Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2011-06-21 — IL
Operator
Bp West Coast Products L.l.c.
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$0
Incident datetime
2011-06-21 12:30
Report number
Location
IL
Narrative
On june 21, 2011, at approximately 12:30pm bp marine terminal 2, csfm id#0092 / line 69 experienced an approximate 4bbl release of jet fuel due to gasket failure on above ground pipeline. The product was contained within the secondary containment area. The line was shutdown and isolated. The long beach fire dept; ca oes arrived on scene. Lbfd sprayed foam over the spill area. Spill response contractor arrived promptly and was dispatched to clean up residual product and a repair plan was developed. Se winds at 5mph, temp 80f w/ 30%humidity & barometric pressure of 29.92 inches. All product was recovered or washed to enclosed facility sump. A garlock blue-guard 3000 cut ring gasket was in service at flange 0028, at time of failure. Gasket ring material separated in service and loss of product incident occurred at facility.
Detailed record list
Report Received Date
2011-07-18 00:00:00
Iyear
2011
Report Number
20110248
Supplemental Number
18930
Report Type
Supplemental Final
Operator Id
31610
Name
Bp West Coast Products L.l.c.
Operator Street Address
150 West Warrenville Road
Operator City Name
Naperville
Operator State Abbreviation
IL
Operator Postal Code
60563
Local Datetime
2011-06-21 12:30:00
Location Latitude
33.4604
Location Longitude
-118.12035
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Diesel, Fuel Oil, Kerosene, Jet Fuel
Unintentional Release Bbls
4
Intentional Release Bbls
0
Recovered Bbls
3.8
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2011-06-21 12:30:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
On Site Datetime
2011-06-21 12:30:00
Nrc Rpt Datetime
2011-06-21 13:15:00
Nrc Rpt Num
980327
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Line 69
Segment Name
Csfm 0092
Onshore State Abbreviation
Ca
Onshore Postal Code
90813
Onshore City Name
Long Beach
Onshore County Name
Los Angeles
Designated Location
Milepost/valve Station
Designated Name
Marine Term 2
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Pipe Facility Type
Intrastate
Item Involved
Flange Assembly
Release Type
Leak
Leak Type
Other
Leak Type Other
Gasket
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
400
Est Cost Prop Damage
0
Est Cost Emergency
45000
Est Cost Environmental
0
Est Cost Other
0
Prpty
45400
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Preparer Name
C***** R********
Preparer Title
Hse Coordinator
Preparer Email
C***************@b*.com
Preparer Telephone
562 728 2782
Preparer Fax
714 670 5037
Prepared Date
2014-01-16 00:00:00
Authorizer Name
M****** S******
Authorizer Telephone
630 536-3495
Authorizer Title
Dot Team Lead
Authorizer Email
M**************@b*.com
Narrative
On june 21, 2011, at approximately 12:30pm bp marine terminal 2, csfm id#0092 / line 69 experienced an approximate 4bbl release of jet fuel due to gasket failure on above ground pipeline. The product was contained within the secondary containment area. The line was shutdown and isolated. The long beach fire dept; ca oes arrived on scene. Lbfd sprayed foam over the spill area. Spill response contractor arrived promptly and was dispatched to clean up residual product and a repair plan was developed. Se winds at 5mph, temp 80f w/ 30%humidity & barometric pressure of 29.92 inches. All product was recovered or washed to enclosed facility sump. A garlock blue-guard 3000 cut ring gasket was in service at flange 0028, at time of failure. Gasket ring material separated in service and loss of product incident occurred at facility.
| Report Received Date | 2011-07-18 00:00:00 |
|---|---|
| Iyear | 2011 |
| Report Number | 20110248 |
| Supplemental Number | 18930 |
| Report Type | Supplemental Final |
| Operator Id | 31610 PHMSA Enforcement |
| Name | Bp West Coast Products L.l.c. |
| Operator Street Address | 150 West Warrenville Road |
| Operator City Name | Naperville |
| Operator State Abbreviation | IL |
| Operator Postal Code | 60563 |
| Local Datetime | 2011-06-21 12:30:00 |
| Location Latitude | 33.4604 Google Maps OpenStreetMap |
| Location Longitude | -118.12035 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Diesel, Fuel Oil, Kerosene, Jet Fuel |
| Unintentional Release Bbls | 4 |
| Intentional Release Bbls | 0 |
| Recovered Bbls | 3.8 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2011-06-21 12:30:00 |
| System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
| On Off Shore | Onshore |
| On Site Datetime | 2011-06-21 12:30:00 |
| Nrc Rpt Datetime | 2011-06-21 13:15:00 |
| Nrc Rpt Num | 980327 NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Line 69 |
| Segment Name | Csfm 0092 |
| Onshore State Abbreviation | Ca |
| Onshore Postal Code | 90813 |
| Onshore City Name | Long Beach |
| Onshore County Name | Los Angeles |
| Designated Location | Milepost/valve Station |
| Designated Name | Marine Term 2 |
| Federal | No |
| Location Type | Totally Contained On Operator-Controlled Property |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Intrastate |
| Item Involved | Flange Assembly |
| Release Type | Leak |
| Leak Type | Other |
| Leak Type Other | Gasket |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 400 |
| Est Cost Prop Damage | 0 |
| Est Cost Emergency | 45000 |
| Est Cost Environmental | 0 |
| Est Cost Other | 0 |
| Prpty | 45400 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Non-Threaded Connection Failure |
| Eq Failure Type | Non-Threaded Connection Failure |
| Preparer Name | C***** R******** |
| Preparer Title | Hse Coordinator |
| Preparer Email | C***************@b*.com |
| Preparer Telephone | 562 728 2782 |
| Preparer Fax | 714 670 5037 |
| Prepared Date | 2014-01-16 00:00:00 |
| Authorizer Name | M****** S****** |
| Authorizer Telephone | 630 536-3495 |
| Authorizer Title | Dot Team Lead |
| Authorizer Email | M**************@b*.com |
| Narrative | On june 21, 2011, at approximately 12:30pm bp marine terminal 2, csfm id#0092 / line 69 experienced an approximate 4bbl release of jet fuel due to gasket failure on above ground pipeline. The product was contained within the secondary containment area. The line was shutdown and isolated. The long beach fire dept; ca oes arrived on scene. Lbfd sprayed foam over the spill area. Spill response contractor arrived promptly and was dispatched to clean up residual product and a repair plan was developed. Se winds at 5mph, temp 80f w/ 30%humidity & barometric pressure of 29.92 inches. All product was recovered or washed to enclosed facility sump. A garlock blue-guard 3000 cut ring gasket was in service at flange 0028, at time of failure. Gasket ring material separated in service and loss of product incident occurred at facility. |
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