GTG incident on 2011-07-08 — TX

Operator
Tennessee Gas Pipeline Co (El Paso)
Cause
Corrosion Failure
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$673,214
Incident datetime
2011-07-08 14:45
Report number
Location
TX
Narrative
Boemre observed bubbles and a light sheen in the vicinity of tennesee gas pipeline's (tgp) facilities on the ocs in eugene island block 320. Boemre contacted the coast guard who contacted tgp gas control. The leak was determined to be coming from tgp's 30" 523m-2300 pipeline which was isolated due to pending abandonment and under only 247 psig of gas pressure. Divers determined a pin hole leak to be the cause and repaired with a clamp. Abandonment of the line will proceed. Subsequent to the above july 8, 2011 occurrence, there was a leak from this tgp 523m-2300 pipeline that involved only liquids and resulted in a small sheen on february 3, 2012. There was no gas released. Consequently, pursuant to approval to do so from mr. Gene roberson, PHMSA sw region, this is being noted here and it was assigned nrc no. 1002085.
Detailed record list
Report Received Date
2011-07-29 00:00:00
Iyear
2011
Report Number
20110261
Supplemental Number
16143
Report Type
Supplemental Final
Operator Id
Name
Tennessee Gas Pipeline Co (El Paso)
Operator Street Address
1001 Louisiana St
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2011-07-08 11:42:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2011-07-08 15:05:00
Commodity Released Type
Natural Gas
Unintentional Release
1000
Intentional Release
27544
Accompanying Liquid
0.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
No
Shutdown Explain
Pipeline Was Shut In Due To Planned Abandonment.
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2011-07-08 14:45:00
On Site Datetime
2011-07-11 17:45:00
On Off Shore
Offshore
Off Water Depth
244
Off Accident Origin
On The Outer Continental Shelf (Ocs)
Off Ocs Area
Eugene Island
Off Ocs Block
320
Off Area Accident Type
Below Water, Pipe Buried Or Jetted Below Seabed
Pipe Facility Type
Interstate
System Part Involved
Offshore Pipeline, Including Riser And Riser Bend
Item Involved
Weld/fusion, Including Heat-Affected Zone
Pipe Diameter
30
Pipe Wall Thickness
0.562
Pipe Smys
60000
Pipe Specification
Api 5lx
Pipe Seam Type
Dsaw
Pipe Manufacturer
Bethlehem
Pipe Coating Type
Coal Tar
Weld Subtype
Pipe Girth Weld
Installation Year
1975
Manufactured Year
1974
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
757
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
4000
Est Cost Intentional Release
110178
Est Cost Prop Damage
673214
Est Cost Emergency
3850
Est Cost Other
0
Est Cost Other Details
None.
Prpty
791242
Accident Psig
247
Mop Psig
1250
Mop Cfr Section
Not On Omb-Approved Form When Submitted
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
168590
Internal Inspection Ind
No
Other Inspection Ind
Yes
Internal Inspection Details
No Platform Connected, No Launchers/receivers, And Pipe Is To Be Abandoned Due To Hurricane Ike.
Operation Complications Ind
Yes
Low Flow Ind
Yes
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Other
Accident Details
Boemre Patrol Observed And Contacted Coast Guard Who Contacted Tgp Gas Control.
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Pipeline was not flowing and pressure was well below maop.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
Internal Corrosion
Internal External
Internal Corrosion
Int Visual Exam Results
Not Cut Open
Int Other Corrosion Ind
Yes
Int Corrosion Type Details
Not Determined Due To Imminent Abandonment Of Pipeline, But Suspicion Is Microbiological.
Int Other Basis Ind
Yes
Int Corrosion Basis Details
Not Determined Due To Imminent Abandonment Of Pipeline, But Suspicion Is Microbiological.
Int Other Loc Ind
Yes
Corrosion Location Details
In Heat Affected Zone Of Girth Weld.
Corrosion Inhibitors
Yes
Corrosion Lining
Yes
Cleaning Dewatering
No
Corrosion Coupons
No
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
1975
Hydrtst Most Rcnt Pressure
1937
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
Z****** R*****
Preparer Title
Engineer - Pipeline
Preparer Email
Z*************@k**********.com
Preparer Telephone
7134206633
Preparer Fax
7134206633
Authorizer Name
Z****** R*****
Authorizer Title
Engineer - Pipeline
Authorizer Telephone
7134206633
Authorizer Email
Z*************@k***********.com
Narrative
Boemre observed bubbles and a light sheen in the vicinity of tennesee gas pipeline's (tgp) facilities on the ocs in eugene island block 320. Boemre contacted the coast guard who contacted tgp gas control. The leak was determined to be coming from tgp's 30" 523m-2300 pipeline which was isolated due to pending abandonment and under only 247 psig of gas pressure. Divers determined a pin hole leak to be the cause and repaired with a clamp. Abandonment of the line will proceed. Subsequent to the above july 8, 2011 occurrence, there was a leak from this tgp 523m-2300 pipeline that involved only liquids and resulted in a small sheen on february 3, 2012. There was no gas released. Consequently, pursuant to approval to do so from mr. Gene roberson, PHMSA sw region, this is being noted here and it was assigned nrc no. 1002085.
