HL incident on 2011-05-09 — TX

Operator
Enterprise Products Operating Llc
Cause
Incorrect Operation
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$100
Incident datetime
2011-05-09 19:15
Report number
Location
TX
Narrative
While transferring product (jet-a) from the bottom of tank 3404 to a frac tank with a diaphram pump, the frac tank was overfilled. The product traveled through a series of drainage ditches and was contained in the north terminal secondary containment pond. Spill was recovered from the containment pond with a vacuum truck and stored in a frac tank. Booms and pads were used to recover product from drainage ditches. Er team from clean harbors responded to scene to perform clean up, along with additional help from the o&m construction crew. An incident investigation is being performed and procedures will be reviewed. Discussion was held with both employees involved and written statements were received. 3/4/2013 updated report to reflect changes in part a9, a10, and a11 total of 60 bbls was unintentionally release. Total of 50 bbls was recovered.
Detailed record list
Report Received Date
2011-06-09 00:00:00
Iyear
2011
Report Number
20110176
Supplemental Number
17616
Report Type
Supplemental Final
Operator Id
Name
Enterprise Products Operating Llc
Operator Street Address
1100 Louisiana Street
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
77002
Local Datetime
2011-05-09 19:15:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls
60
Intentional Release Bbls
0
Recovered Bbls
50
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Operator Employee
Incident Identified Datetime
2011-05-09 19:15:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Frac Tank Was Overfilled While Transferring Product.
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Lebanon Terminal
Segment Name
Lebanon Tank 3404
Onshore State Abbreviation
Oh
Onshore Postal Code
45036
Onshore City Name
Lebanon
Onshore County Name
Warren
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Tank, Including Attached Appurtenances
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Other
Item Involved Details
Frac Tank
Installation Year
2011
Material Involved
Material Other Than Carbon Steel
Material Details
Other Type - Will Investigate
Release Type
Overfill Or Overflow
Wildlife Impact Ind
No
Soil Contamination
Yes
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
7500
Est Cost Prop Damage
100
Est Cost Emergency
184745
Est Cost Environmental
64690
Est Cost Other
0
Est Cost Other Details
0
Prpty
257035
Accident Psig
0
Mop Psig
0
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Incorrect procedure in the leak.
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Incorrect Operation
Cause Details
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type
Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind
Inadequate Monitoring
Related Failure Follow Ind
Yes
Category Type
Other Maintenance
Operator Qualification Ind
Yes
Qualified Individuals
Yes, They Were Qualified For The Task(S)
Preparer Name
N*** B******
Preparer Title
Sr. Pipeline Compliance Specialist
Preparer Email
B****@e****.com
Preparer Telephone
713-381-3536
Preparer Fax
281-887-7704
Prepared Date
2013-03-20 00:00:00
Authorizer Name
N*** B******
Authorizer Telephone
713-381-3536
Authorizer Title
Senior Transportation Compliance Specialist
Authorizer Email
W********@e****.com
Narrative
While transferring product (jet-a) from the bottom of tank 3404 to a frac tank with a diaphram pump, the frac tank was overfilled. The product traveled through a series of drainage ditches and was contained in the north terminal secondary containment pond. Spill was recovered from the containment pond with a vacuum truck and stored in a frac tank. Booms and pads were used to recover product from drainage ditches. Er team from clean harbors responded to scene to perform clean up, along with additional help from the o&m construction crew. An incident investigation is being performed and procedures will be reviewed. Discussion was held with both employees involved and written statements were received. 3/4/2013 updated report to reflect changes in part a9, a10, and a11 total of 60 bbls was unintentionally release. Total of 50 bbls was recovered.
Report Received Date 2011-06-09 00:00:00
Iyear 2011
Report Number 20110176
Supplemental Number 17616
Report Type Supplemental Final
Operator Id 31618 PHMSA Enforcement
Name Enterprise Products Operating Llc
Operator Street Address 1100 Louisiana Street
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 77002
Local Datetime 2011-05-09 19:15:00
Location Latitude 39.482631 Google Maps OpenStreetMap
Location Longitude -84.223042 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Mixture Of Refined Products (Transmix Or Other Mixture)
Unintentional Release Bbls 60
Intentional Release Bbls 0
Recovered Bbls 50
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Operator Employee
Incident Identified Datetime 2011-05-09 19:15:00
System Part Involved Onshore Terminal/tank Farm Equipment And Piping
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Frac Tank Was Overfilled While Transferring Product.
Nrc Rpt Num 975838 NRC Report How to search
Ignite Ind No
Explode Ind No
Num Pub Evacuated 0
Pipe Fac Name Lebanon Terminal
Segment Name Lebanon Tank 3404
Onshore State Abbreviation Oh
Onshore Postal Code 45036
Onshore City Name Lebanon
Onshore County Name Warren
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Tank, Including Attached Appurtenances
Crossing No
Pipe Facility Type Interstate
Item Involved Other
Item Involved Details Frac Tank
Installation Year 2011
Material Involved Material Other Than Carbon Steel
Material Details Other Type - Will Investigate
Release Type Overfill Or Overflow
Wildlife Impact Ind No
Soil Contamination Yes
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca No
Est Cost Oper Paid 0
Est Cost Gas Released 7500
Est Cost Prop Damage 100
Est Cost Emergency 184745
Est Cost Environmental 64690
Est Cost Other 0
Est Cost Other Details 0
Prpty 257035
Accident Psig 0
Mop Psig 0
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Pipeline Function > 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Incorrect procedure in the leak.
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Incorrect Operation
Cause Details Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Operation Type Tank, Vessel, Or Sump/separator Allowed Or Caused To Overfill Or Overflow
Overflow Other Ind Inadequate Monitoring
Related Failure Follow Ind Yes
Category Type Other Maintenance
Operator Qualification Ind Yes
Qualified Individuals Yes, They Were Qualified For The Task(S)
Preparer Name N*** B******
Preparer Title Sr. Pipeline Compliance Specialist
Preparer Email B****@e****.com
Preparer Telephone 713-381-3536
Preparer Fax 281-887-7704
Prepared Date 2013-03-20 00:00:00
Authorizer Name N*** B******
Authorizer Telephone 713-381-3536
Authorizer Title Senior Transportation Compliance Specialist
Authorizer Email W********@e****.com
Narrative While transferring product (jet-a) from the bottom of tank 3404 to a frac tank with a diaphram pump, the frac tank was overfilled. The product traveled through a series of drainage ditches and was contained in the north terminal secondary containment pond. Spill was recovered from the containment pond with a vacuum truck and stored in a frac tank. Booms and pads were used to recover product from drainage ditches. Er team from clean harbors responded to scene to perform clean up, along with additional help from the o&m construction crew. An incident investigation is being performed and procedures will be reviewed. Discussion was held with both employees involved and written statements were received. 3/4/2013 updated report to reflect changes in part a9, a10, and a11 total of 60 bbls was unintentionally release. Total of 50 bbls was recovered.

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