Incident details
Operator, cause, commodity and consequences with raw source fields.
HL incident on 2011-04-13 — OH
Operator
Marathon Pipe Line Llc
Cause
Equipment Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities
0 injuries
Property damage (nominal)
$193,000
Incident datetime
2011-04-13 18:58
Report number
Location
OH
Narrative
Wolverine received a call from a landowner indicating odors and sheen in bauer drain. Wolverine initially responded, later notifying marathon petroleum company. It was determined that the release was from a marathon petroleum company tank line, operated by wolverine. Initial nrc call was made by wolverine. Supplemental nrc reports were made by marathon pipe line. A gasket failure on the tank line was initially identified as the leak source. After the completion of the investigation it was determined that the gasket failed due to misalignment during construction. The amount released was calculated based on field investigation data. Boom was initially placed in bauer drain and recovery wells installed to collect free product. Mpl has removed 4,500 tons of non-hazardous impacted soils from this site. This is an on-going remediation effort and the report includes the estimated final remediation costs.
Detailed record list
Report Received Date
2011-05-13 00:00:00
Iyear
2011
Report Number
20110140
Supplemental Number
20225
Report Type
Supplemental Final
Operator Id
32147
Name
Marathon Pipe Line Llc
Operator Street Address
539 South Main Street
Operator City Name
Findlay
Operator State Abbreviation
OH
Operator Postal Code
45840
Local Datetime
2011-04-13 18:58:00
Location Latitude
42.514136
Location Longitude
-84.242059
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
9000
Intentional Release Bbls
0
Recovered Bbls
6643
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Notification From Public
Incident Identified Datetime
2011-04-13 18:58:00
System Part Involved
Onshore Terminal/tank Farm Equipment And Piping
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2011-04-13 19:02:00
Restart Datetime
2011-04-18 15:20:00
On Site Datetime
2011-04-13 18:58:00
Nrc Rpt Datetime
2011-04-13 21:55:00
Nrc Rpt Num
972904
Ignite Ind
No
Explode Ind
No
Num Pub Evacuated
0
Pipe Fac Name
Wolverine Pipeline
Segment Name
Stockbridge Tank 681 Tank Line
Onshore State Abbreviation
Mi
Onshore Postal Code
48819
Onshore City Name
Dansville
Onshore County Name
Ingham
Designated Location
Milepost/valve Station
Designated Name
Stockbridge
Federal
No
Location Type
Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property
Incident Area Type
Underground
Incident Area Subtype
Under Soil
Depth Of Cover
24
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Flange Assembly
Installation Year
2002
Material Involved
Material Other Than Carbon Steel
Material Details
Gasket
Release Type
Leak
Leak Type
Connection Failure
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Surface Water Remed Ind
Yes
Groundwater Remed Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
Yes
Surface Contam Ind
Yes
Groundwater Contam Ind
Yes
Amount Released
1
Rel Water Name
Bauer Drain
Could Be Hca
No
Commodity Reached Hca
No
Est Cost Oper Paid
0
Est Cost Gas Released
350000
Est Cost Prop Damage
193000
Est Cost Emergency
14885903
Est Cost Environmental
20300000
Est Cost Other
0
Prpty
35728903
Accident Psig
0
Mop Psig
0
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Pipeline Function
> 20% Smys Regulated Transmission
Scada In Place Ind
Yes
Scada Operating Ind
Yes
Scada Functional Ind
Yes
Scada Detection Ind
No
Scada Conf Ind
No
Cpm In Place Ind
No
Investigation Status
Yes, specify investigation result(s): (select all that apply)
Invest No Control Room Ind
Yes
Invest No Controller Ind
Yes
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Equipment Failure
Cause Details
Non-Threaded Connection Failure
Eq Failure Type
Non-Threaded Connection Failure
Other Non Threaded Ind
Gasket
Additional Installation Ind
Yes
Ief Addl Misalignment Ind
Yes
Preparer Name
R**** S********
Preparer Title
Hes Professional
Preparer Email
R**********@m****************.com
Preparer Telephone
4194212121
Prepared Date
2015-03-12 00:00:00
Authorizer Name
R****** B*****
Authorizer Telephone
4194212121
Authorizer Title
Regulatory Compliance Supervisor
Authorizer Email
R*******@m****************.com
Narrative
Wolverine received a call from a landowner indicating odors and sheen in bauer drain. Wolverine initially responded, later notifying marathon petroleum company. It was determined that the release was from a marathon petroleum company tank line, operated by wolverine. Initial nrc call was made by wolverine. Supplemental nrc reports were made by marathon pipe line. A gasket failure on the tank line was initially identified as the leak source. After the completion of the investigation it was determined that the gasket failed due to misalignment during construction. The amount released was calculated based on field investigation data. Boom was initially placed in bauer drain and recovery wells installed to collect free product. Mpl has removed 4,500 tons of non-hazardous impacted soils from this site. This is an on-going remediation effort and the report includes the estimated final remediation costs.
