Incident details
Operator, cause, commodity and consequences with raw source fields.
GD incident on 2011-06-06 — WA
Operator
Puget Sound Energy
Cause
Excavation Issue
Commodity
Natural Gas
Program
GD
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$44,601
Incident datetime
2011-06-06 16:15
Report number
Location
WA, KING
Narrative
See attached
Detailed record list
Occurred At
2011-06-06 16:15:00
Year
2011
Report Received Date
2011-07-03 00:00:00
Iyear
2011.0
Report Number
20110224.0
Supplemental Number
15537.0
Report Type
Supplemental Final
Operator Id
22189
Name
Puget Sound Energy
Operator Street Address
355 110th Ave Ne
Operator City Name
Bellevue
Operator State Abbreviation
WA
Operator Postal Code
98004
Local Datetime
2011-06-04 21:00:00
Location Street Address
3605 E Marginal Way S
Location City Name
Seattle
Location County Name
King
Location State Abbreviation
WA
Location Postal Code
98134
Location Latitude
47.57274
Location Longitude
-122.339778
Nrc Rpt Datetime
2011-06-06 17:12:00
Nrc Rpt Num
978852
Commodity Released Type
Natural Gas
Unintentional Release
0.0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0.0
Incident Identified Datetime
2011-06-06 16:15:00
On Site Datetime
2011-06-06 16:15:00
Federal
No
Location Type
Public Property
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
40.0
Crossing
No
Pipe Facility Type
Privately Owned
System Part Involved
Main
Installation Year
1960.0
Pipe Diameter
16.0
Pipe Specification
Api 5l X-42
Pipe Manufacturer
Unknown
Material Involved
Steel
Steel Seam Type
Other
Steel Seam Type Details
Unknown
Wt Steel
0.25
Release Type
Other
Release Type Details
No Release Of Gas
Class Location Type
Class 4 Location
Est Cost Oper Paid
0.0
Est Cost Prop Damage
44601.0
Est Cost Emergency
23503.0
Est Cost Other
35029.0
Est Cost Other Details
Additional Operator Labor, Material And Rented Equipment
Est Cost Unintentional Release
0.0
Prpty
103133.0
Commercial Affected
0.0
Industrial Affected
0.0
Residences Affected
0.0
Accident Psig
143.0
Normal Psig
143.0
Mop Psig
150.0
Accident Pressure
Pressure Did Not Exceed Maop
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The incident is a result of a third-party damage
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Excavation Damage
Cause Details
Excavation Damage By Third Party
Ex Party Type
Excavation Damage By Third Party
Prior Notification Ind
No
Notify Cga Dirt
No
Public Row Ind
Yes
Public Subtype
City Street
Excavator Type
Contractor
Excavator Equipment
Backhoe/trackhoe
Work Performed
Pole
One Call Notified Ind
Yes
One Call Ticket Num
11106851
One Call Center Name
Utilities Underground Location Center
Locator Type
Contract Locator
Visible Marks
Yes
Root Cause Category
Excavation Issue
Root Cause Type
Excavator Failed To Maintain Clearance After Verifying Marks
Preparer Name
A********* I***
Preparer Title
Consulting Engineer
Preparer Email
A**************@p**.com
Preparer Telephone
425 456 2970
Preparer Fax
425 462 3770
Authorizer Name
C***** M******
Authorizer Title
Manager
Authorizer Telephone
4254623207
Authorizer Email
C*************@p**.com
Narrative
See attached
| Occurred At | 2011-06-06 16:15:00 |
|---|---|
| Year | 2011 |
| Report Received Date | 2011-07-03 00:00:00 |
| Iyear | 2011.0 |
| Report Number | 20110224.0 |
| Supplemental Number | 15537.0 |
| Report Type | Supplemental Final |
| Operator Id | 22189 PHMSA Enforcement |
| Name | Puget Sound Energy |
| Operator Street Address | 355 110th Ave Ne |
| Operator City Name | Bellevue |
| Operator State Abbreviation | WA |
| Operator Postal Code | 98004 |
| Local Datetime | 2011-06-04 21:00:00 |
| Location Street Address | 3605 E Marginal Way S |
| Location City Name | Seattle |
| Location County Name | King |
| Location State Abbreviation | WA |
| Location Postal Code | 98134 |
| Location Latitude | 47.57274 Google Maps OpenStreetMap |
| Location Longitude | -122.339778 Google Maps OpenStreetMap |
| Nrc Rpt Datetime | 2011-06-06 17:12:00 |
| Nrc Rpt Num | 978852 NRC Report How to search |
| Commodity Released Type | Natural Gas |
| Unintentional Release | 0.0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0.0 |
| Incident Identified Datetime | 2011-06-06 16:15:00 |
| On Site Datetime | 2011-06-06 16:15:00 |
| Federal | No |
| Location Type | Public Property |
| Incident Area Type | Underground |
| Incident Area Subtype | Exposed Due To Excavation |
| Depth Of Cover | 40.0 |
| Crossing | No |
| Pipe Facility Type | Privately Owned |
| System Part Involved | Main |
| Installation Year | 1960.0 |
| Pipe Diameter | 16.0 |
| Pipe Specification | Api 5l X-42 |
| Pipe Manufacturer | Unknown |
| Material Involved | Steel |
| Steel Seam Type | Other |
| Steel Seam Type Details | Unknown |
| Wt Steel | 0.25 |
| Release Type | Other |
| Release Type Details | No Release Of Gas |
| Class Location Type | Class 4 Location |
| Est Cost Oper Paid | 0.0 |
| Est Cost Prop Damage | 44601.0 |
| Est Cost Emergency | 23503.0 |
| Est Cost Other | 35029.0 |
| Est Cost Other Details | Additional Operator Labor, Material And Rented Equipment |
| Est Cost Unintentional Release | 0.0 |
| Prpty | 103133.0 |
| Commercial Affected | 0.0 |
| Industrial Affected | 0.0 |
| Residences Affected | 0.0 |
| Accident Psig | 143.0 |
| Normal Psig | 143.0 |
| Mop Psig | 150.0 |
| Accident Pressure | Pressure Did Not Exceed Maop |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Accident Identifier | Local Operating Personnel, Including Contractors |
| Operator Type | Contractor Working For The Operator |
| Investigation Status | No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate) |
| Investigation Status Details | The incident is a result of a third-party damage |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Excavation Damage |
| Cause Details | Excavation Damage By Third Party |
| Ex Party Type | Excavation Damage By Third Party |
| Prior Notification Ind | No |
| Notify Cga Dirt | No |
| Public Row Ind | Yes |
| Public Subtype | City Street |
| Excavator Type | Contractor |
| Excavator Equipment | Backhoe/trackhoe |
| Work Performed | Pole |
| One Call Notified Ind | Yes |
| One Call Ticket Num | 11106851 |
| One Call Center Name | Utilities Underground Location Center |
| Locator Type | Contract Locator |
| Visible Marks | Yes |
| Root Cause Category | Excavation Issue |
| Root Cause Type | Excavator Failed To Maintain Clearance After Verifying Marks |
| Preparer Name | A********* I*** |
| Preparer Title | Consulting Engineer |
| Preparer Email | A**************@p**.com |
| Preparer Telephone | 425 456 2970 |
| Preparer Fax | 425 462 3770 |
| Authorizer Name | C***** M****** |
| Authorizer Title | Manager |
| Authorizer Telephone | 4254623207 |
| Authorizer Email | C*************@p**.com |
| Narrative | See attached |
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