Report Received Date 2011-07-29 00:00:00
Iyear 2011
Report Number 20110261
Supplemental Number 16143
Report Type Supplemental Final
Operator Id 19160 PHMSA Enforcement
Name Tennessee Gas Pipeline Co (El Paso)
Operator Street Address 1001 Louisiana St
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2011-07-08 11:42:00
Location Latitude 28.280666 Google Maps OpenStreetMap
Location Longitude -91.429833 Google Maps OpenStreetMap
Nrc Rpt Num 982085 NRC Report How to search
Nrc Rpt Datetime 2011-07-08 15:05:00
Commodity Released Type Natural Gas
Unintentional Release 1000
Intentional Release 27544
Accompanying Liquid 0.5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind No
Shutdown Explain Pipeline Was Shut In Due To Planned Abandonment.
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2011-07-08 14:45:00
On Site Datetime 2011-07-11 17:45:00
On Off Shore Offshore
Off Water Depth 244
Off Accident Origin On The Outer Continental Shelf (Ocs)
Off Ocs Area Eugene Island
Off Ocs Block 320
Off Area Accident Type Below Water, Pipe Buried Or Jetted Below Seabed
Pipe Facility Type Interstate
System Part Involved Offshore Pipeline, Including Riser And Riser Bend
Item Involved Weld/fusion, Including Heat-Affected Zone
Pipe Diameter 30
Pipe Wall Thickness 0.562
Pipe Smys 60000
Pipe Specification Api 5lx
Pipe Seam Type Dsaw
Pipe Manufacturer Bethlehem
Pipe Coating Type Coal Tar
Weld Subtype Pipe Girth Weld
Installation Year 1975
Manufactured Year 1974
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 757
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 4000
Est Cost Intentional Release 110178
Est Cost Prop Damage 673214
Est Cost Emergency 3850
Est Cost Other 0
Est Cost Other Details None.
Prpty 791242
Accident Psig 247
Mop Psig 1250
Mop Cfr Section Not On Omb-Approved Form When Submitted View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 168590
Internal Inspection Ind No
Other Inspection Ind Yes
Internal Inspection Details No Platform Connected, No Launchers/receivers, And Pipe Is To Be Abandoned Due To Hurricane Ike.
Operation Complications Ind Yes
Low Flow Ind Yes
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Other
Accident Details Boemre Patrol Observed And Contacted Coast Guard Who Contacted Tgp Gas Control.
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Pipeline was not flowing and pressure was well below maop.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details Internal Corrosion
Internal External Internal Corrosion
Int Visual Exam Results Not Cut Open
Int Other Corrosion Ind Yes
Int Corrosion Type Details Not Determined Due To Imminent Abandonment Of Pipeline, But Suspicion Is Microbiological.
Int Other Basis Ind Yes
Int Corrosion Basis Details Not Determined Due To Imminent Abandonment Of Pipeline, But Suspicion Is Microbiological.
Int Other Loc Ind Yes
Corrosion Location Details In Heat Affected Zone Of Girth Weld.
Corrosion Inhibitors Yes
Corrosion Lining Yes
Cleaning Dewatering No
Corrosion Coupons No
Collected Data Ind No
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 1975
Hydrtst Most Rcnt Pressure 1937
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name Z****** R*****
Preparer Title Engineer - Pipeline
Preparer Email Z*************@k**********.com
Preparer Telephone 7134206633
Preparer Fax 7134206633
Authorizer Name Z****** R*****
Authorizer Title Engineer - Pipeline
Authorizer Telephone 7134206633
Authorizer Email Z*************@k***********.com
Narrative Boemre observed bubbles and a light sheen in the vicinity of tennesee gas pipeline's (tgp) facilities on the ocs in eugene island block 320. Boemre contacted the coast guard who contacted tgp gas control. The leak was determined to be coming from tgp's 30" 523m-2300 pipeline which was isolated due to pending abandonment and under only 247 psig of gas pressure. Divers determined a pin hole leak to be the cause and repaired with a clamp. Abandonment of the line will proceed. Subsequent to the above july 8, 2011 occurrence, there was a leak from this tgp 523m-2300 pipeline that involved only liquids and resulted in a small sheen on february 3, 2012. There was no gas released. Consequently, pursuant to approval to do so from mr. Gene roberson, PHMSA sw region, this is being noted here and it was assigned nrc no. 1002085.

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