HL incident on 2011-05-19 — OH

Operator
Marathon Pipe Line Llc
Cause
Incorrect Operation
Commodity
Crude Oil
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$178,000
Incident datetime
2011-05-19 09:30
Report number
Location
OH
Narrative
Price of commodity lost was calculated assuming $100/barrel. 3 gallons of crude oil at $100/barrel was less than $10. During the installation of a casing vent to prep a casing for wax filling, a welder was torch cutting a hole in the casing for the installation of a new 2" casing vent. There was at least a 1" gap between the casing and the carrier pipe. While cutting the casing, a flash fire and 3 gallon crude release occurred from an inadvertent burn-through of the carrier pipe. Contractor informed operator about release, but delayed in informing the operator of the fire. Call to nrc was made approximately 30 minutes after operator received notification that a flash fire event occurred. Pipe segment has not been cut out and it is not currently scheduled to be cut out.
Detailed record list
Report Received Date
2011-06-09 00:00:00
Iyear
2011
Report Number
20110172
Supplemental Number
17960
Report Type
Supplemental Final
Operator Id
Name
Marathon Pipe Line Llc
Operator Street Address
539 South Main Street
Operator City Name
Findlay
Operator State Abbreviation
OH
Operator Postal Code
45840
Local Datetime
2011-05-19 09:30:00
Location Latitude
Location Longitude
Commodity Released Type
Crude Oil
Unintentional Release Bbls
0.08
Intentional Release Bbls
0
Recovered Bbls
0.08
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Local Operating Personnel, Including Contractors
Operator Type
Contractor Working For The Operator
Incident Identified Datetime
2011-05-19 09:30:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
No
Shutdown Explain
Mainline Was Delivering To Another Party, So This Delivery Line Was Not Active.
On Site Datetime
2011-05-19 09:30:00
Nrc Rpt Datetime
2011-05-19 13:41:00
Nrc Rpt Num
Ignite Ind
Yes
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Remotely Controlled
Num Pub Evacuated
0
Pipe Fac Name
Martinsville-Lima 22" Crude
Segment Name
Lima Metering To Lima Tank Farm
Onshore State Abbreviation
Oh
Onshore Postal Code
45804
Onshore City Name
Lima
Onshore County Name
Allen
Designated Location
Milepost/valve Station
Designated Name
Tank Farm
Federal
No
Location Type
Totally Contained On Operator-Controlled Property
Incident Area Type
Underground
Incident Area Subtype
Exposed Due To Excavation
Depth Of Cover
72
Crossing
Yes
Railroad Crossing Ind
Yes
Railroad Type
Cased, Bored/drilled
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
22
Pipe Wall Thickness
0.312
Pipe Smys
46000
Pipe Specification
Api 5l
Pipe Seam Type
Seamless
Pipe Manufacturer
Unknown
Pipe Coating Type
Coal Tar
Installation Year
1952
Manufactured Year
1952
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Other
Leak Type Other
Inadvertent Burn-Through.
Wildlife Impact Ind
No
Soil Contamination
No
Long Term Assessment
No
Remediation Ind
No
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
10
Est Cost Prop Damage
178000
Est Cost Emergency
0
Est Cost Environmental
0
Est Cost Other
0
Prpty
178010
Accident Psig
11
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
5800
Internal Inspection Ind
No
Diameter Change Ind
Yes
Operation Complications Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
Yes
Cpm Operating Ind
Yes
Cpm Functional Ind
Yes
Cpm Detection Ind
No
Cpm Conf Ind
No
Investigation Status
No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details
Release was identified during project execution in field while line segment was down. Controllers had no influence on the situation, and release rate was below scada and cpm leak detection thresholds.
Employee Drug Test Ind
No
Contractor Drug Test Ind
Yes
Num Contractors Tested
2
Num Contractors Failed
0
Cause
Incorrect Operation
Cause Details
Other Incorrect Operation
Operation Type
Other Incorrect Operation
Operation Details
While Torch Cutting A Hole In The Casing For The Installation Of A New 2" Casing Vent, A Flash Fire And 3 Gallon Release Occurred From An Inadvertent Burn-Through Of The Carrier Pipe. Procedures Will Be Updated To Require A Heat Shield Or Equivalent Protections When Performing Such Work In The Future.
Related Inadequate Proc Ind
Yes
Category Type
Other Maintenance
Operator Qualification Ind
No
Preparer Name
R**** S********
Preparer Title
Hes Professional
Preparer Email
R**********@m****************.com
Preparer Telephone
4194212891
Preparer Fax
4194213917
Prepared Date
2013-04-29 00:00:00
Authorizer Name
R**** B*****
Authorizer Telephone
4194213712
Authorizer Title
Regulatory Compliance Supervisor
Authorizer Email
R*******@m****************.com
Narrative
Price of commodity lost was calculated assuming $100/barrel. 3 gallons of crude oil at $100/barrel was less than $10. During the installation of a casing vent to prep a casing for wax filling, a welder was torch cutting a hole in the casing for the installation of a new 2" casing vent. There was at least a 1" gap between the casing and the carrier pipe. While cutting the casing, a flash fire and 3 gallon crude release occurred from an inadvertent burn-through of the carrier pipe. Contractor informed operator about release, but delayed in informing the operator of the fire. Call to nrc was made approximately 30 minutes after operator received notification that a flash fire event occurred. Pipe segment has not been cut out and it is not currently scheduled to be cut out.
