HL incident on 2011-04-12 — PA

Operator
West Shore Pipeline Co
Cause
Corrosion Failure
Commodity
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Program
HL
Damage and Injuries
0 fatalities 0 injuries
Property damage (nominal)
$23,000
Incident datetime
2011-04-12 10:25
Report number
Location
PA
Narrative
At 6:06 pm on april 12, 2011, a release was identified by a third party customer on the fx999a1 line in green bay, wisconsin. The line was isolated and emergency response procedures were initiated. An estimated 10 barrels of gasoline were released through a pinhole leak. The line has been repaired, tested, and is back in service. An incident investigation is underway and metallurgical analysis on the failed pipe is ongoing. All impacted soil was removed and remediation is ongoing. Update metallurgical analysis indicated the cause of the leak was external pitting corrosion. The corrosion was localized suggesting it was likely associated with an area of disbonded coating. Remediation is ongoing ' however charges have been estimated to cover remediation charges until the close of the process chain of events: 10:25 west shore employees in green bay was notified by US oil of gas vapor in a sanitary sewer in the area of the fox river station. 10:28 west shore employees in green bay contacted the pipeline control center and notified them on the potential release. The pipeline that supplies fox river was already shut down as part of normal operations. 10:32 west shore employees arrived onsite. 10:34 west shore employees met with US oil, green bay city department of public works and the green bay fire department. 11:00 green bay city department of public works ordered a camera crew to site to examine the sewer to determine where product was entering 11:21 osro arrived onsite 12:15 camera crew determines that product is coming from an abandon sewer lateral 12:21 west shore employees places a one call to prepare to dig 14:50 excavation crew arrives on site. 15:50 during excavation contaminated soil was determined. 17:55 nrc was notified 19:15 excavation activities were stopped for the night. 4/13/2011 08:00 shoring onsite and excavation resumed 18:00 night shift starts. Excavation continues 4/14/2011 00:44 leak detected 01:15 PHMSA arrives onsite 02:00 leak clamp installed
Detailed record list
Report Received Date
2011-05-12 00:00:00
Iyear
2011
Report Number
20110138
Supplemental Number
21801
Report Type
Supplemental Final
Operator Id
Name
West Shore Pipeline Co
Operator Street Address
5 Tek Park
Operator City Name
Breinigsville
Operator State Abbreviation
PA
Operator Postal Code
18031
Local Datetime
2011-04-12 08:15:00
Location Latitude
Location Longitude
Commodity Released Type
Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype
Gasoline (Non-Ethanol)
Unintentional Release Bbls
11.9
Intentional Release Bbls
0
Recovered Bbls
2.4
Fatality Ind
No
Fatal
0
Injury Ind
No
Injure
0
Accident Identifier
Other
Accident Details
Third Party Customer
Incident Identified Datetime
2011-04-12 10:25:00
System Part Involved
Onshore Pipeline, Including Valve Sites
On Off Shore
Onshore
Shutdown Due Accident Ind
Yes
Shutdown Datetime
2011-04-10 04:34:00
Restart Datetime
2011-05-07 16:00:00
On Site Datetime
2011-04-12 10:34:00
Nrc Rpt Datetime
2011-04-12 17:55:00
Nrc Rpt Num
Ignite Ind
No
Explode Ind
No
Upstream Valve Type Ind
Remotely Controlled
Downstream Valve Type Ind
Manual
Num Pub Evacuated
0
Pipe Fac Name
Fox River To Us Oil
Segment Name
Fx999a1
Onshore State Abbreviation
Wi
Onshore Postal Code
54303
Onshore City Name
Green Bay
Onshore County Name
Brown
Designated Location
Survey Station No.