| Report Received Date | 2011-05-13 00:00:00 |
|---|---|
| Iyear | 2011 |
| Report Number | 20110140 |
| Supplemental Number | 20225 |
| Report Type | Supplemental Final |
| Operator Id | 32147 PHMSA Enforcement |
| Name | Marathon Pipe Line Llc |
| Operator Street Address | 539 South Main Street |
| Operator City Name | Findlay |
| Operator State Abbreviation | OH |
| Operator Postal Code | 45840 |
| Local Datetime | 2011-04-13 18:58:00 |
| Location Latitude | 42.514136 Google Maps OpenStreetMap |
| Location Longitude | -84.242059 Google Maps OpenStreetMap |
| Commodity Released Type | Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions |
| Commodity Subtype | Gasoline (Non-Ethanol) |
| Unintentional Release Bbls | 9000 |
| Intentional Release Bbls | 0 |
| Recovered Bbls | 6643 |
| Fatality Ind | No |
| Fatal | 0 |
| Injury Ind | No |
| Injure | 0 |
| Accident Identifier | Notification From Public |
| Incident Identified Datetime | 2011-04-13 18:58:00 |
| System Part Involved | Onshore Terminal/tank Farm Equipment And Piping |
| On Off Shore | Onshore |
| Shutdown Due Accident Ind | Yes |
| Shutdown Datetime | 2011-04-13 19:02:00 |
| Restart Datetime | 2011-04-18 15:20:00 |
| On Site Datetime | 2011-04-13 18:58:00 |
| Nrc Rpt Datetime | 2011-04-13 21:55:00 |
| Nrc Rpt Num | 972904 NRC Report How to search |
| Ignite Ind | No |
| Explode Ind | No |
| Num Pub Evacuated | 0 |
| Pipe Fac Name | Wolverine Pipeline |
| Segment Name | Stockbridge Tank 681 Tank Line |
| Onshore State Abbreviation | Mi |
| Onshore Postal Code | 48819 |
| Onshore City Name | Dansville |
| Onshore County Name | Ingham |
| Designated Location | Milepost/valve Station |
| Designated Name | Stockbridge |
| Federal | No |
| Location Type | Originated On Operator-Controlled Property, But Then Flowed Or Migrated Off The Property |
| Incident Area Type | Underground |
| Incident Area Subtype | Under Soil |
| Depth Of Cover | 24 |
| Crossing | No |
| Pipe Facility Type | Interstate |
| Item Involved | Flange Assembly |
| Installation Year | 2002 |
| Material Involved | Material Other Than Carbon Steel |
| Material Details | Gasket |
| Release Type | Leak |
| Leak Type | Connection Failure |
| Wildlife Impact Ind | No |
| Soil Contamination | Yes |
| Long Term Assessment | No |
| Remediation Ind | Yes |
| Surface Water Remed Ind | Yes |
| Groundwater Remed Ind | Yes |
| Soil Remed Ind | Yes |
| Water Contam Ind | Yes |
| Surface Contam Ind | Yes |
| Groundwater Contam Ind | Yes |
| Amount Released | 1 |
| Rel Water Name | Bauer Drain |
| Could Be Hca | No |
| Commodity Reached Hca | No |
| Est Cost Oper Paid | 0 |
| Est Cost Gas Released | 350000 |
| Est Cost Prop Damage | 193000 |
| Est Cost Emergency | 14885903 |
| Est Cost Environmental | 20300000 |
| Est Cost Other | 0 |
| Prpty | 35728903 |
| Accident Psig | 0 |
| Mop Psig | 0 |
| Accident Pressure | Pressure Did Not Exceed Mop |
| Pressure Restriction Ind | No |
| Pipeline Function | > 20% Smys Regulated Transmission |
| Scada In Place Ind | Yes |
| Scada Operating Ind | Yes |
| Scada Functional Ind | Yes |
| Scada Detection Ind | No |
| Scada Conf Ind | No |
| Cpm In Place Ind | No |
| Investigation Status | Yes, specify investigation result(s): (select all that apply) |
| Invest No Control Room Ind | Yes |
| Invest No Controller Ind | Yes |
| Employee Drug Test Ind | No |
| Contractor Drug Test Ind | No |
| Cause | Equipment Failure |
| Cause Details | Non-Threaded Connection Failure |
| Eq Failure Type | Non-Threaded Connection Failure |
| Other Non Threaded Ind | Gasket |
| Additional Installation Ind | Yes |
| Ief Addl Misalignment Ind | Yes |
| Preparer Name | R**** S******** |
| Preparer Title | Hes Professional |
| Preparer Email | R**********@m****************.com |
| Preparer Telephone | 4194212121 |
| Prepared Date | 2015-03-12 00:00:00 |
| Authorizer Name | R****** B***** |
| Authorizer Telephone | 4194212121 |
| Authorizer Title | Regulatory Compliance Supervisor |
| Authorizer Email | R*******@m****************.com |
| Narrative | Wolverine received a call from a landowner indicating odors and sheen in bauer drain. Wolverine initially responded, later notifying marathon petroleum company. It was determined that the release was from a marathon petroleum company tank line, operated by wolverine. Initial nrc call was made by wolverine. Supplemental nrc reports were made by marathon pipe line. A gasket failure on the tank line was initially identified as the leak source. After the completion of the investigation it was determined that the gasket failed due to misalignment during construction. The amount released was calculated based on field investigation data. Boom was initially placed in bauer drain and recovery wells installed to collect free product. Mpl has removed 4,500 tons of non-hazardous impacted soils from this site. This is an on-going remediation effort and the report includes the estimated final remediation costs. |
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