HL incident on 2011-06-16 — TX

Operator
Enterprise Products Operating Llc
Cause
Corrosion Failure
Commodity
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$303,053
Incident datetime
2011-06-16 15:05
Report number
Location
TX
Narrative
Liquid control center received a call from a deputy with san patricio county stating that he smelled gas near the intersection of hwy 181 and county road 79 near taft texas. Pl technicians were dispatched to the location and reported that vapors were coming from the casing vent on the north side of hwy 181 pipeline crossing. Blocked valves were closed and the line was isolated. Block valves were closed to isolate the section of pipeline where the leak occurred. Notifications where made to pipeline compliance, environmental and safety departments. Ncr# 979887, tx rrc# 665. Soil contamination - recommendation to dig out the area and replace with new soil. Corrective action: a pig will be placed into the pipeline and nitrogen will be used to remove the product from the section of pipeline containing the leak. The remaining nitrogen/product mix will be flared to the atmosphere and repairs will be made to correct the leak. Discovery - hole in pipe 1/8" in circumference, it was on the bottom inside of casing underneath railroad tract. Coating on the pipe was tgf3. This pipe and location was under rectifier current approx. 296.5 feet south of the rectifier location. 10'-0" segment of pipe with the corrosion caused hole was sent to stress engineering lab in houston. Last ili inspection on the system was in 2007.
Detailed record list
Report Received Date
2011-06-22 00:00:00
Iyear
2011
Report Number
20110189
Supplemental Number
16014
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2011-06-16 14:00:00
Location Latitude
Location Longitude
Commodity Released Type
Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype
Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls
50
Intentional Release Bbls
450
Recovered Bbls
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Call From A Deputy With San Patricio County Stating That He Smelled Gas
Incident Identified Datetime
2011-06-16 15:05:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2011-06-16 15:08:00
Restart Datetime
2011-06-30 03:30:00
On Site Datetime
2011-06-16 15:06:00
Nrc Rpt Datetime
2011-06-16 16:00:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Automatic
Downstream Valve Type Ind
Automatic
Num Pub Evacuated
0
Pipe Fac Name
L27a-10
Segment Name
Buttane Shuttle System
Onshore State Abbreviation
Tx
Onshore Postal Code
78390
Onshore City Name
Taft
Onshore County Name
San Patricio
Designated Location
Milepost/valve Station
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Other
Incident Area Details
Inside Casing Rr Tract And Roadway
Crossing
Yes
Railroad Crossing Ind
Yes
Railroad Type
Cased
Pipe Facility Type
Intrastate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
10
Pipe Wall Thickness
0.25
Pipe Smys
42000
Pipe Specification
Api-5l
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
1966
Manufactured Year
1966
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Corrosion
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
10000
Est Cost Gas Released
47250
Est Cost Prop Damage
303053
Est Cost Emergency
1000
Est Cost Environmental
5000
Est Cost Other
278697
Est Cost Other Details
Pipeline Bore, Replacement Pipe, Nitrogen, Flaring Of The Pipe Segment.
Prpty
645000
Accident Psig
190
Mop Psig
672
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
45408
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Leak inside casing
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Galvanic Corrosion Ind
Yes
Field Exam Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
1966
Shielding Evident
No
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Cp Annual Survey Year
2010
Prior Damage
Yes
Collected Data Ind
Yes
Other Tool Tech Ind
Yes
Has Hydrtst Conduc Before Ind
No
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
J*** J*****
Preparer Title
Compliance Engineer
Preparer Email
J******@e****.com
Preparer Telephone
7133817918
Preparer Fax
7133816660
Prepared Date
2011-08-25 00:00:00
Authorizer Name
J*** J*****
Authorizer Telephone
7133817918
Authorizer Title
Compliance Engineer
Authorizer Email
J******@e****.com
Narrative
Liquid control center received a call from a deputy with san patricio county stating that he smelled gas near the intersection of hwy 181 and county road 79 near taft texas. Pl technicians were dispatched to the location and reported that vapors were coming from the casing vent on the north side of hwy 181 pipeline crossing. Blocked valves were closed and the line was isolated. Block valves were closed to isolate the section of pipeline where the leak occurred. Notifications where made to pipeline compliance, environmental and safety departments. Ncr# 979887, tx rrc# 665. Soil contamination - recommendation to dig out the area and replace with new soil. Corrective action: a pig will be placed into the pipeline and nitrogen will be used to remove the product from the section of pipeline containing the leak. The remaining nitrogen/product mix will be flared to the atmosphere and repairs will be made to correct the leak. Discovery - hole in pipe 1/8" in circumference, it was on the bottom inside of casing underneath railroad tract. Coating on the pipe was tgf3. This pipe and location was under rectifier current approx. 296.5 feet south of the rectifier location. 10'-0" segment of pipe with the corrosion caused hole was sent to stress engineering lab in houston. Last ili inspection on the system was in 2007.