Designated Name
964
Federal
No
Location Type
Pipeline Right-Of-Way
Incident Area Type
Underground
Incident Area Subtype
Under Pavement
Depth Of Cover
84
Crossing
No
Pipe Facility Type
Interstate
Item Involved
Pipe
Pipe Type
Pipe Body
Pipe Diameter
10
Pipe Wall Thickness
0.203
Pipe Smys
52000
Pipe Specification
5l X52
Pipe Seam Type
Erw - Low Frequency
Pipe Manufacturer
Kaiser
Pipe Coating Type
Coal Tar
Installation Year
1961
Manufactured Year
1961
Material Involved
Carbon Steel
Release Type
Leak
Leak Type
Pinhole
Wildlife Impact Ind
No
Soil Contamination
Yes
Long Term Assessment
No
Remediation Ind
Yes
Soil Remed Ind
Yes
Water Contam Ind
No
Could Be Hca
Yes
Commodity Reached Hca
Yes
High Pop Ind
Yes
High Pop Yes No
Yes
Est Cost Oper Paid
0
Est Cost Gas Released
0
Est Cost Prop Damage
23000
Est Cost Emergency
10000
Est Cost Environmental
561361
Est Cost Other
0
Prpty
594361
Accident Psig
50
Mop Psig
275
Accident Pressure
Pressure Did Not Exceed Mop
Pressure Restriction Ind
No
Length Segment Isolated
1300
Internal Inspection Ind
No
Tight Mitered Ind
Yes
Other Inspection Ind
Yes
Internal Inspection Details
No Launch Or Receipt Traps Currently Installed
Operation Complications Ind
No
Pipeline Function
< 20% Smys Regulated Transmission
Scada In Place Ind
No
Cpm In Place Ind
No
Investigation Status
No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind
No
Contractor Drug Test Ind
No
Cause
Corrosion Failure
Cause Details
External Corrosion
Internal External
External Corrosion
Visual Exam Results
Localized Pitting
Galvanic Corrosion Ind
Yes
Metallurgical Basis Ind
Yes
Underground Location
Yes
Under Cathodic Protection Ind
Yes
Cathodic Pro Start Year
1966
Shielding Evident
Yes
Cathodic Survey Type
Yes
Cp Annual Survey Ind
Yes
Close Interval Survey Ind
Yes
Cp Annual Survey Year
2010
Close Interval Survey Year
2009
Prior Damage
Yes
Collected Data Ind
No
Has Hydrtst Conduc Before Ind
Yes
Hydrtst Most Rcnt Year
2009
Hydrtst Most Rcnt Pressure
397
Direct Asmnt Conducted
No
Non Destructive Exam Ind
No
Preparer Name
M***** E*****
Preparer Title
Sr. District Compliance Specialist
Preparer Email
M******@b******.com
Preparer Telephone
2197968230
Prepared Date
2016-10-27 00:00:00
Authorizer Name
C****** P********
Authorizer Telephone
610-904-4113
Authorizer Title
Director Regulatory Compliance
Authorizer Email
C**********@b******.com
Narrative
At 6:06 pm on april 12, 2011, a release was identified by a third party customer on the fx999a1 line in green bay, wisconsin. The line was isolated and emergency response procedures were initiated. An estimated 10 barrels of gasoline were released through a pinhole leak. The line has been repaired, tested, and is back in service. An incident investigation is underway and metallurgical analysis on the failed pipe is ongoing. All impacted soil was removed and remediation is ongoing. Update metallurgical analysis indicated the cause of the leak was external pitting corrosion. The corrosion was localized suggesting it was likely associated with an area of disbonded coating. Remediation is ongoing ' however charges have been estimated to cover remediation charges until the close of the process chain of events: 10:25 west shore employees in green bay was notified by US oil of gas vapor in a sanitary sewer in the area of the fox river station. 10:28 west shore employees in green bay contacted the pipeline control center and notified them on the potential release. The pipeline that supplies fox river was already shut down as part of normal operations. 10:32 west shore employees arrived onsite. 10:34 west shore employees met with US oil, green bay city department of public works and the green bay fire department. 11:00 green bay city department of public works ordered a camera crew to site to examine the sewer to determine where product was entering 11:21 osro arrived onsite 12:15 camera crew determines that product is coming from an abandon sewer lateral 12:21 west shore employees places a one call to prepare to dig 14:50 excavation crew arrives on site. 15:50 during excavation contaminated soil was determined. 17:55 nrc was notified 19:15 excavation activities were stopped for the night. 4/13/2011 08:00 shoring onsite and excavation resumed 18:00 night shift starts. Excavation continues 4/14/2011 00:44 leak detected 01:15 PHMSA arrives onsite 02:00 leak clamp installed
Report Received Date 2011-05-12 00:00:00
Iyear 2011
Report Number 20110138
Supplemental Number 21801
Report Type Supplemental Final
Operator Id 22430 PHMSA Enforcement
Name West Shore Pipeline Co
Operator Street Address 5 Tek Park
Operator City Name Breinigsville
Operator State Abbreviation PA
Operator Postal Code 18031
Local Datetime 2011-04-12 08:15:00
Location Latitude 44.5311 Google Maps OpenStreetMap
Location Longitude -88.0121 Google Maps OpenStreetMap
Commodity Released Type Refined And/or Petroleum Product (Non-Hvl) Which Is A Liquid At Ambient Conditions
Commodity Subtype Gasoline (Non-Ethanol)
Unintentional Release Bbls 11.9
Intentional Release Bbls 0
Recovered Bbls 2.4
Fatality Ind No
Fatal 0
Injury Ind No
Injure 0
Accident Identifier Other
Accident Details Third Party Customer
Incident Identified Datetime 2011-04-12 10:25:00
System Part Involved Onshore Pipeline, Including Valve Sites
On Off Shore Onshore
Shutdown Due Accident Ind Yes
Shutdown Datetime 2011-04-10 04:34:00
Restart Datetime 2011-05-07 16:00:00
On Site Datetime 2011-04-12 10:34:00
Nrc Rpt Datetime 2011-04-12 17:55:00
Nrc Rpt Num 972765 NRC Report How to search
Ignite Ind No
Explode Ind No
Upstream Valve Type Ind Remotely Controlled
Downstream Valve Type Ind Manual
Num Pub Evacuated 0
Pipe Fac Name Fox River To Us Oil
Segment Name Fx999a1
Onshore State Abbreviation Wi
Onshore Postal Code 54303
Onshore City Name Green Bay
Onshore County Name Brown
Designated Location Survey Station No.