Report Received Date 2011-06-09 00:00:00
Iyear 2011
Report Number 20110172
Supplemental Number 17960
Report Type Supplemental Final
Operator Id 32147 PHMSA Enforcement
Name Marathon Pipe Line Llc
Operator Street Address 539 South Main Street
Operator City Name Findlay
Operator State Abbreviation OH
Operator Postal Code 45840
Local Datetime 2011-05-19 09:30:00
Location Latitude 40.706216 Google Maps OpenStreetMap
Location Longitude -84.1146149 Google Maps OpenStreetMap
Commodity Released Type Crude Oil
Unintentional Release Bbls 0.08
Intentional Release Bbls 0
Recovered Bbls 0.08
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Local Operating Personnel, Including Contractors
Operator Type Contractor Working For The Operator
Incident Identified Datetime 2011-05-19 09:30:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind No
Shutdown Explain Mainline Was Delivering To Another Party, So This Delivery Line Was Not Active.
On Site Datetime 2011-05-19 09:30:00
Nrc Rpt Datetime 2011-05-19 13:41:00
Nrc Rpt Num 976769 NRC Report How to search
Ignite Ind Yes
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Remotely Controlled
Num Pub Evacuated 0
Pipe Fac Name Martinsville-Lima 22" Crude
Segment Name Lima Metering To Lima Tank Farm
Onshore State Abbreviation Oh
Onshore Postal Code 45804
Onshore City Name Lima
Onshore County Name Allen
Designated Location Milepost/valve Station
Designated Name Tank Farm
Federal No
Location Type Totally Contained On Operator-Controlled Property
Incident Area Type Underground
Incident Area Subtype Exposed Due To Excavation
Depth Of Cover 72
Crossing Yes
Railroad Crossing Ind Yes
Railroad Type Cased, Bored/drilled
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 22
Pipe Wall Thickness 0.312
Pipe Smys 46000
Pipe Specification Api 5l
Pipe Seam Type Seamless
Pipe Manufacturer Unknown
Pipe Coating Type Coal Tar
Installation Year 1952
Manufactured Year 1952
Material Involved Carbon Steel
Release Type Leak
Leak Type Other
Leak Type Other Inadvertent Burn-Through.
Wildlife Impact Ind No
Soil Contamination No
Long Term Assessment No
Remediation Ind No
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 10
Est Cost Prop Damage 178000
Est Cost Emergency 0
Est Cost Environmental 0
Est Cost Other 0
Prpty 178010
Accident Psig 11
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 5800
Internal Inspection Ind No
Diameter Change Ind Yes
Operation Complications Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind No
Cpm In Place Ind Yes
Cpm Operating Ind Yes
Cpm Functional Ind Yes
Cpm Detection Ind No
Cpm Conf Ind No
Investigation Status No, the operator did not find that an investigation of the controller(s) actions or control room issues was necessary due to: (provide an explanation for why the operator did not investigate)
Investigation Status Details Release was identified during project execution in field while line segment was down. Controllers had no influence on the situation, and release rate was below scada and cpm leak detection thresholds.
Employee Drug Test Ind No
Contractor Drug Test Ind Yes
Num Contractors Tested 2
Num Contractors Failed 0
Cause Incorrect Operation
Cause Details Other Incorrect Operation
Operation Type Other Incorrect Operation
Operation Details While Torch Cutting A Hole In The Casing For The Installation Of A New 2" Casing Vent, A Flash Fire And 3 Gallon Release Occurred From An Inadvertent Burn-Through Of The Carrier Pipe. Procedures Will Be Updated To Require A Heat Shield Or Equivalent Protections When Performing Such Work In The Future.
Related Inadequate Proc Ind Yes
Category Type Other Maintenance
Operator Qualification Ind No
Preparer Name R**** S********
Preparer Title Hes Professional
Preparer Email R**********@m****************.com
Preparer Telephone 4194212891
Preparer Fax 4194213917
Prepared Date 2013-04-29 00:00:00
Authorizer Name R**** B*****
Authorizer Telephone 4194213712
Authorizer Title Regulatory Compliance Supervisor
Authorizer Email R*******@m****************.com
Narrative Price of commodity lost was calculated assuming $100/barrel. 3 gallons of crude oil at $100/barrel was less than $10. During the installation of a casing vent to prep a casing for wax filling, a welder was torch cutting a hole in the casing for the installation of a new 2" casing vent. There was at least a 1" gap between the casing and the carrier pipe. While cutting the casing, a flash fire and 3 gallon crude release occurred from an inadvertent burn-through of the carrier pipe. Contractor informed operator about release, but delayed in informing the operator of the fire. Call to nrc was made approximately 30 minutes after operator received notification that a flash fire event occurred. Pipe segment has not been cut out and it is not currently scheduled to be cut out.

All rights reserved. Copyright © by ClearPHMSA