GTG incident on 2011-04-25 — TX

Operator
Panhandle Eastern Pipeline Co
Cause
Natural Force Damage
Commodity
Natural Gas
Program
GTG
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$286,759
Incident datetime
2011-04-25 02:20
Report number
Location
TX
Narrative
The pleasant hill 200 line is 22-in. Od x 0.281-in. Wt, API 5l grade x42, seamless pipeline. The cause of the coupling separation at mp 31.5 was the combined effect of local loss of soil cover in conjunction with recent high rainfall. The month preceding the incident experienced historically high quantities of rainfall. The resulting water table was high enough to produce upward buoyant forces on the pipe, while the probable saturation of the soil cover reduced its breakout resistance. The combination of buoyant forces and upward thrust forces produced by an apparent small angular misalignment at the separated coupling exceeded the upthrust resistance of the soil. **this report is being submitted in response to PHMSA's request, (docket id PHMSA-2013-0028), for supplemental reports from operators who submitted reports for incidents occurring after january 1, 2010, with any of the following: (1) ``pipe girth weld'' was selected as the ``item involved in incident'' in part c3 of the report. The revised report collects data about the pipe adjacent to the girth weld. (2) ``function of pipeline system'' is null in part e5f of the report. The revised report collects the function of the pipeline system for all incidents.** this supplemental report is to acknowledge that the two relevant sections in PHMSA's request have been reviewed and no further actions were needed.
Detailed record list
Report Received Date
2011-05-24 00:00:00
Iyear
2011
Report Number
20110151
Supplemental Number
16025
Report Type
Supplemental Final
Operator Id
Name
Panhandle Eastern Pipeline Co
Operator Street Address
5051 Westheimer Road
Operator City Name
Houston
Operator State Abbreviation
TX
Operator Postal Code
770565306
Local Datetime
2011-04-25 02:07:00
Location Latitude
Location Longitude
Nrc Rpt Num
Nrc Rpt Datetime
2011-04-25 04:45:00
Commodity Released Type
Natural Gas
Unintentional Release
58700
Intentional Release
5155
Accompanying Liquid
0
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2011-04-25 03:20:00
Restart Datetime
2011-05-05 08:10:00
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
30
Incident Identified Datetime
2011-04-25 02:20:00
On Site Datetime
2011-04-25 03:26:00
On Off Shore
Onshore
Onshore State Abbreviation
Il
Onshore Postal Code
62633
Onshore City Name
Manchester
Onshore County Name
Scott
Designated Location
Survey Station No.
Designated Name
1666+17
Pipe Fac Name
Pleasant Hill 200
Segment Name
41-05-002-2000
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
10
Crossing
No
Pipe Facility Type
Interstate
System Part Involved
Onshore Pipeline, Including Valve Sites
Item Involved
Other
Item Involved Details
Coupling
Installation Year
1940
Material Involved
Carbon Steel
Release Type
Other
Release Type Details
Pipe Pulled Out Of The Coupling
Class Location Type
Class 1 Location
Could Be Hca
No
Pir Radius
429
Heat Damage Ind
No
Non Heat Damage Ind
No
Hca Fatalities Ind
No
Est Cost Oper Paid
2000
Est Cost Unintentional Release
232728
Est Cost Intentional Release
21865
Est Cost Prop Damage
286759
Est Cost Emergency
3000
Est Cost Other
20000
Est Cost Other Details
Other Cost Is Failure Analysis Estimate
Prpty
566352
Accident Psig
749
Mop Psig
800
Mop Cfr Section
Not On Omb-Approved Form When Submitted
Accident Pressure
Pressure Did Not Exceed Maop
Pressure Restriction Ind
No
Upstream Valve Type Ind
Manual
Downstream Valve Type Ind
Manual
Length Segment Isolated
73898
Internal Inspection Ind
Yes
Operation Complications Ind
No
Pipeline Function
Transmission System
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
Yes
Accident Identifier
Notification From Public
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind
Yes
Invest No Controller Ind
Yes
Invest Other Ind
Yes
Invest Other Ind Details
Lessons Learned Regarding Staffing, Alarm Management And Labeling.
Employee Drug Test Ind
Yes
Contractor Drug Test Ind
No
Num Employees Tested
1
Num Employees Failed
0
Cause
Natural Force Damage
Cause Details
Heavy Rains/floods
Natural Force Type
Heavy Rains/floods
Heavy Rains Subtype
Flotation
Nf Extreme Weather Ind
No
Preparer Name
N***** H******
Preparer Title
Director Interstate Regulatory Compliance
Preparer Email
N*************@e*************.com
Preparer Telephone
713-857-5479
Authorizer Name
N***** H******
Authorizer Title
Director Interstate Regulatory Compliance
Authorizer Telephone
713-857-5479
Authorizer Email
N*************@e*************.com
Narrative
The pleasant hill 200 line is 22-in. Od x 0.281-in. Wt, API 5l grade x42, seamless pipeline. The cause of the coupling separation at mp 31.5 was the combined effect of local loss of soil cover in conjunction with recent high rainfall. The month preceding the incident experienced historically high quantities of rainfall. The resulting water table was high enough to produce upward buoyant forces on the pipe, while the probable saturation of the soil cover reduced its breakout resistance. The combination of buoyant forces and upward thrust forces produced by an apparent small angular misalignment at the separated coupling exceeded the upthrust resistance of the soil. **this report is being submitted in response to PHMSA's request, (docket id PHMSA-2013-0028), for supplemental reports from operators who submitted reports for incidents occurring after january 1, 2010, with any of the following: (1) ``pipe girth weld'' was selected as the ``item involved in incident'' in part c3 of the report. The revised report collects data about the pipe adjacent to the girth weld. (2) ``function of pipeline system'' is null in part e5f of the report. The revised report collects the function of the pipeline system for all incidents.** this supplemental report is to acknowledge that the two relevant sections in PHMSA's request have been reviewed and no further actions were needed.
