HL incident on 2011-07-17 — TX

Operator
Chevron Pipe Line Co
Cause
Other Accident Cause
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$0
Incident datetime
2011-07-17 18:20
Report number
Location
TX
Narrative
At 1750 cdt on 17 jul 11 cpl personnel were notified by 3rd party personnel of a possible mechanical connection failure near the scrapper traps @ the venice multiple traps facility. 3rd party personnel indicated crude oil had entered the inland water adjacent to the traps; the volume released is 2 bbls.. Csc has stopped flowing from a portion of producers into the venice multiples. 3rd party personnel are deploying boom and sorbent material. Cpl ee's are en route. The cause is under investigation. Cpl installed a temporary launcher barrel on the venice multiple pipeline system in venice, la. The temporary launcher was installed on 7/14/11 and was pressure tested by means of a stand up test. The mechanical connection used on the temporary launcher and the scrapper was a yale type connection. The temporary launcher was 14 ft. Long and the section was supported by wooden timbers. At the time of the installation and pressure test, there was no evidence of any product leakage from the connection. Over the weekend there was heavy rain in the area and the alignment of the temporary launcher and the pipeline shifted and a release of product occured at the mechanical connection. The area was immediately contained with absorbent boom and the crude is being cleaned up with sorbent pads. As of 7/18/11, the mitigation of the area was at approximately 75% complete. The temporary launcher has been removed from the pipeline and the end closure has been reattached. The pipeline has been put back in normal operations and the end closure is being monitored. The clean up response will continue until the area is completely mitigated. As of 7/28/11 the site was remediated and there are no signs of any crude oil present on the water. Cpl has started and internal investigation of the release.
Detailed record list
Report Received Date
2011-08-04 00:00:00
Iyear
2011
Report Number
20110268
Supplemental Number
15960
Report Type
Original Final
Operator Id
Name
Chevron Pipe Line Co
Operator Street Address
1400 Smith Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2011-07-17 17:50:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
2
Intentional Release Bbls
0
Recovered Bbls
2
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2011-07-17 18:20:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2011-07-17 20:00:00
Restart Datetime
2011-07-18 11:00:00
On Site Datetime
2011-07-18 09:30:00
Nrc Rpt Datetime
2011-07-17 18:22:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Venice Multiples
Onshore State Abbreviation
La
Onshore Postal Code
70091
Onshore City Name
Venice, La
Onshore County Name
Plaquemines
Designated Location
Milepost/valve Station
Designated Name
0
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Scraper/pig Trap
Installation Year
2011
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
The Release Was Cause By A Shift In A Mechanical Connection Associated With A Temperary Launching Barrel And An Existing Scrapper Trap.
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
Yes
Surface Water Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Amount Released
2
Rel Water Name
Release Occured In A Small Pod Hole Of Water In A Marshy Area Near The Mississippi River
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
192
Est Cost Prop Damage
0
Est Cost Emergency
30000
Est Cost Environmental
0
Est Cost Other
0
Prpty
30192
Accident Psig
250
Mop Psig
400
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
14
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The release was cause by a shift in a mechanical connection associated with a temperary launching barrel and an existing scrapper trap.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Other Accident Cause
Cause Details
Miscellaneous
Other Type
Miscellaneous
Misc Details
The Mechanical Connection Used On The Temporary Launcher And The Scrapper Trap Was A Yale Screw Type Connection. The Temporary Launcher Was 14 Ft. Long And The Section Was Supported By Wooden Timbers. At The Time Of The Installation And Pressure Test, There Was No Evidence Of Any Leakage From The Connection. Over The Weekend There Was Heavy Rain In The Area And The Alignment Of The Temporary Launcher And The Pipeline Shifted And A Release Of Product Occured At The Mechanical Connection.
Preparer Name
P*** F******
Preparer Title
Dot Safety Specialist
Preparer Email
P***********@c******.com
Preparer Telephone
337-519-7709
Preparer Fax
337-572-3720
Prepared Date
2011-08-04 00:00:00
Authorizer Name
P*** F******
Authorizer Telephone
337-519-7709
Authorizer Title
Dot Safety Specialist
Authorizer Email
P***********@c******.com
Narrative
A***********************************************************************************************************************************************@ the venice multiple traps facility. 3rd party personnel indicated crude oil had entered the inland water adjacent to the traps; the volume released is 2 bbls.. Csc has stopped flowing from a portion of producers into the venice multiples. 3rd party personnel are deploying boom and sorbent material. Cpl ee's are en route. The cause is under investigation. Cpl installed a temporary launcher barrel on the venice multiple pipeline system in venice, la. The temporary launcher was installed on 7/14/11 and was pressure tested by means of a stand up test. The mechanical connection used on the temporary launcher and the scrapper was a yale type connection. The temporary launcher was 14 ft. Long and the section was supported by wooden timbers. At the time of the installation and pressure test, there was no evidence of any product leakage from the connection. Over the weekend there was heavy rain in the area and the alignment of the temporary launcher and the pipeline shifted and a release of product occured at the mechanical connection. The area was immediately contained with absorbent boom and the crude is being cleaned up with sorbent pads. As of 7/18/11, the mitigation of the area was at approximately 75% complete. The temporary launcher has been removed from the pipeline and the end closure has been reattached. The pipeline has been put back in normal operations and the end closure is being monitored. The clean up response will continue until the area is completely mitigated. As of 7/28/11 the site was remediated and there are no signs of any crude oil present on the water. **********************************************************.