Designated Name 964
Federal No
Location Type Pipeline Right-Of-Way
Incident Area Type Underground
Incident Area Subtype Under Pavement
Depth Of Cover 84
Crossing No
Pipe Facility Type Interstate
Item Involved Pipe
Pipe Type Pipe Body
Pipe Diameter 10
Pipe Wall Thickness 0.203
Pipe Smys 52000
Pipe Specification 5l X52
Pipe Seam Type Erw - Low Frequency
Pipe Manufacturer Kaiser
Pipe Coating Type Coal Tar
Installation Year 1961
Manufactured Year 1961
Material Involved Carbon Steel
Release Type Leak
Leak Type Pinhole
Wildlife Impact Ind No
Soil Contamination Yes
Long Term Assessment No
Remediation Ind Yes
Soil Remed Ind Yes
Water Contam Ind No
Could Be Hca Yes
Commodity Reached Hca Yes
High Pop Ind Yes
High Pop Yes No Yes
Est Cost Oper Paid 0
Est Cost Gas Released 0
Est Cost Prop Damage 23000
Est Cost Emergency 10000
Est Cost Environmental 561361
Est Cost Other 0
Prpty 594361
Accident Psig 50
Mop Psig 275
Accident Pressure Pressure Did Not Exceed Mop
Pressure Restriction Ind No
Length Segment Isolated 1300
Internal Inspection Ind No
Tight Mitered Ind Yes
Other Inspection Ind Yes
Internal Inspection Details No Launch Or Receipt Traps Currently Installed
Operation Complications Ind No
Pipeline Function < 20% Smys Regulated Transmission
Scada In Place Ind No
Cpm In Place Ind No
Investigation Status No, the facility was not monitored by a controller(s) at the time of the accident
Employee Drug Test Ind No
Contractor Drug Test Ind No
Cause Corrosion Failure
Cause Details External Corrosion
Internal External External Corrosion
Visual Exam Results Localized Pitting
Galvanic Corrosion Ind Yes
Metallurgical Basis Ind Yes
Underground Location Yes
Under Cathodic Protection Ind Yes
Cathodic Pro Start Year 1966
Shielding Evident Yes
Cathodic Survey Type Yes
Cp Annual Survey Ind Yes
Close Interval Survey Ind Yes
Cp Annual Survey Year 2010
Close Interval Survey Year 2009
Prior Damage Yes
Collected Data Ind No
Has Hydrtst Conduc Before Ind Yes
Hydrtst Most Rcnt Year 2009
Hydrtst Most Rcnt Pressure 397
Direct Asmnt Conducted No
Non Destructive Exam Ind No
Preparer Name M***** E*****
Preparer Title Sr. District Compliance Specialist
Preparer Email M******@b******.com
Preparer Telephone 2197968230
Prepared Date 2016-10-27 00:00:00
Authorizer Name C****** P********
Authorizer Telephone 610-904-4113
Authorizer Title Director Regulatory Compliance
Authorizer Email C**********@b******.com
Narrative At 6:06 pm on april 12, 2011, a release was identified by a third party customer on the fx999a1 line in green bay, wisconsin. The line was isolated and emergency response procedures were initiated. An estimated 10 barrels of gasoline were released through a pinhole leak. The line has been repaired, tested, and is back in service. An incident investigation is underway and metallurgical analysis on the failed pipe is ongoing. All impacted soil was removed and remediation is ongoing. Update metallurgical analysis indicated the cause of the leak was external pitting corrosion. The corrosion was localized suggesting it was likely associated with an area of disbonded coating. Remediation is ongoing ' however charges have been estimated to cover remediation charges until the close of the process chain of events: 10:25 west shore employees in green bay was notified by US oil of gas vapor in a sanitary sewer in the area of the fox river station. 10:28 west shore employees in green bay contacted the pipeline control center and notified them on the potential release. The pipeline that supplies fox river was already shut down as part of normal operations. 10:32 west shore employees arrived onsite. 10:34 west shore employees met with US oil, green bay city department of public works and the green bay fire department. 11:00 green bay city department of public works ordered a camera crew to site to examine the sewer to determine where product was entering 11:21 osro arrived onsite 12:15 camera crew determines that product is coming from an abandon sewer lateral 12:21 west shore employees places a one call to prepare to dig 14:50 excavation crew arrives on site. 15:50 during excavation contaminated soil was determined. 17:55 nrc was notified 19:15 excavation activities were stopped for the night. 4/13/2011 08:00 shoring onsite and excavation resumed 18:00 night shift starts. Excavation continues 4/14/2011 00:44 leak detected 01:15 PHMSA arrives onsite 02:00 leak clamp installed

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