GTG incident on 2011-05-24 — TX

Operator
Enogex Llc
Cause
Natural Force Damage
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$100
Incident datetime
2011-05-24 15:45
Report number
Location
TX
Narrative
A tornado struck the l-102 wiedemann junction. A utility pole located outside the junction fell across the above ground portion of our sixteen inch pipeline and broke a 1 inch pipe nipple at the threaded connection to the pipeline. Gas control remotely closed the nearest automated upstream valve at our 12-12 juction and the nearest downstream valve at our edmond junction. On-call personnel arrived onsite to discover natural gas venting through the broken nipple. Personnel isolated a 16 inch manual valve inside the junction and vented a 10 miles segment of pipeline prior to replacing the broken nipple and 1 inch vent valve.
Detailed record list
Report Received Date
2011-06-23 00:00:00
Iyear
2011
Report Number
20110193
Supplemental Number
15263
Report Type
Original Final
Operator Id
Name
Enogex Llc
Operator Street Address
1300 Main Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2011-05-24 15:45:00
Location Latitude
Location Longitude
Commodity Released Type
Natural Gas
Unintentional Release
361.93
Intentional Release
2404.93
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2011-05-24 16:15:00
Restart Datetime
2011-05-24 17:45:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Incident Identified Datetime
2011-05-24 15:45:00
On Site Datetime
2011-05-24 16:15:00
On Off Shore
Onshore
Onshore State Abbreviation
Ok
Onshore Postal Code
73078
Onshore City Name
Piedmont
Onshore County Name
Canadian
Designated Location
Milepost
Designated Name
None
Pipe Fac Name
Wiedemann Junction
Segment Name
None
Federal
No
Location Type
Operator-Controlled Property
Incident Area Type
Aboveground
Incident Area Subtype
Typical Aboveground Facility Piping Or Appurtenance
Crossing
No
Pipe Facility Type
Intrastate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Other
Item Involved Details
1 Inch Pipe Nipple
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Utility Pole Fell On Top Of Above Ground Piping And Broke 1 Inch Pipe Nipple At Threaded Conenction To Pipeline.
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
293
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
0
Est Cost Unintentional Release
1494
Est Cost Intentional Release
8437
Est Cost Prop Damage
100
Est Cost Emergency
600
Est Cost Other
0
Prpty
10631
Accident Psig
381
Mop Psig
720
Mop Cfr Section
Not On Omb-Approved Form When Submitted
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Length Segment Isolated
68640
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Accident Identifier
Notification From Emergency Responder
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Incident was caused by an act of god, I.E. Tornado.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Natural Force Damage
Cause Details
High Winds
Natural Force Type
High Winds
Nf Extreme Weather Ind
Yes
Nf Tornado Ind
Yes
Preparer Name
M*** R***
Preparer Title
Manager Ehs Assessment And Compliance
Preparer Email
R*****@o**.com
Preparer Telephone
405 558-4685
Preparer Fax
405 557-8618
Authorizer Name
P*** M B*****
Authorizer Title
Vp Operations
Authorizer Telephone
405 525-7788
Authorizer Email
B*******@o**.com
Narrative
A tornado struck the l-102 wiedemann junction. A utility pole located outside the junction fell across the above ground portion of our sixteen inch pipeline and broke a 1 inch pipe nipple at the threaded connection to the pipeline. Gas control remotely closed the nearest automated upstream valve at our 12-12 juction and the nearest downstream valve at our edmond junction. On-call personnel arrived onsite to discover natural gas venting through the broken nipple. Personnel isolated a 16 inch manual valve inside the junction and vented a 10 miles segment of pipeline prior to replacing the broken nipple and 1 inch vent valve.
Report Received Date 2011-06-23 00:00:00
Iyear 2011
Report Number 20110193
Supplemental Number 15263
Report Type Original Final
Operator Id 26330 PHMSA Enforcement
Name Enogex Llc
Operator Street Address 1300 Main Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2011-05-24 15:45:00
Location Latitude 36.6385 Google Maps OpenStreetMap
Location Longitude -97.816 Google Maps OpenStreetMap
Commodity Released Type Natural Gas
Unintentional Release 361.93
Intentional Release 2404.93
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind Yes
Shutdown Datetime 2011-05-24 16:15:00
Restart Datetime 2011-05-24 17:45:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Incident Identified Datetime 2011-05-24 15:45:00
On Site Datetime 2011-05-24 16:15:00
On Off Shore Onshore
Onshore State Abbreviation Ok
Onshore Postal Code 73078
Onshore City Name Piedmont
Onshore County Name Canadian
Designated Location Milepost
Designated Name None
Pipe Fac Name Wiedemann Junction
Segment Name None
Federal No
Location Type Operator-Controlled Property
Incident Area Type Aboveground
Incident Area Subtype Typical Aboveground Facility Piping Or Appurtenance
Crossing No
Pipe Facility Type Intrastate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Other
Item Involved Details 1 Inch Pipe Nipple
Material Involved Carbon Steel
Release Type Other
Release Type Details Utility Pole Fell On Top Of Above Ground Piping And Broke 1 Inch Pipe Nipple At Threaded Conenction To Pipeline.
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 293
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 0
Est Cost Unintentional Release 1494
Est Cost Intentional Release 8437
Est Cost Prop Damage 100
Est Cost Emergency 600
Est Cost Other 0
Prpty 10631
Accident Psig 381
Mop Psig 720
Mop Cfr Section Not On Omb-Approved Form When Submitted View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Length Segment Isolated 68640
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Accident Identifier Notification From Emergency Responder
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Incident was caused by an act of god, I.E. Tornado.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Natural Force Damage
Cause Details High Winds
Natural Force Type High Winds
Nf Extreme Weather Ind Yes
Nf Tornado Ind Yes
Preparer Name M*** R***
Preparer Title Manager Ehs Assessment And Compliance
Preparer Email R*****@o**.com
Preparer Telephone 405 558-4685
Preparer Fax 405 557-8618
Authorizer Name P*** M B*****
Authorizer Title Vp Operations
Authorizer Telephone 405 525-7788
Authorizer Email B*******@o**.com
Narrative A tornado struck the l-102 wiedemann junction. A utility pole located outside the junction fell across the above ground portion of our sixteen inch pipeline and broke a 1 inch pipe nipple at the threaded connection to the pipeline. Gas control remotely closed the nearest automated upstream valve at our 12-12 juction and the nearest downstream valve at our edmond junction. On-call personnel arrived onsite to discover natural gas venting through the broken nipple. Personnel isolated a 16 inch manual valve inside the junction and vented a 10 miles segment of pipeline prior to replacing the broken nipple and 1 inch vent valve.

All rights reserved. Copyright © by ClearPHMSA