Report Received Date 2011-05-24 00:00:00
Iyear 2011
Report Number 20110151
Supplemental Number 16025
Report Type Supplemental Final
Operator Id 15105 PHMSA Enforcement
Name Panhandle Eastern Pipeline Co
Operator Street Address 5051 Westheimer Road
Operator City Name Houston
Operator State Abbreviation TX
Operator Postal Code 770565306
Local Datetime 2011-04-25 02:07:00
Location Latitude 39.573555 Google Maps OpenStreetMap
Location Longitude -90.3549 Google Maps OpenStreetMap
Nrc Rpt Num 973910 NRC Report How to search
Nrc Rpt Datetime 2011-04-25 04:45:00
Commodity Released Type Natural Gas
Unintentional Release 58700
Intentional Release 5155
Accompanying Liquid 0
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Shutdown Due Accident Ind Yes
Shutdown Datetime 2011-04-25 03:20:00
Restart Datetime 2011-05-05 08:10:00
Ignite Ind No
Explode Ind No
Num Pub Evacuated 30
Incident Identified Datetime 2011-04-25 02:20:00
On Site Datetime 2011-04-25 03:26:00
On Off Shore Onshore
Onshore State Abbreviation Il
Onshore Postal Code 62633
Onshore City Name Manchester
Onshore County Name Scott
Designated Location Survey Station No.
Designated Name 1666+17
Pipe Fac Name Pleasant Hill 200
Segment Name 41-05-002-2000
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Soil
Depth Of Cover 10
Crossing No
Pipe Facility Type Interstate
System Part Involved Onshore Pipeline, Including Valve Sites
Item Involved Other
Item Involved Details Coupling
Installation Year 1940
Material Involved Carbon Steel
Release Type Other
Release Type Details Pipe Pulled Out Of The Coupling
Class Location Type Class 1 Location
Could Be Hca No
Pir Radius 429
Heat Damage Ind No
Non Heat Damage Ind No
Hca Fatalities Ind No
Est Cost Oper Paid 2000
Est Cost Unintentional Release 232728
Est Cost Intentional Release 21865
Est Cost Prop Damage 286759
Est Cost Emergency 3000
Est Cost Other 20000
Est Cost Other Details Other Cost Is Failure Analysis Estimate
Prpty 566352
Accident Psig 749
Mop Psig 800
Mop Cfr Section Not On Omb-Approved Form When Submitted View CFR 49 §192
Accident Pressure Pressure Did Not Exceed Maop
Pressure Restriction Ind No
Upstream Valve Type Ind Manual
Downstream Valve Type Ind Manual
Length Segment Isolated 73898
Internal Inspection Ind Yes
Operation Complications Ind No
Pipeline Function Transmission System
Scada In Place Ind Yes
Scada Operating Ind Yes
Scada Functional Ind Yes
Scada Detection Ind No
Scada Conf Ind Yes
Accident Identifier Notification From Public
Investigation Status Yes, specify investigation result(s): (select all that apply)
Invest Schedule Ind Yes
Invest No Controller Ind Yes
Invest Other Ind Yes
Invest Other Ind Details Lessons Learned Regarding Staffing, Alarm Management And Labeling.
Employee Drug Test Ind Yes
Contractor Drug Test Ind No
Num Employees Tested 1
Num Employees Failed 0
Cause Natural Force Damage
Cause Details Heavy Rains/floods
Natural Force Type Heavy Rains/floods
Heavy Rains Subtype Flotation
Nf Extreme Weather Ind No
Preparer Name N***** H******
Preparer Title Director Interstate Regulatory Compliance
Preparer Email N*************@e*************.com
Preparer Telephone 713-857-5479
Authorizer Name N***** H******
Authorizer Title Director Interstate Regulatory Compliance
Authorizer Telephone 713-857-5479
Authorizer Email N*************@e*************.com
Narrative The pleasant hill 200 line is 22-in. Od x 0.281-in. Wt, API 5l grade x42, seamless pipeline. The cause of the coupling separation at mp 31.5 was the combined effect of local loss of soil cover in conjunction with recent high rainfall. The month preceding the incident experienced historically high quantities of rainfall. The resulting water table was high enough to produce upward buoyant forces on the pipe, while the probable saturation of the soil cover reduced its breakout resistance. The combination of buoyant forces and upward thrust forces produced by an apparent small angular misalignment at the separated coupling exceeded the upthrust resistance of the soil. **this report is being submitted in response to PHMSA's request, (docket id PHMSA-2013-0028), for supplemental reports from operators who submitted reports for incidents occurring after january 1, 2010, with any of the following: (1) ``pipe girth weld'' was selected as the ``item involved in incident'' in part c3 of the report. The revised report collects data about the pipe adjacent to the girth weld. (2) ``function of pipeline system'' is null in part e5f of the report. The revised report collects the function of the pipeline system for all incidents.** this supplemental report is to acknowledge that the two relevant sections in PHMSA's request have been reviewed and no further actions were needed.

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