HL incident on 2011-05-29 — TX

Operator
Tc Oil Pipeline Operations Inc
Cause
Equipment Failure
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$25,000
Incident datetime
2011-05-29 02:00
Report number
Location
TX
Narrative
Pressure transmitter pt 201 at the severance pump station experienced a failure of the threaded 3/4 inch fitting. The failure of the 3/4" fitting failure occurred as a result of excessive vibration. The pump station was shutdown by oil control and isolated when pressure transmitter pt 201 began reading 4000 kpa less than station discharge pressure transmitter pt 203.The failed fitting resulted in the release of oil.
Detailed record list
Report Received Date
2011-06-28 00:00:00
Iyear
2011
Report Number
20110208
Supplemental Number
17794
Report Type
Supplemental Final
Operator Id
Name
Tc Oil Pipeline Operations Inc
Operator Street Address
920 Memorial City Way Suite 800
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77024
Local Datetime
2011-05-29 02:00:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
8.5
Intentional Release Bbls
0
Recovered Bbls
8.5
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Controller
Operator Type
Operator Employee
Incident Identified Datetime
2011-05-29 02:00:00
System Part Involved
Onshore Pump/meter Station Equipment And Piping
On Off Shore
Onshore
On Site Datetime
2011-05-29 03:00:00
Nrc Rpt Datetime
2011-05-29 03:12:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Severance Pump Station
Segment Name
Glacial Lakes
Onshore State Abbreviation
Ks
Onshore Postal Code
66538
Onshore City Name
Bendena
Onshore County Name
Doniphan
Designated Location
Milepost/valve Station
Designated Name
Mp742.2
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Instrumentation
Installation Year
2009
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Crack
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
8500
Est Cost Prop Damage
25000
Est Cost Emergency
120000
Est Cost Environmental
180000
Est Cost Other
0
Prpty
333500
Accident Psig
1100
Mop Psig
1297
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
Yes
Scada Conf Ind
Yes
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
The oil control center identified a pressure drop at the pump station.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Threaded Connection/coupling Failure
Eq Failure Type
Threaded Connection/coupling Failure
Other Stripped Ind
Pipe Nipple
Additional Vibration Ind
Yes
Preparer Name
D***** C* C*******
Preparer Title
Compliance Engineer
Preparer Email
D***********@t**********.com
Preparer Telephone
7014831434
Preparer Fax
7014831431
Prepared Date
2013-04-03 00:00:00
Authorizer Name
D***** C* C*******
Authorizer Telephone
7012901176
Authorizer Title
Compliance Engineer
Authorizer Email
D***********@t**********.com
Narrative
Pressure transmitter pt 201 at the severance pump station experienced a failure of the threaded 3/4 inch fitting. The failure of the 3/4" fitting failure occurred as a result of excessive vibration. The pump station was shutdown by oil control and isolated when pressure transmitter pt 201 began reading 4000 kpa less than station discharge pressure transmitter pt 203.The failed fitting resulted in the release of oil.
Report Received Date 2011-06-28 00:00:00
Iyear 2011
Report Number 20110208
Supplemental Number 17794
Report Type Supplemental Final
Operator Id 32334 PHMSA Enforcement
Name Tc Oil Pipeline Operations Inc
Operator Street Address 920 Memorial City Way Suite 800
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77024
Local Datetime 2011-05-29 02:00:00
Location Latitude 39.71864 Google Maps OpenStreetMap
Location Longitude -95.135 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 8.5
Intentional Release Bbls 0
Recovered Bbls 8.5
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Controller
Operator Type Operator Employee
Incident Identified Datetime 2011-05-29 02:00:00
System Part Involved Onshore Pump/meter Station Equipment And Piping
On Off Shore Onshore
On Site Datetime 2011-05-29 03:00:00
Nrc Rpt Datetime 2011-05-29 03:12:00
Nrc Rpt Num 977695 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Severance Pump Station
Segment Name Glacial Lakes
Onshore State Abbreviation Ks
Onshore Postal Code 66538
Onshore City Name Bendena
Onshore County Name Doniphan
Designated Location Milepost/valve Station
Designated Name Mp742.2
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Interstate
Item Involved Instrumentation
Installation Year 2009
Material Involved Carbon Steel
Release Type Leak
Leak Type Crack
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 8500
Est Cost Prop Damage 25000
Est Cost Emergency 120000
Est Cost Environmental 180000
Est Cost Other 0
Prpty 333500
Accident Psig 1100
Mop Psig 1297
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind Yes
Scada Conf Ind Yes
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details The oil control center identified a pressure drop at the pump station.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Equipment Failure
Cause Details Threaded Connection/coupling Failure
Eq Failure Type Threaded Connection/coupling Failure
Other Stripped Ind Pipe Nipple
Additional Vibration Ind Yes
Preparer Name D***** C* C*******
Preparer Title Compliance Engineer
Preparer Email D***********@t**********.com
Preparer Telephone 7014831434
Preparer Fax 7014831431
Prepared Date 2013-04-03 00:00:00
Authorizer Name D***** C* C*******
Authorizer Telephone 7012901176
Authorizer Title Compliance Engineer
Authorizer Email D***********@t**********.com
Narrative Pressure transmitter pt 201 at the severance pump station experienced a failure of the threaded 3/4 inch fitting. The failure of the 3/4" fitting failure occurred as a result of excessive vibration. The pump station was shutdown by oil control and isolated when pressure transmitter pt 201 began reading 4000 kpa less than station discharge pressure transmitter pt 203.The failed fitting resulted in the release of oil.

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