Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2011-06-04 — OK
Operator
Magellan Ammonia Pipeline, L.p.
Cause
Equipment Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$0
Incident datetime
2011-06-04 22:05
Report number
Location
OK
Narrative
Magellan operations control received a report form a third party of an ammonia smell and promptly executed its code red shut-down of the line and called out personel to investigate. Investigation revealed a small drip from the packing fitting on a mainline block valve. The fitting was repaired, stopping the release.
Detailed record list
Report Received Date
2011-06-28 00:00:00
Iyear
2011
Report Number
20110209
Supplemental Number
17057
Report Type
Supplemental
Operator Id
12105
Name
Magellan Ammonia Pipeline, L.p.
Operator Street Address
One Williams Center, Otc-9 P.o. Box 22186
Operator City Name
Tulsa
Operator State Abbreviation
OK
Operator Postal Code
74172
Local Datetime
2011-06-04 22:05:00
Location Latitude
38.08131
Location Longitude
-97.85245
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Anhydrous Ammonia
Unintentional Release Bbls
0.36
Intentional Release Bbls
0
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Incident Identified Datetime
2011-06-04 22:05:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
On Site Datetime
2011-06-05 00:15:00
Nrc Rpt Datetime
2011-06-04 00:00:00
Nrc Rpt Num
978677
Ignite Ind
No
Explode Ind
No
Pipe Fac Name
Verdigris To Partridge Lateral
Segment Name
Enid To Harper Line Segment
Onshore State Abbreviation
Ks
Onshore Postal Code
67018
Onshore City Name
Bluff City
Onshore County Name
Harper
Designated Location
Milepost/valve Station
Designated Name
68.5
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Aboveground
Pipe Facility Type
Interstate
Item Involved
Valve
Valve Type
Mainline
Release Type
Leak
Leak Type
Seal Or Packing
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
Usa Drinking Ind
Yes
Usa Drinking Yes No
No
Est Cost Oper Paid
0
Est Cost Gas Released
30
Est Cost Prop Damage
0
Est Cost Emergency
0
Est Cost Environmental
25000
Est Cost Other
0
Prpty
25030
Pipeline Function
> 20% Smys Regulated Transmission
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Malfunction Of Control/relief Equipment
Eq Failure Type
Malfunction Of Control/relief Equipment
Preparer Name
K****** L* L*******
Preparer Title
Sr. Compliance Coordinator
Preparer Email
K***********@m*********.com
Preparer Telephone
918-574-7315
Preparer Fax
918-574-7246
Prepared Date
2012-11-30 00:00:00
Authorizer Name
K****** L* L*******
Authorizer Telephone
918-574-7315
Authorizer Title
Sr. Compliance Coordinator
Authorizer Email
K***********@m*********.com
Narrative
Magellan operations control received a report form a third party of an ammonia smell and promptly executed its code red shut-down of the line and called out personel to investigate. Investigation revealed a small drip from the packing fitting on a mainline block valve. The fitting was repaired, stopping the release.
| Report Received Date | 2011-06-28 00:00:00 |
|---|---|
| Iyear | 2011 |
| Report Number | 20110209 |
| Supplemental Number | 17057 |
| Report Type | Supplemental |
| Operator Id | 12105 PHMSA Enforcement |
| Name | Magellan Ammonia Pipeline, L.p. |
| Operator Street Address | One Williams Center, Otc-9 P.o. Box 22186 |
| Operator City Name | Tulsa |
| Operator State Abbreviation | OK |
| Operator Postal Code | 74172 |
| Local Datetime | 2011-06-04 22:05:00 |
| Location Latitude | 38.08131 Google Maps OpenStreetMap |
| Location Longitude | -97.85245 Google Maps OpenStreetMap |
| Commodity Released Type | Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions |
| Commodity Subtype | Anhydrous Ammonia |
| Unintentional Release Bbls | 0.36 |
| Intentional Release Bbls | 0 |
| Recovered Bbls | 0 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Incident Identified Datetime | 2011-06-04 22:05:00 |
| System Part Involved | Onshore Pipeline, Including Valve Sites |
| On Off Shore | Onshore |
| On Site Datetime | 2011-06-05 00:15:00 |
| Nrc Rpt Datetime | 2011-06-04 00:00:00 |
| Nrc Rpt Num | 978677 NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Pipe Fac Name | Verdigris To Partridge Lateral |
| Segment Name | Enid To Harper Line Segment |
| Onshore State Abbreviation | Ks |
| Onshore Postal Code | 67018 |
| Onshore City Name | Bluff City |
| Onshore County Name | Harper |
| Designated Location | Milepost/valve Station |
| Designated Name | 68.5 |
| Federal | No |
| Location Type | Pipeline Right-Of-Way |
| Incident Area Type | Aboveground |
| Pipe Facility Type | Interstate |
| Item Involved | Valve |
| Valve Type | Mainline |
| Release Type | Leak |
| Leak Type | Seal Or Packing |
| Water Contam Ind | No |
| Could Be Hca | Yes |
| Commodity Reached Hca | Yes |
| Usa Drinking Ind | Yes |
| Usa Drinking Yes No | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 30 |
| Est Cost Prop Damage | 0 |
| Est Cost Emergency | 0 |
| Est Cost Environmental | 25000 |
| Est Cost Other | 0 |
| Prpty | 25030 |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Malfunction Of Control/relief Equipment |
| Eq Failure Type | Malfunction Of Control/relief Equipment |
| Preparer Name | K****** L* L******* |
| Preparer Title | Sr. Compliance Coordinator |
| Preparer Email | K***********@m*********.com |
| Preparer Telephone | 918-574-7315 |
| Preparer Fax | 918-574-7246 |
| Prepared Date | 2012-11-30 00:00:00 |
| Authorizer Name | K****** L* L******* |
| Authorizer Telephone | 918-574-7315 |
| Authorizer Title | Sr. Compliance Coordinator |
| Authorizer Email | K***********@m*********.com |
| Narrative | Magellan operations control received a report form a third party of an ammonia smell and promptly executed its code red shut-down of the line and called out personel to investigate. Investigation revealed a small drip from the packing fitting on a mainline block valve. The fitting was repaired, stopping the release. |
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