Report Received Date 2011-08-04 00:00:00
Iyear 2011
Report Number 20110268
Supplemental Number 15960
Report Type Original Final
Operator Id 2731 PHMSA Enforcement
Name Chevron Pipe Line Co
Operator Street Address 1400 Smith Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2011-07-17 17:50:00
Location Latitude 29.238862 Google Maps OpenStreetMap
Location Longitude -89.384553 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 2
Intentional Release Bbls 0
Recovered Bbls 2
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Notification From Public
Incident Identified Datetime 2011-07-17 18:20:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2011-07-17 20:00:00
Restart Datetime 2011-07-18 11:00:00
On Site Datetime 2011-07-18 09:30:00
Nrc Rpt Datetime 2011-07-17 18:22:00
Nrc Rpt Num 982982 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Venice Multiples
Onshore State Abbreviation La
Onshore Postal Code 70091
Onshore City Name Venice, La
Onshore County Name Plaquemines
Designated Location Milepost/valve Station
Designated Name 0
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Scraper/pig Trap
Installation Year 2011
Material Involved Carbon Steel
Release Type Other
Release Type Details The Release Was Cause By A Shift In A Mechanical Connection Associated With A Temperary Launching Barrel And An Existing Scrapper Trap.
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind Yes
Surface Water Remed Ind Yes
Water Contam Ind Yes
Surface Contam Ind Yes
Amount Released 2
Rel Water Name Release Occured In A Small Pod Hole Of Water In A Marshy Area Near The Mississippi River
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 192
Est Cost Prop Damage 0
Est Cost Emergency 30000
Est Cost Environmental 0
Est Cost Other 0
Prpty 30192
Accident Psig 250
Mop Psig 400
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 14
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The release was cause by a shift in a mechanical connection associated with a temperary launching barrel and an existing scrapper trap.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Other Accident Cause
Cause Details Miscellaneous
Other Type Miscellaneous
Misc Details The Mechanical Connection Used On The Temporary Launcher And The Scrapper Trap Was A Yale Screw Type Connection. The Temporary Launcher Was 14 Ft. Long And The Section Was Supported By Wooden Timbers. At The Time Of The Installation And Pressure Test, There Was No Evidence Of Any Leakage From The Connection. Over The Weekend There Was Heavy Rain In The Area And The Alignment Of The Temporary Launcher And The Pipeline Shifted And A Release Of Product Occured At The Mechanical Connection.
Preparer Name P*** F******
Preparer Title Dot Safety Specialist
Preparer Email P***********@c******.com
Preparer Telephone 337-519-7709
Preparer Fax 337-572-3720
Prepared Date 2011-08-04 00:00:00
Authorizer Name P*** F******
Authorizer Telephone 337-519-7709
Authorizer Title Dot Safety Specialist
Authorizer Email P***********@c******.com
Narrative A***********************************************************************************************************************************************@ the venice multiple traps facility. 3rd party personnel indicated crude oil had entered the inland water adjacent to the traps; the volume released is 2 bbls.. Csc has stopped flowing from a portion of producers into the venice multiples. 3rd party personnel are deploying boom and sorbent material. Cpl ee's are en route. The cause is under investigation. Cpl installed a temporary launcher barrel on the venice multiple pipeline system in venice, la. The temporary launcher was installed on 7/14/11 and was pressure tested by means of a stand up test. The mechanical connection used on the temporary launcher and the scrapper was a yale type connection. The temporary launcher was 14 ft. Long and the section was supported by wooden timbers. At the time of the installation and pressure test, there was no evidence of any product leakage from the connection. Over the weekend there was heavy rain in the area and the alignment of the temporary launcher and the pipeline shifted and a release of product occured at the mechanical connection. The area was immediately contained with absorbent boom and the crude is being cleaned up with sorbent pads. As of 7/18/11, the mitigation of the area was at approximately 75% complete. The temporary launcher has been removed from the pipeline and the end closure has been reattached. The pipeline has been put back in normal operations and the end closure is being monitored. The clean up response will continue until the area is completely mitigated. As of 7/28/11 the site was remediated and there are no signs of any crude oil present on the water. **********************************************************.

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