.0
Prpty 104749.0
Commercial Affected 0.0
Industrial Affected 0.0
Residences Affected 24.0
Accident Psig 41.7
Normal Psig 41.7
Mop Psig 60.0
Accident Pressure Pressure Did Not Exceed Maop
Scada In Place Ind No
Accident Identifier Other
Accident Details 911 Operator
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Incident was caused by third party damage.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Excavation Damage
Cause Details Excavation Damage By Third Party
Ex Party Type Excavation Damage By Third Party
Prior Notification Ind Yes
One Call System Ind Yes
Notify Cga Dirt No
Private Row Ind Yes
Private Subtype Private Business
Excavator Type Contractor
Excavator Equipment Milling Equipment
Work Performed Milling
One Call Notified Ind Yes
One Call Ticket Num 11671065
Locator Type Contract Locator
Visible Marks Yes
Service Interruption Yes
Service Interruption Hours 1.0
Root Cause Category Miscellaneous Root Causes
Root Cause Type Root Cause Not Listed (Comment Required)
Root Cause Type Other Site Grading After 1976 Install Damaged During Pavement Removal
Preparer Name A*** M* C*********
Preparer Title Gas Regulatory Services Engineer
Preparer Email A**************@c********.com
Preparer Telephone 989-791-5841
Preparer Fax 517-788-1369
Authorizer Name T**** A* G****
Authorizer Title Regulatory Compliance Manager
Authorizer Telephone 517-768-3187
Authorizer Email T**********@c********.com
Narrative Contractor asi paving while milling a parking lot cut through a 1-1/8" plastic medium pressure gas service to 135 crawford causing a fire and igniting contractor's equipment. The apartment complex was evacuated. There were no injuries. Oxford fire department responded to extinguish the fire and put it out at 14:41. Gas flow was squeezed off at 15:30. Once the damaged equipment was removed, the damaged service was repaired and the gas was back on at 00:30. Asi paving had requested staking, which was then accurately provided. However, the 1-1/8" plastic that was damaged was only 2 inches below the bottom of the 6-inch thick pavement being removed. This minimal depth did not allow asi to hand expose the service to determine depth prior to removing pavement (the damage occurred during the pavement removal operation). It is surmised that the 1-1/8" plastic service was buried at proper depth when installed in 1976, but subsequent parking area grading since the installation likely caused the service to be at a shallow depth.

All rights reserved. Copyright © by ClearPHMSA