Report Received Date 2011-06-22 00:00:00
Iyear 2011
Report Number 20110189
Supplemental Number 16014
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2011-06-16 14:00:00
Location Latitude 27.959521 Google Maps OpenStreetMap
Location Longitude -97.360576 Google Maps OpenStreetMap
Commodity Released Type Hvl Or Other Flammable Or Toxic Fluid Which Is A Gas At Ambient Conditions
Commodity Subtype Lpg (Liquefied Petroleum Gas) / Ngl (Natural Gas Liquid)
Unintentional Release Bbls 50
Intentional Release Bbls 450
Recovered Bbls 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Call From A Deputy With San Patricio County Stating That He Smelled Gas
Incident Identified Datetime 2011-06-16 15:05:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2011-06-16 15:08:00
Restart Datetime 2011-06-30 03:30:00
On Site Datetime 2011-06-16 15:06:00
Nrc Rpt Datetime 2011-06-16 16:00:00
Nrc Rpt Num 979887 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Automatic
Downstream Valve Type Ind Automatic
Num Pub Evacuated 0
Pipe Fac Name L27a-10
Segment Name Buttane Shuttle System
Onshore State Abbreviation Tx
Onshore Postal Code 78390
Onshore City Name Taft
Onshore County Name San Patricio
Designated Location Milepost/valve Station
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Other
Incident Area Details Inside Casing Rr Tract And Roadway
Crossing Yes
Railroad Crossing Ind Yes
Railroad Type Cased
Pipe Facility Type Intrastate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 10
Pipe Wall Thickness 0.25
Pipe Smys 42000
Pipe Specification Api-5l
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Installation Year 1966
Manufactured Year 1966
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Corrosion
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca No
Commodity Reached Hca No
Est Cost Oper Paid 10000
Est Cost Gas Released 47250
Est Cost Prop Damage 303053
Est Cost Emergency 1000
Est Cost Environmental 5000
Est Cost Other 278697
Est Cost Other Details Pipeline Bore, Replacement Pipe, Nitrogen, Flaring Of The Pipe Segment.
Prpty 645000
Accident Psig 190
Mop Psig 672
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 45408
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Leak inside casing
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Galvanic Corrosion Ind Yes
Field Exam Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year 1966
Shielding Evident No
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Cp Annual Survey Year 2010
Prior Damage Yes
Collected Data Ind Yes
Other Tool Tech Ind Yes
Has Hydrtst Conduc Before Ind No
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name J*** J*****
Preparer Title Compliance Engineer
Preparer Email J******@e****.com
Preparer Telephone 7133817918
Preparer Fax 7133816660
Prepared Date 2011-08-25 00:00:00
Authorizer Name J*** J*****
Authorizer Telephone 7133817918
Authorizer Title Compliance Engineer
Authorizer Email J******@e****.com
Narrative Liquid control center received a call from a deputy with san patricio county stating that he smelled gas near the intersection of hwy 181 and county road 79 near taft texas. Pl technicians were dispatched to the location and reported that vapors were coming from the casing vent on the north side of hwy 181 pipeline crossing. Blocked valves were closed and the line was isolated. Block valves were closed to isolate the section of pipeline where the leak occurred. Notifications where made to pipeline compliance, environmental and safety departments. Ncr# 979887, tx rrc# 665. Soil contamination - recommendation to dig out the area and replace with new soil. Corrective action: a pig will be placed into the pipeline and nitrogen will be used to remove the product from the section of pipeline containing the leak. The remaining nitrogen/product mix will be flared to the atmosphere and repairs will be made to correct the leak. Discovery - hole in pipe 1/8" in circumference, it was on the bottom inside of casing underneath railroad tract. Coating on the pipe was tgf3. This pipe and location was under rectifier current approx. 296.5 feet south of the rectifier location. 10'-0" segment of pipe with the corrosion caused hole was sent to stress engineering lab in houston. Last ili inspection on the system was in 2007.

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